ML14182A264

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SALP Rept 50-261/93-30 for 920628-931225
ML14182A264
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 02/08/1994
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14182A263 List:
References
50-261-93-30, NUDOCS 9402230305
Download: ML14182A264 (6)


See also: IR 05000261/1993030

Text

SALP REPORT -

H. B. ROBINSON UNIT 2

50-261/93-30

JUNE 28, 1992 -

DECEMBER 25, 1993

I.

BACKGROUND

The SALP Board convened on January 13, 1994, to assess the nuclear safety

performance of Robinson Unit 2 for the period of June 28, 1992, through

December 25, 1993. The Board was conducted pursuant to NRC Management

Directive 8.6, "Systematic Assessment of Licensee Performance."

Board members

were Albert F. Gibson (Chairperson), Director, Division of Reactor Safety,

Region II (RII); Jon R. Johnson, Deputy Director, Division of Reactor

Projects, RII; J. Philip Stohr, Director, Division of Radiation Safety and

Safeguards, RII; and S. Singh Bajwa, Acting Director, Project Directorate III,

Office of Nuclear Reactor Regulation.

The performance category ratings and the assessment functional areas used

below are defined and described in NRC Management Directive 8.6, "Systematic

Assessment of Licensee Performance (SALP)."

II. PERFORMANCE ANALYSIS -

PLANT OPERATIONS

Overall plant operational performance during this SALP period, up to the 1993

refueling outage, was good. During the 1992-1993 operating cycle there was

one unplanned shutdown to remove debris blocking the recirculation line of a

safety injection pump and one plant trip due to a relay failure that resulted

in loss of off-site power. The outage that followed this trip was extended to

perform additional corrective maintenance and testing to verify removal of

foreign material from the safety injection recirculation piping. Following

restart, the plant operated for about a year without a trip or forced outage

until it was shut down on September 10, 1993, for refueling.

Control room operator response to plant events was mixed. Good performance

was demonstrated early in the period during the August 1992 plant trip

following a loss of off-site electrical power. Operators successfully

controlled plant systems following the trip when both emergency diesel

generators were loaded for an extended period. This good performance was not

exhibited later in the period during a routine plant startup in November

following the 1993 refueling outage. This attempted return to power

,operations was conducted without appropriate procedures, without appropriate

reactor engineering support, and without effective plant management oversight.

The licensee senior management recognized weaknesses that occurred during the

startup and initiated steps to improve the standards of plant operations as

well as the effectiveness of self-assessments performed by the operations

staff.

Licensed operators had excellent knowledge of plant systems and administrative

requirements as evidenced by excellent performance on both initial and

requalification examinations. However, several examples of procedural

violations and lack of adherence to plant technical specifications indicated a

lack of understanding of management's expectations in this area.

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A weakness in control room performance and professionalism during routine

plant operations continued from the previous SALP period. Examples of laxness

in formality included a Shift Technical Advisor leaving the operating shift

without requesting permission or conducting watch turnover; operators not

noticing a control room alarm for an extended period (about nine hours);

operators being unaware that their keys would not provide access to certain

plant areas because the health physics staff had changed all high radiation

area locks; and operators in the control room taking direction for power

ascension via electronic mail without the approval of the operations manager.

During the last half of this assessment period the plant operations management

was in a state of transition. Several key positions in the operations

department remained vacant for significant periods of time. The Plant

Manager's position was permanently filled after a six-month vacancy, and at

the end of the SALP period two key operations department positions (Operations

Manager and Operations Shift Manager) were not permanently filled.

The deficiencies in operator performance discussed above represent a decline

from the level of performance in the previous SALP period and indicate a

weakness in management oversight.

The Plant Operations area is rated Category 2.

III.

PERFORMANCE ANALYSIS - MAINTENANCE

Performance in the area of maintenance and surveillance of plant structures,

systems and components remained good. Maintenance support contributed to

generally good plant performance as evidenced by the extended period without

an automatic reactor trip and few forced shutdowns caused by maintenance

related activities. However, weaknesses in procedural controls, oversight of

work, and corrective actions caused deficiencies in maintenance, surveillance

and refueling activities.

