ML15224A465

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IE Insp Repts 50-269/81-21,50-270/81-21 & 50-287/81-21 on 810921-23.Noncompliance Noted:Total Radioactivity Limit for Chemical Treatment Pond Exceeded Util Commitment
ML15224A465
Person / Time
Site: Oconee  
Issue date: 11/13/1981
From: Collins T, Hosey C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15224A463 List:
References
50-269-81-21, 50-270-81-21, 50-287-81-21, NUDOCS 8112070316
Download: ML15224A465 (3)


See also: IR 05000269/1981021

Text

- REGo

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION Il

101 MARIETTA ST., N.W., SUITE 3100

ATLANTA, GEORGIA 30303

Report No. 50-269/81-21, 50-270/81-21, and 50-287/81-21

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC

28242

Facility Name:

Oconee Nuclear Power Station

Docket Nos. 50-270, 50-270, and 50-287

License Nos. DPR-47, DPR-38, and DPR-55

Inspection at Oconee site near Seneca, South Carolina

Inspector:

/'

'

T. R. Collins

Date Signed

Approved by:___

C. Hos 'y,

Acting Section Chief

Date Signed

Techoe'cal Inspection Branch

Engineering and Technical Inspection Division

SUMMARY

Inspection on September 21-23, 1981

Areas Inspected

This special,

unannounced inspection involved 13.5 inspector-hours on site to

review the radiological aspects of a steam generator tube leak.

Results

In the area inspected, one deviation was identified (Exceeding the total radio

activity limit for the chemical treatment pond).

8112070316 811i1'

PDR ADOCK 05000269

PDR

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • J. E. Smith, Station Manager
  • T. B. Owen, Superintendent of Technical Services

D. P. Rochester, Station Chemist

J. J. Sevic, Biologist

J. A. Long, Health Physics Support Functions Coordinator

  • T. E. Cribbe, Licensing Engineer
  • T. C. Matthews, Technical Specialist-Licensing
  • H. Lowery, Operating Engineer

NRC Resident Inspector

  • D. Myers

W. Orders

.

  • Attended exit interview

2.

Exit Interview

The inspection scope and findings were summarized on September 22,

1981 with

those persons indicated in paragraph 1 above. The inspector stated that

failure to meet the requirements of Duke Power Company, Oconee Nuclear Power

Station letter to the Nuclear Regulatory Commission,

dated December 27,

1978, Attachment 1, Chemical Treatment Pond radioactive material release

limits would result in a Notice of Deviation.

Plant management acknowledged

the inspector's comments and stated their intention was not to continue dis

charging radioactive material to the Chemical Treatment Pond #2 and their

prime responsibility was to protect public health and safety.

3.

Licensee Action on Previous Inspection Findings

Not inspected.

4.

Unresolved Items

Unresolved items were not identified during this inspection.

5. Radiological Aspects of Steam Generator Tube Leak of September 18, 1981

a.

On September 21 and 22, 1981,

an inspector reviewed health physics

records and interviewed personnel to ascertain the extent of radio

logical problems associated with the steam generator tube leak to the

turbine building (secondary system) and release of radioactivity to the

environment. Based on a review of the Auxiliary Building vent monitor

data R1A-43, R1A-44, and R1A-45, environmental air sample records,

2

environmental TLD results, and environmental liquid samples taken from

the plant surroundings indicated no regulatory limits were exceeded and

the dose to members of the general public were minimal. The inspector

determined that appropriate evaluations of release of radioactivity to

the environment as a result of the steam generator tube leak were made.

b.

Further review by the inspector revealed that the licensee did release

radioactivity to the Chemical Treatment Pond #2 in excess of the limits

specified in Duke Power Company, Oconee Nuclear Station, letter to the

Nuclear Regulatory Commission, dated December 27, 1978. Attachment 1

of the licensee's commitment states in part that radiaoctive material

in the Chemical Treatment Ponds (CTP)

shall be limited so that, for all

radionuclides identified, excluding noble gases, the sum of the ratios

of activity to the limits in 10 CFR 20, Appendix B, Table II,

Column 2,

shall not exceed 1.7 X 10s.

As a result of the steam generator tube

leak the licensee did discharge radioactive material to the Chemical

Treatment Pond #2 (CTP) in excess of 1.7 X 10s. The value of the ratio

summation of all radionuclides identified as of September 21, 1981 was

5.19 X 10'.

The major contributor to the CTP #2 was Iodine-131, 127,

745 microcuries.

C. As a result of the steam generator tube leak from approximately

1530 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.82165e-4 months <br /> on September 18,

1981,

to approximately 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> on

September 20,

1981,

approximately 200,000 gallons of radioactive

secondary water was collected in units 1, 2, and 3 turbine building

sumps and basements. Licensee management personnel stated that this

volume of water would be held and processed using two portable mixed

bed demineralizers and released via the normal liquid radwaste release

systems. At the time of this inspection,

no radioactive secondary

water had been released. The inspector concluded that this was an

appropriate method for release and had no further questions.

d. The total gaseous activity released through the SJAE Monitor, 2R1A

40,

from September 18,

19,

and 20,

1981 was 8.94 curies which was

4.65 X 10-4 percent of the total release of gaseous activity during

1980; total particulates and halogens were

.078 curies which was

5.83 X 10-1 percent of the total release of halogens and particulates

during 1980. Total gas for all three units released during this same

period was 246.29 curies through the vent stack (monitor R1A-45) which

was 1.28 X 10-2 percent of the total release of gaseous activity during

1980 and the total iodine released through the vent stack for all three

units was 1.3 X 10-4 curies (monitor R1A-44)

which was 1.13 X 10-3

percent of the total releases of iodine during 1980.