ML14191B084

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Insp Rept 50-261/89-02 on 890109-13.Violation Noted.Major Areas Inspected:Resistance Temp Detector Bypass Elimination, Svc Water Piping Replacement Mods,Main Feedwater Pump Flow Testing & Steam Generator Tube Eddy Current Test Results
ML14191B084
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 02/10/1989
From: Blake J, Economos N
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14191B082 List:
References
50-261-89-02, NUDOCS 8902280046
Download: ML14191B084 (8)


See also: IR 05000261/1989002

Text

UNITED STATES

2

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA ST., N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/89-02

Licensee:

Carolina Power and Light Company

P.O. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.:

DPR-23

Facility Name: H.B. Robinson

Inspection Conducted- January 9-13 1989

Inspector: ____

,

Nick

o mos.,

/bad Signed

Approved by:

A).

Jero eBlake/

ief

_Date Signed

Mat rials OdProcesses Section

En i

neerir

Branch

D'vision of Reactor Safety

SUMMARY

Scope

This routine unannounced inspection was conducted in the areas of resistance

temperature detector (RTD) bypass elimination, service water piping replacement

modifications, main feedwater pump flow testing, steam generator (SG) tube eddy

current test (ET) results and previously identified inspection findings.

Results

Work on the service water pipe replacement and resistance temperature detector

(RTD) bypass elimination modification is essentially completed. Therefore, the

inspector reviewed the documentation packages and conducted a field inspection

to verify as-built conditions including pipe configuration, dimensions, eleva

tion, etc. Flow testing of the main feedwater pumps (FWP) was in progress using

an ultrasonic flow detection device produced by Controllatron.

Current and

previous flow test data was reviewed and discussed with cognizant personnel. A

review of FWP maintenance procedures and historical corrective maintenance

records disclosed that the approved procedure used to perform this activity was

inadequate and, therefore, a violation was issued.

8902280046

8902

1

F DR

DC

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REPORT DETAILS

1. Persons Contacted

Licensee Employees

S. B. Clark, Project Engineer Configuration Control

R. Cox, Modification Project Liaison Engineer

  • J. M. Curley, Director, Regulatory Compliance
  • R. H. Dufresne, Project Engineering Supervisor, Civil Engineering

W. Farmer, System Supervisor Technical Support

B. Harward, Principal Engineer Modification Projects

J. Latimer, Welding Engineer

  • R. E. Morgan, General Manager

R. Munday, Engineering Technician I, Modifications Projects

  • M. F. Page, Manager, Technical Support
  • S. M. Pruitt, Inservice Inspection (ISI) Coordinator
  • D. R. Quick, Manager, Maintenance
  • D. Sayer, Senior Specialist Regulatory Compliance

H. J. Young, Director, Quality Assurance (QA)

Other licensee employees contacted during this inspection included

craftsmen,

engineers,

operators,

mechanics,

security force members,

technicians, and administrative personnel.

NRC Resident Inspector

  • Attended Exit Interview

2. Follow-up on Inspector Identified Problems and unresolved Items (92701)

a. (Closed) Inspector Follow-up Item (IFI), 88-24-01 Setpoint Basis for

HVH Cooler Low Water Flow Alarm

This item was identified when the inspector ascertained that a remote

HVH flow indication was not available in the control room.

This

would preclude verification of HVH cooler operability in case of

emergency. There is a low setpoint alarm which activates when outlet

flow is 700 gpm.

Because the 700 gpm setpoint was determined by

analysis to be lower than the minimum required flow for full cooler

operability, the licensee revised upward the minimum set point to 750

gpm.

The new setting was established by analysis performed by

Westinghouse, Mechanical Equipment Design (MED),

and documented by

letter, S/N MED-FCE-6583, dated 9/9/88.

b. (Closed) Unresolved Item (URI), 88-24-02, UV/SW Relay Timing and the

Impact on Cooling Water Flows During Safety Inspection Sequel.

L

This item was identified following review of SAR Section 6.2.2.3.2

and Operation Surveillance Procedure OST-301 to determine availabilty

of full flow to the HVH cooler following a safety injection (SI)

signal.

