ML15224A695

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Insp Repts 50-269/90-17,50-270/90-17 & 50-287/90-17 on 900520-0616.Violations Noted.Major Areas Inspected:Maint Activities,Operations,Surveillance Testing & Unmonitored Discharge from Unit 1 Vent & Plant Startup from Refueling
ML15224A695
Person / Time
Site: Oconee  
Issue date: 06/26/1990
From: Binoy Desai, Shymlock M, Skinner P, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15224A693 List:
References
50-269-90-17, 50-270-90-17, 50-287-90-17, GL-88-14, NUDOCS 9007170295
Download: ML15224A695 (15)


See also: IR 05000269/1990017

Text

UNITED STATES

0G

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-269/90-17, 50-270/90-17, 50-287/90-17

Licensee: Duke Power Company

422 South Church Street

Charlotte, N.C.

28242

Docket Nos.:

50-269, 50-270, 50-287

License Nos.:

DPR-38, DPR-47, DPR-55

Facility Name:

Oconee Nuclear Station

Inspection Conducted:

May 20 - June 16, 1990

Inspectors:

V/

P. H. Skinner, Senior esident Inspector

Date Signed

L. D. Wert, Resident

nspector

B. .

esal, Residen7Inspector

Date Signed

Approved by:

_

_

_

_

___

_

__

_

M. B. Shymlock, Section Chief

Date Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection involved inspection on-site in

the

areas of operations, surveillance testing, maintenance

activities, an unmonitored discharge from the Unit 1 vent, and plant

startup from refueling.

Results:

One apparent violation was identified involving the Penetration Room

Ventilation System. The inspectors identified that the system would

be inoperable under certain accident conditions (paragraph 5).

It

was also noted during this review that the licensee's response to

Generic Letter (GL)

88 -

14, Instrument Air Supply System Problems

Affecting Safety Related Equipment, was inadequate (paragraph 5).

A violation was cited for failure to follow procedures involving

calibration

and testing of the Reactor Protection System

(paragraph 3.b).

Three Non-cited Violations (NCV) were identified:

-

Violation of Technical Specifications regarding radioactive

effluent monitoring (paragraph 6).

2

-

Inoperability of the Safe Shutdown Facility Makeup.System due

to a mispositioned valve (paragraph 8).

-

Violation of Technical Specifications associated with Upper

Surge Tank minimum level requirements (paragraph 2.b).

A weakness was noted in the control of scaffolding over

safety-related equipment (paragraph 4.b).

REPORT DETAILS

1. Persons Contacted

Licensee Employees

B. Barron, Station Manager

D. Couch, Keowee Hydrostation Manager

  • T. Curtis, Compliance Manager

J. Davis, Technical Services Superintendent

D. Deatherage, Operations Support Manager

  • B. Dolan, Design Engineering Manager, Oconee Site Office
  • W. Foster, Maintenance Superintendent
  • T. Glenn, Engineering Supervisor

D. Hubbard, Performance Engineer

E. LeGette, Compliance Engineer

  • C. Little, Instrument and Electrical Manager
  • H. Lowery, Chairman, Oconee Safety Review Group

B. Millsap, Maintenance Engineer

  • D. Powell, Station Services Superintendent
  • G. Rothenberger, Integrated Scheduling Superintendent
  • R. Sweigart, Operations Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors:

a

Skinner

  • L. Wert
  • B. Desai
  • Attended exit interview.

2.

Plant Operations (71707)(71710)

a. The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements, Technical

Specifications (TS), and administrative controls. Control room logs,

shift turnover records,

temporary modification log and equipment

removal and restoration records were reviewed routinely.

Discussions

were conducted with plant operations, maintenance, chemistry, health

physics, instrument and electrical (I&E), and performance personnel.

Activities within the control rooms were monitored on an almost daily

basis.

Inspections were conducted on day and on night shifts during

weekdays and on weekends.

Some inspections were made during shift

change in order to evaluate shift turnover performance.

Actions

observed were conducted as required by the licensee's Administrative

Procedures.

The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS.

Operators were

2

responsive to plant annunciator alarms and were cognizant of plant

conditions.

During this report period, the inspectors reviewed the licensee's

posting of Notices to workers required by 10 CFR 19.11.

Several

minor discrepancies were noted concerning a security violation issued

on December 21, 1989.

