ML14181A770

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Insp Rept 50-261/95-23 on Stated Date.Violations Noted.Major Areas Inspected:Plant Operations & Maint Activities
ML14181A770
Person / Time
Site: Robinson 
Issue date: 09/18/1995
From: William Orders, Verrelli D
NRC Office of Inspection & Enforcement (IE Region II)
To:
Carolina Power & Light Co
Shared Package
ML14181A768 List:
References
50-261-95-23, NUDOCS 9509280240
Download: ML14181A770 (10)


See also: IR 05000261/1995023

Text

C,"pkREG114.9

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/95-23

Licensee:

Carolina Power & Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.:

DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducte

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</26, 1995

Lead Inspector:

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,

dent Inspector

ate Signed

Other Inspectors: R. McWhorter, Senior Resident Inspector, North Anna

.Oge, Resident Inspector, Robinson

Approved by:

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Davd M. Verrlli, Chief

Date S-.gned

Reactor Projects Branch 1A

Division of Reactor Projects

SUMMARY

SCOPE:

This routine, resident inspection was conducted in the areas of plant

operations, and maintenance activities.

RESULTS:

One violation with two examples was identified concerning an inadequate

operating procedure and an operator's failure to communicate intended plant

configuration changes.

[Paragraph 3]

Based on the results of this inspection, the licensee effectively implemented

the maintenance program during this evaluation period.

[Paragraph 4]

9509280240 950918

PDR ADOCK 05000261

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PDR

REPORT DETAILS

1.

PERSONS CONTACTED

Licensee Employees:

  • B. Baum, Manager, Human Resources
  • P. Cafarella, Superintendent, Mechanical Systems
  • A. Carley, Manager, Site Communications

B. Clark, Manager, Maintenance

T. Cleary, Manager, Mechanical Maintenance

  • D. Crook, Licensing/Regulatory Compliance

D. Gudger, Senior Specialist, Licensing/Regulatory Programs

  • C. Hinnant, Vice President, Robinson Nuclear Plant

P. Jenny, Manager, Emergency Preparedness

J. Kozyra, Licensing/Regulatory Programs

  • R. Krich, Manager, Regulatory Affairs

B. Meyer, Manager, Operations

  • G. Miller, Manager, Robinson Engineering Support Services
  • J. Moyer, Manager, Nuclear Assessment Section

B. Steele, Manager, Shift Operations

D. Stoddard, Manager, Operating Experience Assessment

  • D. Taylor, Plant Controller

R. Warden, Manager, Plant Support Nuclear Assessment Section

W. Whelan, Industrial Health and Safety Representative

D. Whitehead, Manager, Plant Support Services

T. Wilkerson, Manager, Environmental Control

  • D. Young, Plant General Manager

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

NRC Personnel:

  • W. Orders, Senior Resident Inspector

R. McWhorter, Senior Resident Inspector, North Anna

C. Ogle, Resident Inspector

  • Attended exit interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

PLANT STATUS AND ACTIVITIES

a.

Operating Status

The unit operated at or near full power for the entire report

period.

b.

Other NRC Inspections and Meetings

Rick McWhorter, RII, Senior Resident Inspector, North Anna, was on

site during the week of August 7 -

11, 1995. His inspection

efforts included a review of the technical specification bases

2

supporting the requirement for the pressurizer spray valves.

Results of this inspection are contained in paragraph 3 of this

report.

3. OPERATIONS

Plant Operations (71707)

The inspectors evaluated licensee activities to determine if the

facility was being operated safely and in conformance with regulatory

requirements. These activities were assessed through direct observation

of ongoing activities, facility tours, discussions with licensee

personnel, evaluation of equipment status, and review of facility

records. The inspectors evaluated the operating staff to determine if

they were knowledgeable of plant conditions, responded properly to

alarms, and adhered to procedures. Selected shift changes were observed

to determine that system status continuity was maintained and that

proper control room staffing existed.

Routine plant tours were conducted to evaluate equipment operability,

assess the general condition of plant equipment, and to verify that

radiological controls, fire protection controls, physical protection

controls, and equipment tagging procedures were properly implemented.