Weak procedural controls continued to affect the quality of maintenance and

surveillance adversely .

Previous efforts to improve the quality of

maintenance procedures were not effective as evidenced by numerous examples of

deficient maintenance and surveillance procedures identified during this SALP

period. Many examples of failure to follow procedures were also noted during

this period. These weaknesses were particularly evident in the areas of

testing and calibration of plant equipment.

Failure to take effective corrective action resulted in recurring problems.

For example, failure to remove all foreign material from inside the safety

injection system after it caused recirculation flow degradation in July 1992

resulted in recurrence of the problem in August 1992. Similarly, the cause of

an emergency diesel generator air distributor failure in October 1993 was not

fully corrected, and a similar problem occurred in November 1993.

The Nuclear

Assessment Department had identified continuing weaknesses in the corrective

action program early in the SALP period.

3

Weaknesses in the oversight of certain maintenance and refueling activities

were observed late in the SALP period. For example, both emergency diesel

generators were degraded when voltage regulators were misadjusted, apparently

by painters who inadvertently turned the control knobs; the licensee was not

aware that its contractors had lost a portion of a tool inside a spent fuel

assembly until a control rod could not be inserted; and several deficiencies

in the oversight of welding activities were found by the Nuclear Assessment

Department.

The licensee developed a program to identify and eliminate equipment problems

that operators were "working around." The program was effective in reducing

the number of such problems, but equipment problems remained a challenge for

operators. This was apparent during the plant restart following refueling.in

November 1993, when several equipment failures in the balance of plant were a

distraction to operators.

Licensee management took several steps to improve the quality of maintenance

activities. Organizational changes were made, including establishment and

filling of positions for Manager-Mechanical Maintenance and Manager

Electrical/I&C Maintenance. The threshold for identifying deficiencies in

material condition was lowered, and a process was established to manage the

resulting backlog. New maintenance facilities, including shops and equipment,

were placed in service. New programs were established including a minor

maintenance program and an enhanced program for predicting piping degradation

due to erosion and corrosion. A Maintenance Procedures Group was established

to improve the quality of maintenance procedures, and a handbook clearly

defining maintenance performance expectations was distributed.

The Maintenance area is rated Category 3.

IV. PERFORMANCE ANALYSIS -

ENGINEERING

Engineering performance continued to be effective in most cases. This

performance is attributed to a well qualified, highly motivated staff.

Performance deficiencies were caused by a weak interface between design

engineering and site technical staffs and by ineffective corrective actions.

Engineering staffing levels were suffient to provide adequate support to the

plant and the engineering staff was knowledgeable, competent, and exhibited a

willingness to provide maximum effort in performing their engineering duties.

The technical support staff was actively involved in day-to-day activities at

the plant and communicated effectively with the maintenance and operations

staffs. System engineers were responsible and accountable for assuring the

readiness of their systems.

Engineering modification packages were complete and detailed. Packages

contained design and work instructions, design bases, and completed control

room drawings before turnover to operations. Replacement of the 230 KV

generator breakers demonstrated the licensee's strength in this area. This

modification was completed ahead of schedule, with the majority of the work

4

completed while the plant was at full power. The actions taken to minimize

the site's vulnerability to a switchyard related event included an appropriate

level of attention to risk. In addition, the licensee had an effective

program for temporary modification control.

The licensee identified a weakness in the interface between site and corporate

engineering staffs and took steps to strengthen this interface. A

reorganization was initiated which included relocation of the design

engineering staff from the corporate office to the plant site. Interface

problems during this SALP period contributed to miscalibration of power range

nuclear instrumentation and inconsistencies between design calculations and

service water pump performance.

Engineering support provided to operations and maintenance was generally

adequate. Engineers assisted operations in system inspections. The

erosion/corrosion program, which was weak during the previous SALP period, was

significantly strengthened, and good engineering oversight was provided to

assure effective implementation. However, the program established to monitor

the performance of heat exchangers in the service water system was an

exception to this good support. The lack of performance testing and

definitive acceptance criteria for inspecting and cleaning these heat

exchangers provided poor assurance of system performance. Also, deficiencies

in engineering support for the cycle-16 refueling outage resulted in the

installation of improperly configured fuel assemblies.