The

licensee promptly corrected the

deficiencies.

Plant tours were taken throughout the reporting period on a routine

basis.

The areas toured included the following:

Turbine Building

Auxiliary Building

CCW Intake Structure

Independent Spent Fuel Storage Facility

Units 1, 2, and 3 Electrical Equipment Rooms

Units 1, 2, and 3 Cable Spreading Rooms

Units 1, 2, and 3 Penetration Rooms

Unit 1 Containment

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Units 1, 2, and 3 Spent Fuel Pool Rooms

Keowee Hydro Station

During the plant tours, ongoing activities, housekeeping, security,

equipment status, and radiation control practices were observed.

During this report period, the inspector walked down the Penetration

Room Ventilation (PRV)

System in accordance with the requirements of

Inspection Procedure

71710:

Engineered Safety Feature System

Walkdown.

Paragraph 5 contains further details of the results of

this inspection.

Additionally the inspectors completed detailed

walkdowns

of

safety-related

portions

of

the

following

systems/locations:

Unit 1 Reactor Building Spray System

Unit 1 High Pressure Injection Pump Rooms

Unit 1 Emergency Feedwater System

Unit 1/2 Low Pressure Service Water

Unit 1 East Penetration Room

Minor discrepancies

noted were communicated to the licensee.

Paragraph 7 contains details of the East Penetration Room Walkdown.

-

Unit 1 entered this reporting period in a refueling outage.

On

June 5, the unit was taken critical, and on June 6, the

generator was

closed onto the grid and power escalation

commenced.

3

b. Units 2 and 3 operated at 100 percent power for the duration of

the report period.

b.

Upper Surge Tank Low Level During Hot Shutdown Operations On. Unit 1

On June 4, 1990, at approximately 9:15 a.m.,

the Control

Room

Operator (CRO) observed a rapid increase in Condensate Storage Tank

(CST)

level and an associated decrease in Upper Surge Tank (UST)

level.

The level in the UST was noted to be 5.85 feet which was

below the TS 3.4.4 lower limit of 6 feet.

Secondary makeup was

immediately commenced to increase level to above TS requirements.

The level was returned to greater than 6 feet at approximately

9:50 a.m.

Investigation into this problem by the inspectors and licensee

personnel identified that the condensate and feedwater systems were

in a "condensate cleanup" mode.

This recirculates water from the

hotwell,

through the condensate system, and back to the hotwell.

Unit 1 at this time was also transferring water from the Unit 1 CST

to the Unit 3 CST.

Upon completion of the transfer to Unit 3, the

transfer pump was secured.

At the same time, a reduction in steam

supply to one of the secondary system heaters occurred.

These

actions appear to have caused the rapid level changes.

The level in

the UST reached a low level indication of approximately 4 feet.

The

licensee is continuing the investigation of this problem and will

submit an LER in accordance with 10 CFR 50.73(a)(2)(i)(B).

TS 3.4.4 requires a minimum of 6 feet of water to be available in the

UST.

Following this occurrence, this TS was discussed in detail.

The TS is unclear as to what applicable plant conditions must be in

effect for this requirement.

The licensee is reviewing the adequacy

of this TS and will consider submittal of a revision to clarify the

applicable plant conditions.

The failure to maintain UST levels greater than 6 feet as required by

TS 3.4.4 is being identified as non-cited violation

(NCV),

50-269/90-17-03:

Failure to Maintain Level In UST Above 6 Feet.

This licensee-identified violation is not being cited because

criteria specified in Section V.G.1 of the NRC Enforcement Policy

were satisfied.

One violation was identified.

3.

Surveillance Testing (61726)

a. Surveillance tests were reviewed

by the inspectors to verify

procedural and performance adequacy.

The completed tests reviewed

were

examined for necessary test prerequisites,

instructions,

acceptance criteria, technical content, authorization to begin work,

data collection, independent verification where required, handling of

deficiencies noted,

and review of completed work.

The tests

4

witnessed, in whole or in part, were inspected to determine that

approved procedures were available, test equipment was calibrated,

prerequisites were met, tests were conducted according to procedure,

test results were acceptable, and systems restoration was completed.