Pressurizer Spray Valve Failure

At 5:55 a.m., on August 5, 1995, operators identified that RCS pressure

was oscillating slightly. After observing the oscillations for several

hours, at approximately 8:00 a.m., operators energized the pressurizer

backup heaters in an attempt to stop the oscillations. When no effect

was observed, operators returned the backup heaters to automatic.

Shortly thereafter at 8:27 a.m., pressure was noted to be decreasing

despite the fact that all heaters had automatically come on.

Further

investigations revealed that pressurizer spray valve PCV-455A indicated

approximately ten percent open with its controller in automatic.

Operators shifted the controller to manual and attempted to close the

valve, but the valve remained slightly open. During this time, pressure

dropped very slowly at approximately one psig per minute. Operators

entered AOP-19, Malfunction of RCS Pressure Control, and initiated

troubleshooting activities. At approximately 10:39 a.m., technicians

entered containment and shut the spray valve by isolating its air

supplies, and RCS pressure returned to normal.

The lowest pressure

observed during the transient was approximately 2152 psig.

Later on the

same day, technicians entered containment again to adjust the valve's

pneumatic positioner and reconnect the valve's air supplies. The valve

was returned to service, but operators kept the valve shut and its

controller in manual to avoid any possible future problems. On

August 9, technicians entered containment and removed the pneumatic

positioner and booster relay from the valve for further troubleshooting

and maintenance. This action fully disabled the A spray valve.

3

The inspectors reviewed the licensee's actions in response to the failed

spray valve to ascertain if operator response was proper and if TS

requirements were met. TS 3.1.1.3.b required the licensee to maintain

the "pressurizer, including necessary spray and heater control systems"

operable. The TS basis for this specification stated, "The pressurizer

is necessary to maintain acceptable system pressure during normal plant

operation, including surges that may result following anticipated

transients."

The inspectors questioned the licensee concerning how this

specification could be met with only one spray valve operable. The

licensee referred the inspectors to their Expert Operability Analysis,

serial RNP/95-0328, completed on August 7, which concluded that only one

spray valve was required. The inspectors reviewed the analysis and

discussed its basis in detail with licensee engineers. The licensee's

conclusion was based primarily on two interpretations:

1) "normal plant

operation" meant steady state operation, for which one spray valve was

fully capable of working with pressurizer heaters to control pressure,

and 2) "surges following anticipated transients" referred to transients

addressed by the UFSAR chapter 15 accident analyses, in which no credit

was taken for pressurizer spray valve operation. In addition to the TS

basis, the documents discussed in the analysis which provided additional

information were the licensee's RCS DBD and a vendor design basis

review, WCAP-12735.

The inspectors reviewed the DBD and WCAP-12735 and found that the sizing

of the pressurizer spray valves was based on ensuring that they had the

capacity for controlling pressure without opening a pressurizer PORV

during a step change in power from 100 to 90 percent. To accomplish

this, a capacity of at least 420 gpm was listed as the minimum required

with a note stating that the requirement had been revised to 600 gpm.

Since the actual spray valve capacity was 300 gpm each, proper design

response would require two spray valves. The inspectors discussed with

licensee engineers the fact that the system's design basis inferred that

"normal operation," as referred to in the TS basis, appeared to include

response to a 100 to 90 percent power change, which would require two

operating spray valves. The engineers disagreed with this position

because this was not a safety-related function as referred in the UFSAR.

The inspectors also noted that step 3.a of the Expert Operability

Analysis included implementing a compensatory action for the Manager

Operations to issue a night order notifying all personnel of the

unavailability of PCV-455A. On August 9, the inspectors reviewed the

night order book in the control room and found that no such night order

had been issued. During the control room review the inspectors noted

that the unavailability of PCV-455A was denoted for operators by a red

sticker on the controller which had been installed earlier that same

date when the valve's actuator parts had been removed.

The inspectors

informed the licensee of this finding. Additionally, the inspectors

discussed with the licensee questions concerning the requirements for

maintaining emergency power available to the remaining spray valve as

required by TS definitions for operability. This issue was not

addressed by the analysis.

4

The inspectors concluded that the licensee's Expert Operability Analysis

did not fully justify operation with only one spray valve.