The review indicated that full flow would probably not be

available to the HVH coolers for up to ninety (90)

seconds following

an SI signal.

At the time, the inspector of record felt that this

delay was in part due to diversion of water flow to non safety

related loads.

Moreover, the inspector reported that the licensee

could not determine at that time, July 25-29, 1988, the affect of

partial flow on the HVH coolers for the first ninety seconds of an SI

signal.

Following discussions with cognizant personnel, conducted

during this inspection, the inspector ascertained that by using

special procedure SP-814 Rev. 1, written to address Region II con

cerns on the service water system, the licensee demonstrated that

there would be sufficient flow to the HVH coolers following SI

initiation to allow them to perform their design function.

3. Eddy Current Examination

(ET)

of Steam Generator (S/G)

Tubes - Record

Review and Evaluation - Inservice Inspection (ISI) (73755)

Activities during this refueling outage included eddy current examination

of tubes in "A," "B" and "C" S/Gs. - Data acquisition and analysis was

performed by Westinghouse personnel using a multifrequency

ET technique

with the MIZ-18 system to analyze tube integrity.

The inspection was

performed per requirements of ASME Code Section XI (77S78) and Technical

Specifications (TS) 4.2.1., Inservice Inspection of Steam Generator Tubes.

At the time of this inspection, the ET examination was complete.

However

discussions with cognizant licensee personnel disclosed that a total of

626 tubes were examined in S/G "A", 627 tubes in S/G "B" and 643 tubes in

S/G "C".

In addition certain tubes, within each S/G,

were examined

through the U-Bend region.

The number of tubes examined per S/G in this

area included 17 in S/G "A",

16 in S/G "B" and 12 in S/G "C".

The

Licensee stated that one tube in S/G "C", located in Row 7, Column 92, had

exceeded the acceptance criteria of 47% thru-wall thickness and was

plugged.

The flaw was analyzed as a mechanically induced gouge.

The

licensee indicated that these were preliminary results.

The official

results will be included in the report on ISI activities performed during

this outage to be submitted to Region II at a later date.

No violations

or deviations were identified.

4. Design, Design Changes and Modifications (37700)

a. Service Water- System Piping Replacement Modification

This work effort was performed as a follow-up to that documented in

report 50-261/88-35. The work effort during this inspection included

the following:

(1) The inspector selected the following as-built drawings for

review and conduct of walkdown inspections to verify configura

tion, dimensions, elevations, instrument location and tie-in to

existing system:

3

858-2480 Rev. 0 HVH 2 Motor Cooler Line, Supply.

858-2481 Rev. 0 HVH No. 2 Motor Cooler, Return.

858-2494 Rev. 3 HVH 4 Supply Side

858-2501 Rev. 3 HVH 4 pipe to penetration @ containment.

858-2503 Rev. 0 HVH No. 4 Return Line

(2) Service Water Pipe Replacement Modification package MOD-858 was

reviewed to verify that certain line item sign-offs i.e., system

walkdown, FSAR changes and system turnovers had been completed

and signed as appropriate.

(3) Acceptance Test Procedure, Attachment 9, was reviewed to verify

that hydrostatic testing for each of the four, HVH 1 through 4,

trains had been performed at designated temperature and

pressure, with calibrated instruments and that it

had been

witnessed by trained personnel and the code inspector.

b. RTD bypass Elimination

At the time of this inspection, work on this modification had been

completed except for the hydrostatic test which will be performed

during plant start-up.

In that administrative controls and proce

dures on this modification were reviewed and the work effort docu

mented in Report 50-261/88-35, the

inspector discussed field work

activities and progress with cognizant personnel.

Field generated

records/documents selected for review included Westinghouse Field

Service Procedure MPII 2.7.2 CPL-1 Rev. 1, RTD Bypass Elimination for

H.B.

Robinson, field change requests CPL-88-001 through 005 and

nonconformance reports NR-CPL-88-00001 through 00004.

Three field

welds requiring volumetric examination (radiography) were shot using

procedure RT-101 Rev.