The following surveillances were reviewed and witnessed in whole or

in part:

PT/O/A/0610/06

100KV Power Supply From Lee Steam Station

OP/1/A/1106/06

Turbine Driven Emergency Feedwater Pump

Overspeed Testing

PT/1/A/0600/12

Turbine Driven Emergency Feedwater Pump

Performance Test

PT/3/A/0600/12

Turbine Driven Emergency Feedwater Pump

Performance Test

IP/O/A/0330/003A

Control Rod Drive Drop Time Test

PT/1/A/0150/15D

Intersystem LOCA Leak Test

PT/1/A/0261/07

Emergency CCW System Flow Test

PT/1/A/251/19

Main Steam Block Valve Leakage

PT/3/A/0203/06

Low Pressure Injection System Performance

Test

TT/T/A/0711/13

Unit 1 Cycle 13 Zero Power Physics Test

(ZPPT)

PT/O/A/0290/002

Main Steam Stop Valve Closure Time

b. Reactor Protection System Instrumentation Problems Unit 2

On June 4, 1990, Reactor Protection System (RPS) channel C for Unit 2

tripped due to a signal from the flux/flow -

imbalance circuitry. An

investigation by operations personnel indicated that the flux/flow

imbalance was within the TS required criteria and that the signal was

due to a spurious actuation of the instrumentation.

The signal had

returned to normal indications and the channel was reset.

A work

request

(WR)

was written for I&E personnel to troubleshoot the

channel

as necessary..

I&E technicians performed

checks of the

channel later on June 4 but did not identify any faults.

On June 5,

recorders were connected to various inputs to the channel to provide

additional data for further analysis.

On June 6, a WR was generated by I&E Engineering requesting that RPS

channel A loop

'B'

flow transmitter be calibrated since flow

deviations had increased slowly since unit startup. On June 11, I&E

technicians commenced a calibration on RPS channel A flow instrument

in accordance with Instrument Procedure (IP)/2/A/3n5/PI dated

October 2, 1989.

This calibration requires an entry into containment

to connect a test device to the sensing element and to introduce test

signals at the device while recording results at the RPS instrumen

tation cabinet.

This action was performed in accordance with step

5

10.8.7 of IP/2/A/305/1I,

and data was taken as required.

The data

taken was not within the tolerance specified by the procedure. The

supervisor in charge of the test was confused due to the abnormal

readings obtained and felt that the test equipment was in error. He

stopped the procedure in progress, disconnected the test gear, and

after review of the existing parameters and discussion with the unit

supervisor, he concluded the channel was operable and placed it back

in service.

Following this work

on channel A, I&E personnel

commenced a

calibration RPS channel C since the I&E engineer had identified from

the instruments installed on June 5 that the flow channel was

operating on the low side.

Using the same equipment that was used on

channel A, RPS

channel C was calibrated in accordance with

IP/2/A/305/1K dated September 22, 1989. The I&E supervisor then went

back to the procedure used for channel A and re-evaluated the

results, discussed this evaluation with an I&E Engineer and then

declared the channel out of service.

The inspector reviewed the WRs involved in these calibrations.

The

review identified that during the calibration of channel A, I&E

technicians did not follow the required

steps in procedure

IP/2/A/305/1I.

After completion of step 11.8.7, which was performed

and resulted in out of tolerance readings,

the next step is to

perform individual component calibration as appropriate until the

error is found and corrected.

Since this step was not performed, an

RPS channel

was placed in operation although the calibration

indicated the channel was not functioning properly. This resulted in

a violation of TS 3.5.1.1 in that the minimum channels operable

(Table 3.5.1-1) for RPS flow imbalance instruments was not met.

Channel A had been declared operable in error,

and Channel C was

removed for calibration purposes.

Station Directive 3.1.2,

Activities Affecting Station Operation, dated April 27, 1990, section

4.1, identifies that some items are clearly inoperable upon initial

discovery and provides as an example a device failing to meet

quantitative acceptance criteria such as a calibration.

TS 6.4.1

requires the plant to be operated in accordance with approved

procedures.

The failure to follow procedure IP/2/A/305/1I

is

identified as violation 50-270/90-17-02:

Failure to Follow

Procedures Resulting in Violation of TS 3.5.1.1.

One violation was identified.

4. Maintenance Activities (62703)

a. Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures in use adequately described

work that was not within the skill of the trade.