Specifically, the analysis did not address the fact that the system

design basis required two spray valves for controlling pressure during a

100 to 90 percent load reduction. Additionally, the analysis did not

address operability power requirements for the remaining spray valve.

Pending further action to resolve whether one or two spray valves are

required to meet the requirements of TS, this item is identified as

Unresolved Item URI 50-261/95-23-01, Inadequate Justification For Plant

Operation With One Pressurizer Spray Valve Inoperable.

In response to the inspectors' concerns, on August 11, the licensee

completed a more detailed review. The inspectors had not received a

copy of the results of this review by the end of the report period.

The inspectors also reviewed operator response to the transient. The

inspectors learned that operators had experienced difficulty in applying

AOP-19 to the situation. Specifically, when operators reached AOP-19,

step 7 RNO, they had performed the first sub-step to place the spray

valve controller in manual and attempted to shut the valve, but they

stopped their actions at the second sub-step. The second sub-step

required operators to reduce reactor power and stop a RCP if the spray

valve could not be closed. With the concurrence of senior station

managers who were present in the control room, the operators stopped the

procedure at that point, in order to take additional actions (entering

containment to remove air from the valve) to close the valve.

The inspectors inquired how this deviation from the procedure was

allowed.

Licensee managers responded that they believed that the

actions taken were consistent with the intent of the procedure step,

since the pressure decrease was very slow and time was available for

further corrective actions to shut the valve. The inspectors agreed

that it was prudent to defer the power reduction while repair attempts

continued, but questioned how this stopping in the middle of the

procedure was administratively controlled. Licensee management

responded that the shift supervisor had the authority to make such a

decision, and that senior manager concurrence was also present in this

situation. The inspectors agreed that the action and approval authority

was appropriate, but concluded that the procedure deviation should have

been more formally controlled. Even in urgent situations, maintaining

formal control of procedure deviations was necessary to reduce the

opportunity for errors. The inspectors reviewed the licensee

requirements for procedure use and found that OMM-001, Operations

Conduct of Operations, step 5.9.1.3, allowed operators to deviate from

procedures in cases where adherence could cause a worsened condition,

but stated that a procedure change or deviation should be made.

Administratively, the inspectors concluded that the decision to stop in

the middle of the procedure should have been documented by a procedure

change or deviation, such as described in OMM-001, in order to maintain

the preferred formality.

5

Unusual Event, RCS Leakage

At 3:33 p.m., on July 24, 1995, the licensee declared an Unusual Event

due to RCS leakage in excess of 10 gpm. The leakage was coming from

valve CVC-283A, the relief valve on the discharge of the "C" charging

pump, and a piping crack where relief valve CVC-283C is mounted to the

discharge of the "A" charging pump.

The leak was caused by operators closing valves in the flow path of the

running positive displacement charging pump which resulted in system

over-pressurization.

Ultimately, the leaks were isolated and the Unusual Event was terminated

at 4:39 p.m.

The Robinson CVC system includes three, variable speed, three piston,

positive displacement pumps. The pumps have a flow capacity raging from

approximately 25 gpm at minimum speed, to about 77 gpm at maximum speed.

At the time of the event, the "A" charging pump was operating at minimum

speed supplying approximately 25 - 30 gpm to the RCS, split between the

seals and the normal charging flowpath.

The Shift Supervisor had elected to remove the normal letdown flowpath

from service and place excess letdown in service to accommodate

scheduled work on valve LCV-115A. When excess letdown was placed in

service, the "A" charging pump, which was aligned for automatic

pressurizer level control, slowed to minimum speed. The control room

SRO noted that RCP seal differential pressure was lower than normal and

had an AO check seal injection flow using local gauges. The AO reported

that seal injection flow was 6, 0, and 7 gpm respectively for the three

RCP's. Desired seal injection flow is 8 -

13 gpm. The control room SRO

directed the RO to throttle charging flow control valve HCV-121 to force

more flow to the seals. Valve HCV-121 was adjusted to 80 - 85 percent

demand on the controller. This increased seal injection flow to 9 - 11

gpm to all three pumps. Unbeknownst to the operators, their action had

completely closed HCV-121, diverting all charging flow to the seals.