11,

and evaluated per ASME Code Section III,

1983 Edition requirements. The radiographed welds were as follows:

1-7A

3"d schedule 160

Crossover Leg nozzle

2-5Ac

"f

"t

"

3-5A

"1

I

The inspector reviewed the above identified radiographs to verify

that the welds and radiographic technique used met applicable code

requirements. The radiographs and the welds were found to be satis

factory. Within the areas inspected no violations or deviations were

identified.

5. Service Water Pumps - Performance and Corrective Maintenance (73756).

On an earlier Region II inspection, documented in report 50-261/

88-24, the inspector of record performed a design verification and

survey of the service water system.

Potential deficiencies were

identified with respect to system design. Two unresolved items were

identified.

One,

pertained to the timing of the closure signal to

the turbine building service water isolation valves, and another was

4

for the purpose of assessing the impact of the current throttle valve

alignment and associated controls.

Three inspector follow-up items

were identified to document inspector concerns in this area and to

allow.for documentation of their resolution. In order to address the

issues and concerns raised in the aforementioned report, the licensee

generated special procedure SP-814.

The service water system at

H.B. Robinson consists of four main service water pumps and two

service water booster pumps.

These pumps are included in the

licensee's pump and valve program which is governed by.ASME Code

Section XI (77S78) requirements. Relief requests to code required

tests for these pumps were documented in theTechnical Support

Management (TMM) Manual, under TMM-04 inservice inspection, Rev. 18

and were as follows:

5.2.1

Monthly Inservice Test per IWP-3400

5.2.2

Measurement of bearing Temperature (Tb) annually per

IWP-3300

5.2.3

Flow Rate Measurements per IWP-3000 Differential

Pressure (AP) Measurements per IWP-3000

In discussions held with the cognizant engineer in order to review

corrective actions on the two open items in paragraph 2 above of this

report, the inspector ascertained that lack of instrumentation precluded

direct measurement of WP and flow rate on these pumps.

It is the

inspector's understanding that part of the problem was due to the fact

that certain sections of these pipes were lined with concrete which made

installation of instruments difficult and impractical.

To overcome this

obstacle, the licensee has recently contracted the services of Controlla

tron, who uses an ultrasonic multipulse transitetime system to measure

flow through a pipe with a surprising degree of accuracy.

Also the

licensee indicated that flow measurements taken on systems supplied by

service water, as part of the effort to address concerns discussed in the

aforementioned report, revealed disparities between design requirements

and existing field conditions.

Specific plant components where flow

discrepancies were identified were as follows:

Component

Design Requirement

Measured Flow

(1) HVH 1-4 Motor Cooler

50 GPM

30.1 to 36.4 GPM

(2) "A" & B Diesel Cooling

600 GPM

564.5-591 GPM

(3) Steam Driven AFW Pump

9.0 GPM

5.65 GPM

(4) "A"&"B" Motor Driven AFW Pump

15 GPM

1.0 GPM

The licensee indicated that engineering was evaluating these problems in

order to resolve them prior to plant startup.

These items are being

followed more closely by the resident inspector(s) and will be discussed

further in Report 50-261/89-03.

Further discussions on the activities/

flow balance tests, which were in progress, disclosed that the main

feedwater pump head pressure was approximately 20% below reference curve

values even though the pumps had been checked and found to be satisfactory

in accordance with approved corrective maintenance (CM) procedure CM-010,

(II

Rev.

1, "Service Water Pump Overhaul."

Moreover, the licensee stated

these pumps had been operating for years in this degraded condition

without the licensee knowing the root cause of the problem. Upon further

discussion, the licensee stated that following consultations with the pump

vendor, Johnston Pump Company, and an in-depth review of Procedure CM-010,

Rev.

1, 11/7/83,

they determined that the pump shaft adjustment as

described in the procedure was incorrect and was therefore directly

responsible for the degraded pump performance experienced over the past

five to six years.

More specifically the procedural instruction applic

able to rotating assembly adjustment requires the pump shaft to be lowered

until the impeller rests on the pump bowl and subsequently raised enough

to provide for the shaft to turn freely. Following this step, the proce

dure calls for raising the shaft/impeller the height of an additional two

full turns of the adjusting nut.