Activities,

6

procedures,

and work requests were examined to verify proper

authorization to begin work, provisions for fire, cleanliness, and

exposure control, proper return of equipment to service, and that

limiting conditions for operation were met.

The following maintenance was reviewed and witnessed in whole or in

part:

O/MP/3009/14

RBCU Fusible Patches Preventive Maintenance

Inspection and Functional Test

WR 50868J

1C-391 Repairs

WR 57113D

Preventive Maintenance on Main Steam Emergency

Feedwater Turbine

WR 98722C

Installation of OE-3049, Increase '3C' LPI Pump

Recirculation Loop Flow Orifice

b. Concerns Regarding Use of Scaffolds Above Safety-Related Components

On June 6, 1990, the inspector observed a large multi-level scaffold

erected over the Unit 3 Turbine Driven Emergency Feedwater Pump. A

tag on the scaffold indicated it may have been in place as early as

April 17, 1990.

It was built to enable repairs to be conducted on a

plant heating system valve. The scaffold was not tied off to prevent

falling or movement into safety-related equipment.

The licensee

subsequently identified that the work had been completed and removed

the scaffold.

Since several other examples of scaffolding concerns had been noted

during this inspection period (see paragraph 7),

the inspectors

discussed control

of scaffolding with maintenance engineering

personnel.

From these discussions (along with the examples noted

above), the inspector concluded that the installation of scaffolding

near safety-related equipment is not formally controlled at Oconee.

Apparently,

in most cases,

scaffolding erected over or near

safety-related equipment is inspected by a coordinator in the

maintenance engineering department, but since the program is

informal,

numerous scaffolds are erected without this coordinator's

knowledge.

The bulk of the problems appear to be caused by a failure

to promptly remove scaffolding once the task is completed.

The

inspectors noted that significant improvements

have been made

recently in the quality of scaffolding construction and attention to

details concerning safety on and near scaffolding.

Station and maintenance management acknowledged that the controls on

scaffolding could be more rigid. The inspectors were informed that a

task force has been established to develop some basic guidance and

criteria to

be utilized to ensure scaffolding erected over

safety-related equipment will not hazard the operability of that

equipment.

The inspectors will continue to closely follow the

licensee's actions in this area.

7

No violations or deviations were identified.

5. Penetration Room Ventilation System Inoperable Under Certain Conditions

Due To Inadequate Design (71710)(71707)

On June 12,

1990, while in the process of performing a detailed walkdown

of the Reactor Building Penetration Room Ventilation (PRV)

System, the

inspectors identified an apparent design error which could render the

system inoperable under specific circumstances.

The PRV system is

designed to minimize the levels of radioactive materials released to the

environment due to post-accident Reactor Building

(RB)

leakage.

The

system functions by pulling RB leakage (maintains negative pressure in

penetration rooms after an accident) into the two penetration rooms and

passing it

through a pair of filter trains.

Each train consists of a

particulate prefilter, an absolute (HEPA) filter, and a charcoal filter in

series. A fan downstream of each filter train discharges the filtered air

through a common

discharge line to the unit vent for release to

atmosphere.

The filter trains and fans are redundant; only one fan and

one filter train is required to accomplish the system's safety function.

The fans are actuated on an Engineered Safeguards (ES)

signal (Channels 5

and 6, high RB pressure).

The fan discharge valves PR-15 and PR-19

automatically open when the fans start.

In addition to local gages which display differential pressure across the

different filter assemblies,

there is a remote display (located just

outside the room that contains the PRV system)

of air flow at the

discharge of each filter train. Adjacent to each of these flow gages is a

manual loader to permit control of the system flow control valves,

1PR-13

and 1PR-17 (filter discharge valves).

In the control room (CR), PRV fan

and fan discharge valve status indications are available.

Penetration

Room pressure and excessive or insufficient vacuum annunciators are also

available in the CR.

TS 3.15.1 requires that two trains of the PRV system shall be operable at

all times when containment integrity is required or the reactor shall be

shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

(A 7-day limiting condition for operation is

permitted if

only one train is inoperable provided that all active

components of the other train have been demonstrated to be operable.)

The principle discrepancy noted during the walkdown inspection was that

the flow control valves, PR-13 and PR-17, appeared to be designed to fail

shut on a loss of instrument air (IA) pressure to their controllers. IA

is a non-safety non-seismic system at Oconee. Additional related concerns

noted by the inspectors during followup investigation include:

-

There is not a readily available means to override or manually

position the valves open if they were required and air pressure was

not available to their operators.