Noting that pressurizer level was still increasing very slowly, the RO,

of his own volition, and without communicating his intended actions,

directed an AO to adjust RCP seal flow to 8 gpm for each pump. This is

done by adjusting manual valves CVC-297 A, B, and C, in the charging

pump room. As the AO was adjusting seal flow, relief valve CVC-283A

lifted and failed to reseat. The AO had throttled the seal injection

valves such that the positive displacement charging pump had

insufficient flow path.

The operator's failure to communicate his

intended actions to the operating crew is one of two examples which

collectively constitute Violation VIO 50-261/95-23-02, Operator Fails To

Follow OMM-001, Procedure OP-301 Inadequate. This point is significant

because a number of very similar events have occurred. In each of these

6

previous events, the operating crews were made aware of the

circumstances of the incidents. Had the reactor operator announced his

intended actions as required, another member of the operating crew may

have been able to pre-empt the event based on previous experience.

The AO exited the charging pump room to use the P. A. system to .

inform the control room of the situation.

Based on this information and

confirmatory observations of plant parameters the control room SRO

directed the entry into Abnormal Operating Procedure AOP-16, Excessive

Primary Plant Leakage. The RO instructed the AO to check charging pump

discharge pressure. As the AO re-entered the charging pump room, he

noted a small leak on the flange of the A charging pump discharge relief

valve.

He immediately exited the room to inform the control room of

this new observation. The RO directed the AO to close valves CVC-286

and CVC-287, the discharge valves from the C charging pump.

At 3:19 p.m., the idle "B" charging pump was started and the "A"

charging pump was stopped.

By 3:20 p.m., the AO had closed valve CVC

286 and was closing valve CVC-287 when an HP directed the AO to evacuate

the room due to deteriorating conditions associated with the leak on the

piping of the "A" charging pump. As the AO left the room, he noted that

the leak on the "A" charging pump was much worse.

At about 3:26 p.m., the SRO directed another AO to close valves CVC-290

and CVC-291, the discharge valves on the "A" charging pump.

At 3:33 p.m., the SS declared an Unusual Event due to RCS leakage of

greater than 10 gpm after the leak rate was determined to be

approximately 14 gpm based on VCT level profile.

By 3:50 p.m., letdown divert valve LCV-115A was returned to service,

normal letdown was re-established, and excess letdown was isolated.

At 4:20 p.m., an AO entered the charging pump room to complete the

isolation of the "C" charging pump.

At 4:39 p.m., the Unusual Event was terminated after a confirmatory RCS

leak rate determination.

It was subsequently determined that the relief valves for the "A" and

"C" charging pumps had lifted. Both valves revealed severe

internal

damage when disassembled. The valve vendor attributed the damage to

"severe chatter," caused by the valves cycling with each piston stroke

of the positive displacement pump.

Both valves were replaced the

following day. The piping crack was repaired by replacing the section

of piping affected. The licensee determined that the crack was due to

the vibration stresses associated with the relief valves rapidly opening

and closing.

The resident inspectors responded to the control room at the initiation

of the event, reviewed plant parameters, discussed the plant status with

operations personnel, and notified NRC Region II management. The

7

inspectors monitored the event until the leak had been terminated,

normal charging had been established, and a normal leak rate calculated.

Pressurizer level remained relatively stable throughout the event.

The inspectors reviewed the procedures in use at the time of the event,

assessed operator performance, and evaluated the transient to assess

equipment performance. OP-301, Chemical And Volume Control System, was

used by the operators to place excess letdown in service. After

performing a thorough review of the procedure and its contribution to

the event, the inspectors concluded that OP-301 was inadequate. The

procedure contained no specific guidance concerning the manipulation of

the charging and seal injection valves while on excess letdown and the

associated possibility of over-pressurizing the system. This is despite

the fact that the procedure had been used during two very similar events

on November 9 and November 11, 1993, during which the system was over

pressurized. Adverse Condition Report 93-276 documents the licensee's

investigation of those two events and lists OP-301 as the procedure

employed by the operators to remove normal letdown from service and

place excess letdown in service, yet no changes were made to OP-301.

The inadequacy of OP-301 constitutes the second of two examples of

procedure compliance which collectively comprise Violation VIO 50-261/

95-23-02, Operator Fails To Follow OMM-001, Procedure OP-301 Inadequate.