Self-assessments were generally effective in identifying problems, but

corrective actions were not always effective. Assessments by the Nuclear

Assessment Department were aggressive and thorough. System engineers

identified and reported deficiencies on their assigned systems. Problems were

identified through comprehensive evaluations of the service water system and

of events associated with the cycle-16 refueling outage and startup. However,

root cause analyses and corrective actions were not always effective, and some

problems remained months after identification.

The Engineering area is rated Category 2.

V.

PERFORMANCE ANALYSIS - PLANT SUPPORT

The radiation control program was effective in controlling external and

internal exposures, with exposure totals consistent with the radiological work

that was performed during this period. Total collective dose for 1992 was 352

person-rem, and for 1993 the total was 337 person-rem. The exposure for the

refueling outage this .period was approximately 254 person-rem, which was

historically the lowest total achieved at the Robinson site for such an

outage. The ALARA program, which received good support, was effective and

contributed to controlling overall exposures close to preset goals.

Initiatives this period included early boration, use of water shields, remote

cameras, and reduction in respirator usage.

In spite of the good overall radiation control program, there were numerous

examples of performance problems this period with adherence to radiation

5

control procedures. Two of the more significant of these problems involved

the failure to properly control access to a highly radioactive bolt that had

been irradiated in the reactor core and the failure to properly control keys

for access to high radiation areas.

A good contamination control program, including reclamation of the

contaminated process areas, contributed to maintaining the number of personnel

contamination events and the total contaminated area at reasonably low levels.

This was supported by a good housekeeping program at the plant.

The radiological effluent treatment and monitoring systems were effective in

maintaining effluent to low levels this period with virtually no resulting

environmental doses. Effluent monitors were well maintained. The quality of

effluent sample results was excellent, as indicated by samples split with the

NRC and other measurement cross-check programs. The environmental monitoring

program was well run and environmental sample results were consistent with

results from the State of South Carolina's sampling program.

The solid radioactive waste treatment, volume reduction, and shipment programs

were well run this period with a significant volume reduction. The program

was implemented by dedicated, competent personnel.

The training to qualify

more technicians to operate the Post Accident Sampling System (PASS) was

successful in increasing the number of qualified personnel to take liquid and

gaseous samples. The primary and secondary chemistry programs were

effectively implemented. The licensee's audit and associated corrective

action program in the radiation control area were adequate and represented

improvements over the previous SALP period.

The emergency preparedness program continued to improve this period with

enhanced staffing and good management support.

Improvements were noted in the

area of emergency facilities, equipment, and supporting computer programs.

Several actual events were properly responded to this period, with the

exception of one for which the correct classification and notifications were

not timely. Responses during drills this period and during a 1992 exercise

were adequate. The emergency preparedness training program was upgraded to

correct performance problems regarding dose assessment, protective action

recommendations and offsite notifications. Licensee audits in the emergency

preparedness area were detailed, comprehensive, and were considered a

strength. Critiques were adequate, but the corrective actions for critique

and audit findings needed improvement in timeliness.

The security program was adequately implemented during this period with

improved management support later in the period. As a result additional staff

and equipment and, most significantly, dedicated technicians for equipment

maintenance were provided. The security force effectively performed its

duties in a professional manner with good procedural adherence throughout this

period. Late in the period, problems indicated the need for additional

response training to which the licensee responded promptly. Access controls

were adequate with safety-related equipment protected as required. The

licensee's audits in the security area were thorough, complete, and effective.

Corrective actions, however, were marginal, particularly with regard to the

timeliness of technical resolution of problems.

Improvements occurred in this

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area later in the period. Shipments of spent fuel were adequately planned and

controlled.

Implementation of the fire protection program was adequate. The licensee

appropriately maintained fire protection features and support equipment, and

control of flammable materials was adequate.

Several problems were noted with

procedural adherence in this area, some of which were repetitive. For

example, multiple instances were identified in which the designated firewatch

abandoned the assigned post prior to restoration of the fire protection

system.

The Plant Support area is rated Category 2.