8

-

The operation of these valves (or the PRV system) is not addressed in

Abnormal Procedure AP/1,2,3/1700/22:

Loss of Instrument Air.

-

Table 6.5-2 of the FSAR; Single Failure Analysis for the PRV system

states that on a loss of IA to the remote loaders, PR-13 and PR-17

fail open.

-

The licensee's response to GL-88-14:

Instrument Air System Problems

Affecting Safety Related Equipment, did not address valves PR-13 and

PR-17.

The inspectors concluded that portions of this response may

not be complete to ensure that all air-operated safety-related

components will perform

as

expected in accordance with all

design-basis events including a loss of the normal instrument air

system.

-

The inspectors noted a report indicating that a study completed by

the licensee's DE group had identified that these valves would fail

shut on a loss of IA resulting in a loss of the PRV system.

Apparently the significance of this data was overlooked.

The inspectors discussed their concerns regarding the failure position of

PR-13 and PR-17 on a loss of air pressure with the PRV system accountable

engineer and the Operations Support group.

After review by DE,

at

5:00 p.m., on June 13, 1990, the license declared the PRV system inoper

able for a LOCA scenario with a loss of IA to the valves.

At 5:45 p.m.,

the licensee reported this issue in accordance with

10 CFR 50.72

(b)(1)(ii)(B).

The licensee exited the 12-hour LCO on each unit after a

Temporary Station Modification (TSM)

was installed which blocked PR-13

open (such as it would not fail shut on a loss of air pressure),

and the

system was tested.

The 7 day LCO on the remaining train was subsequently

exited after PR-17 was blocked open on each unit.

Incorporating design

basis requirements into the design and operation of safety systems is

essential to ensuring those systems will be able to perform their intended

function when called upon

and

is required

by Criterion III of

10 CFR Part 50, Appendix B.

This design inadequacy is an apparent

violation and is identified as violation 50-269,270,287/90-17-01:

Penetration Room Ventilation System Inoperable Under Certain Conditions

Due to Design Deficiencies.

One apparent violation was identified.

6. Unmonitored Discharge From Unit Vent

At about 10:00 p.m.,

on May 18,

1990,

the licensee identified that the

portable sampler being used for Particulate and Iodine activity sampling

had been removed from service for a 12-hour period. The portable sampler

was being used since the regular monitors were being modified.

9

Review of this event identified that the Unit 1 installed Particulate and

Iodine samplers (RIA 43 and 44) were being replaced during the outage in

progress. In preparation for the Nuclear Station Modification (NSM) being

implemented,

a portable sampler was connected to the piping associated

with the installed units as allowed by TS 3.5.5.2(c) since the electrical

portion of the system had been disconnected.

The portable sampler was

connected into the sample piping of the monitor. Since the sample piping

was to be modified, an alternate portable sample system had been staged in

the area of the first portable sampler, except it could not be connected

to take a sample until a new connection to the stack had been installed.

Due to a communication problem,

the alternate portable sampler sample

lines were connected at the pump,

and the pump was started for sampling

purposes.

The sample lines to the vent stack had not been connected.

This was identified by the Technical Engineer responsible for the NSM. He

immediately notified Radiation Protection (RP) personnel.

RP started the

portable sampler which was still connected to the system and obtained the

required sample.

The licensee reviewed all discharges into the vent

system and determined no abnormal activity had been exhausted to the

system in the previous 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. A report will be submitted to the NRC in

accordance with 10 CFR 50.73(a)(2)(B).

TS 3.5.5.2(c) allows the continuation of effluent releases when the normal

monitoring instrumentation is unavailable provided auxiliary sampling

equipment is used for continuous sample collection.

This failure to

provide for continuous sample collection is identified as non-cited

violation

(NCV)

50-269/90-17-04:

Failure to Provide for Continuous

Sampling of the Unit Ventilation Effluent.

This licensee identified violation is not being cited because criteria

specified in Section V.G.1 of the NRC Enforcement Policy were satisfied.

The actions taken by the licensee are considered to be acceptable for this

incident.

Subsequent review during the modifications to Units 2 and 3

will be performed by the inspectors to further assess the adequacy of the

licensee's corrective actions.