It should be noted that although the licensee recognized during their

associated Event Review, that the operator had failed to follow

procedures and that procedure OP-301 was inadequate, the NRC cannot

exercise enforcement discretion because it is the NRC's opinion that

comprehensive corrective action to the 1993 events could have prevented

this incident.

It should also be noted that the inspector's review of the licensee's

initial set of prompt corrective actions, which included a revision to

OP-301, "Real Time" operator training, and an Operations Night Order,

revealed that OP-301 still did not entail detailed specific operator

guidance in the aforementioned critical areas. The inspectors notified

licensee management of this observation. A subsequent, more detailed

revision to OP-301 was generated. This example of corrective action is

considered marginal and indicative of a minimalistic approach to

corrective actions.

Notice of Enforcement Discretion

On July 21, 1995, the licensee documented a request for the NRC to

exercise enforcement discretion. The combined leakage from the

Penetration Pressurization System (PPS) exceeded the allowable limit of

1.57 SCFM required to meet containment integrity. The Resident Staff

will address the root cause that led to the need for the NOED during a

future inspection. This will be known as Unresolved Item URI 50-261/95

23-03, NOED: PPS Exceeded the Allowable Limit.

8

4.

MAINTENANCE

a.

Maintenance Observation (62703)

The inspectors reviewed selected safety-related maintenance

activities to determine if the activities were conducted in

accordance with regulatory requirements, approved procedures, and

appropriate industry codes and standards.

The inspectors reviewed

associated administrative, material, testing, radiological, and

fire prevention controls requirements to determine licensee

compliance.

b.

Surveillance Observation (61726)

The inspectors evaluated selected safety-related surveillance

activities to determine if these activities were conducted in

accordance with license requirements. The inspectors analyzed the

associated administrative controls, the qualifications of the

personnel, procedure compliance, test instrumentation calibration,

and the required test frequency.

Surveillance activities evaluated included but were not limited to

the following:

OST-010

Power Range Calorimetric During Power Operations

OST-924

Radiation Monitor Quarterly Test (R-3)

OST-051

Reactor Coolant Leakage Evaluation

OST-201

Motor Driven Auxiliary Feedwater System

Component test

OST-750

Control Room Emergency Ventilation System

Based on the results of this inspection, the licensee's programs

were successfully implemented in this functional area.

5.

EXIT INTERVIEW

The inspectors met with licensee representatives (denoted in

paragraph 1) at the conclusion of the inspection on August 29, 1995.

During this meeting, the inspectors summarized the scope and findings of

the inspection as they are detailed in this report. The licensee

representatives acknowledged the inspector's comments and did not

identify as proprietary any of the materials provided to or reviewed by

the inspectors during this inspection. No dissenting comments from the

licensee were received.

Item Number

Status

Description/Reference Paragraph

URI 95-23-01

Opened

Inadequate Justification For Plant

Operation With One Pressurizer Spray

Valve Inoperable, paragraph 3.

9

VIO 95-23-02

Opened

Operator Fails To Follow OMM-001,

Procedure OP-301 Inadequate,

paragraph 3.

URI 95-23-03

Opened

NOED:

PPS Exceeded the Allowable

Limit, paragraph 3.

6.

ACRONYMS AND INITIALISMS

AO

Auxiliary Operator

AOP

Abnormal Operating Procedure

CVC

Chemical and Volume Control

DBD

Design Basis Documentation

gpm

Gallons Per Minute

HCV

Hand Control Valve

HE&E

Harris Environmental & Engineering

HP

Health Physicist

LCV

Level Control Valve

LCO

Limiting Condition for Operation

LDV

Letdown Divert Valve

OP

Operating Procedure

P.A.

Public Announcement

PCV

Pressure Control Valve

PORV

Power Operated Relief Valve

psi

Pounds Per Square Inch

psig

pounds Per Square Inch - Gage

QC

Quality Control

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RNP

Robinson Nuclear Plant

RO

Reactor Operator

SRO

Senior Reactor Operator

SS

Shift Supervisor

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

VCT

Volume Control Tank

VIO

Violation

WCAP

Westinghouse Corporate Atomic Power