Mistakenly, this in affect raises the

impeller approximately 200 mils instead of the 20 to 40 mils range recom

mended by the vendor.

The licensee therefore concluded that the addi

tional two full turns of the adjusting nut, called for in step 7.3.45 of

the procedure, should have read two flats of the adjusting nut instead of

"two full turns."

Performance data taken after the rotating assembly had

been adjusted to the new setting, raised the pump reference curves back to

normal output levels.

Following these discussions and the related dis

closure, the inspector performed an in-depth review of procedure CM-010,

Rev. 1, and associated records generated each time the procedure was

utilized, for corrective maintenance on these pumps.

Records reviewed

covered a period of about two years, dating back to 1986.

The stated

purpose of Procedure CM-010,

Rev. 1, was to address disassembly and

reassembly of the service water pumps.

This included the removal and

installation of the motor,

pump casing disassembly and reassembly, pump

rotating element repairs, pump replacement and lubrications. In reference

to the stated purpose, the inspector found the procedure inadequate in

that it:

a. Failed to identify the vendor's specific technical manual applicable

to these pumps.

The only reference to the vendor was that updated

technical information was

forthcoming.

The procedure contained no

other creditable reference except to state that it had been drafted

from technical notes taken by maintenance supervision during a

service water pump overhaul.

b. Lacked specific bolt torquing requirements with tolerances specified

by referenced vendor documents.

c. Lacked requirements for using, calibrated tools i.e. torque wrenches

dial indicators, micrometers or other specified materials, i.e.

gaskets, packing, and lubricants.

d. Contained no requirements for documenting field assembly information,

i.e. total indicated shaft runout, bearing clearances, torque values,

lubricants used, rotating element adjustments.

6

e. Contained no requirement for line item sign-offs by craft and/or QC

to verify adherence to procedural requirements.

The inspector outlined these procedural deficiencies to management and

stated that running these pumps in a degraded condition over the last five

or six years is more than sufficient evidence to verify the procedure's

inadequacy.

Following is a list of work requests issued for corrective maintenance to

be performed on these pumps in accordance with the aforementioned proce

dure over the last two years.

Work Request (W/R)

Date

Scope

W/R J 08 G - AIVJ1

10/27/86

SW pump "A" install

motor and set impeller

clearances

as

per

applicable steps

in CM-010

H12Z32-529

12/11/85

SW Pump "B" - pump

removed for maintenance

and

reinstalled.

Checked

for

proper

rotations.

H12Z33-529

1/8/86

SW pump "B" - Following

repairs install pump as

per CM-010.

W/R/J087-AFSI1

5/4/87

SW pump "B" - Adjust

pump per CM-010 correct

low discharge pressure.

These records were reviewed to ascertain to what extent procedural

requirements were followed and weather

field measurements taken by the

craft were documented.

In these cases, the inspector found that the

records outlined the work assignment, referenced applicable procedure,

CM-010, and the action taken to correct the existing problem but, provided

none of the information discussed above which made it impossible to audit

this maintenance activity. The inspector stated that the failure of the

procedure to contain provisions for documenting field measurements and

inspections and specifying applicable vendor manual and correct acceptance

criteria was in violation of 10CFR 50,

Appendix B, criterion V and the

licensee's accepted QA program, FSAR section 17.2.5. This violation was

identified as 50-261/89-02-01, Inadequate Corrective Maintenance Procedure

CM-010, Revision 1, Service Water Pump Overhaul.

Except for the violation identified above there were no deviations or

other violations identified.

7

6. Exit Interview

The inspection scope and results were summarized on January 13, 1989, with

those persons indicated in paragraph 1. The inspector described the areas

inspected and discussed the inspection finding listed below. Dissenting

comments were not received from the licensee. Proprietary information is

not contained in this report.

(Open) violation 261/89-02-01 Inadequate Corrective Maintenance Procedure

CM-010 Revision 1, Service Water Pump Overhaul (paragraph 5).

II