7. Plant Startup From Refueling (71711) (Unit 1)

On June 1, 1990,

following a 41-day, EOC-12,

refueling outage, Unit 1

exceeded 200 degrees F. Hot shutdown conditions were reached on June 3,

1990.

The inspectors witnessed portions of PT/0/A/0290/002, Main Steam

Stop Valve Closure Time Test, and IP/0/A/0330/3A, Control Rod Drive Trip

Test.

The test results were within the acceptance criteria of these

procedures. The inspectors witnessed in part TT/1/A/0711/13, Unit 1 Cycle

13 Zero Power Physics Test, which commenced on June 5, 1990.

The measured

10

total worth of rod group 5, 6, and 7 was determined to be 10.6 percent

greater than the predicted worth.

Since the acceptance criteria is

plus/minus 10 percent of predicted, the worth of rod group 4 had to be

measured.

The total worth of rod groups 4, 5, 6, and 7 was within the

acceptance criteria.

In addition, on June 4, 1990,

the inspectors toured the Unit 1 East

Penetration Room.

Unit 1 was in hot shutdown conditions, proceeding with

reactor startup.

Among the significant discrepancies noted were the

following items:

-

Several examples of scaffolding (not being utilized for work in

progress)

over safety-related equipment were identified.

One

scaffold was against the air operator on valve 1FDW-315,

Emergency

Feedwater flow control valve.

-

Several examples of unsealed or unprotected safety-related cabling

terminal box connections including a missing junction box cover were

identified.

-

Several examples of poor -cable connections (metal sheathing not

properly attached)

involving safety-related power operated valves

were identified.

  • -

Two High Pressure Injection system vent or drain valve pipe caps were

found not installed, and two minor packing leaks were identified.

The discrepancies were discussed with station management.

Corrective

actions were initiated immediately. The scaffolding which was not being

utilized was removed from the Penetration Room or moved away from

safety-related equipment.

Work Requests were initiated to correct the

cabling and junction box discrepancies, the packing leaks, and several

other discrepancies. By June 6, the licensee informed the inspectors that

all of the cabling discrepancies had been corrected, work was initiated to

build a terminal

box cover,

and Work Requests written on other

discrepancies not yet fully resolved. Followup discussions on scaffolding

issues are described in paragraph 4.b of this report.

When attempts were made to synchronize the generator to the grid on

June 6,

the turbine control

valves did not respond as expected.

Apparently,

a small stator coolant leak was wetting some electrical

contacts in the EHC cabinet.

This caused a stator coolant runback

circuitry relay to stick which prevented the turbine speed from

increasing.

Following repairs, the generator was placed on line at 8:26

p.m.

Power was gradually escalated and was held at 93 percent due to

problems with the 102 heater drain pump motor.

The unit reached power

approximately 98 percent and operated at that level for the remainder of

the report period.

No violations or deviations were identified.

11

8. Valve SSF-1HP-405 Found Open (71707)

On June 6, 1990, at approximately 8:00 p.m., a non-licensed operator (NLO)

making rounds in the Safe Shutdown Facility (SSF)

discovered that valve

SSF-1HP-405 was open.

This valve is utilized for testing and is located

on the discharge side of the SSF Makeup Pump in a recirculation line. The

valve should be normally shut so the the makeup pump discharges into the

Reactor Coolant Pump (RCP) seal injection lines for reactor coolant system

(RCS) inventory makeup.

The SSF is a separate bunkered installation designed to provide an

alternate secure means for attaining and maintaining hot shutdown

conditions on all three Oconee units.

It was intended for incidents of

sabotage, fires, and some flooding scenarios.

The SSF systems are

manually actuated and are to be utilized only if the installed normal and

emergency systems are inoperable.

The primary makeup portion of the SSF

is designed to maintain the RCS filled to sufficient pressurizer level to

assure natural circulation and core cooling.

Following the postulated SSF event, once the decision has been made to

utilize the SSF,

operators will start the SSF diesel generator and shut

SSF controlled RB isolation valves. Next, the breakers for the SSF makeup

pump and makeup system valves are closed, and the makeup pump is started.

The procedure (OP/O/A/1600/11:SSF Emergency Operating Procedure) does not

require closing in of the breaker associated with SSF-1HP-405 since the

valve is supposed to be maintained shut and is only utilized for testing

purposes.

Valve SSF-1HP-417 is a separate recirculation line to permit

reduced RCS makeup flowrate once pressurizer level is recovered and

stable.

The mispositioned SSF-1HP-405 was discovered through a routine Unit 1 SSF

Control Room panel alarm test. The NLO noted that the annunciator for the

"RC Makeup Containment Not Isolated" alarm would not light, replaced the

light bulb, and found the alarm locked in. With the assistance of other

operators and supervisors it was determined that the alarm was caused by

SSF-1HP-405 being left open.

Subsequently, the valve was closed and the

breaker reopened.

Additional information was gained through followup

investigation by the licensee and the inspectors;

-

Apparently there was some problem with the SSF CR annunicator. The

alarm condition had not been noted despite several other NLO rounds

being completed. After SSF-1HP-405 was shut, it was noted the alarm

would again not test.

A Work Request was initiated to repair the

alarm circuit.

-

SSF-1HP-405 had been left open after a test of the Unit 1 SSF RC

makeup pump manual override circuitry had been completed late in the

refueling outage.

This test was completed by

I&E utilizing

is

IP/O/A/0100/001, Troubleshooting and Corrective Maintenance, and an

12

accompanying checklist of instructions.

The procedure was not

adequate to control the work process and ensure the system was

restarted after testing.

Unit 3 had completed the same test during its most recent outage

utilizing IP/3/A/0370/004,

SSF Unit 3 Makeup Pump Manual Override

Circuitry Test,

(a specific procedure to address this test).

However,

the inspectors noted that this procedure incorrectly

required SSF-1HP-405 to be left open at the end of the test.

Additionally the inspectors noted statements in the safety evaluation

for this procedure which were incorrect.

Apparently these incorrect/inadequate procedures have not been a

problem with earlier tests because additional procedures were

performed after this test which shut SSF-1HP-405 prior to unit

startup.

Due to the location of the

SSF makeup flow detector,

the

mispositioned valve would be hard to detect.

Since its breaker is

not required to be shut, no SSF CR indication is available. If the

valve breaker was shut an interlock with the pump would cause the

valve to automatically shut.

SSF-1HP-405 is a containment isolation valve but the actions required

by TS 3.6.3c were already met since there are additional valves in

the system which were deenergized and shut.

The inspectors noted that NUREG/CR-5006, PRA Applications Program for

Inspection at Oconee Unit 3, specifically discusses a failure to shut

SSF-1HP-405 after testing as a condition which could lead to failure

of the SSF HPI system.

The licensee submitted a set of proposed TS addressing the SSF which have

not yet been approved by the staff.

Proposed TS 3.18.3 requires the SSF

RCS Makeup System to be operable for each unit at or above 250 degrees F.

SSF-1HP-405 being open significantly affected the ability of the Unit 1

SSF Makeup Pump to accomplish its intended function.

The SSF makeup system is required to be operable in order for the Oconee

units to achieve and maintain hot shutdown conditions in certain

postulated met. This issue will be addressed as NCV 50-269/90-17-05:

SSF

Makeup Pump Inoperable Due to Mispositioned Valve.

This licensee

identified violation is not being cited because criteria specified in

Section V.G.1 of the NRC Enforcement Policy were satisfied.

13

9. Exit Interview (30703)

The inspection scope and findings were summarized on June 18, 1990, with

those persons indicated in paragraph 1 above.

The inspectors described

the areas inspected and discussed in detail the inspection findings. The

licensee did not identify as proprietary any of the material provided to

or reviewed by the inspectors during this inspection.

Item Number

Description and Reference

VIO 269,270,287/90-17-01

Penetration

Room

Ventilation

System

Inoperable Under Certain Conditions Due to

Design Deficiencies (paragraph 5)

VIO 270/90-17-02

Failure to Follow Procedures Resulting in

Violation of TS 3.5.1.1 (paragraph 3.b)

NCV 269/90-17-03

Failure to Maintain Level in UST Above 6

Feet (paragraph 2.b)

NCV 269/90-17-04

Failure to Provide for Continuous Sampling

of

the

Unit

Ventilation

Effluent

(paragraph 6)

NCV 269/90-17-05

SSF Makeup Pump

Inoperable Due to

Mispositioned Valve (paragraph 8)

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