ML14181A700

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Insp Rept 50-261/95-14 on 950423-0513.Violations Noted. Major Areas Inspected:Plant Operations,Maintenance Activities,Engineering Efforts,Plant Support Functions & Review Activities During non-regular Work Hours
ML14181A700
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 06/12/1995
From: Ogle C, William Orders, Verrelli D
NRC Office of Inspection & Enforcement (IE Region II)
To:
Carolina Power & Light Co
Shared Package
ML14181A698 List:
References
50-261-95-14, NUDOCS 9506200304
Download: ML14181A700 (14)


See also: IR 05000261/1995014

Text

og REGoj

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

Co

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/95-14

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.:

DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducted: April 23 - May 13, 1995

Lead Inspector:

- 12 -V5

QT T. Or ers, S ior/Resident Inspector

ate igne

Other Inspector:

/ -"1.

q

R J

OgIe, Res ent nspector

ate Signed

Approved by:

4

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-

4 -.--

.

Davi(d M. Verelli, Chief

Date Signed

Reactor Prdjects Branch 1A

Division of Reactor Projects

SUMMARY

SCOPE:

This routine, resident inspection was conducted in the areas of plant

operations, maintenance activities, engineering efforts, and plant support

functions. The inspection effort included reviews of activities during non

regular work hours on April 28, 29, and 30, as well as May 5, 7, and 9, 1995.

RESULTS:

Plant Operations:

One of three examples of a Violation pertaining to inadequate control of

contracted services was identified in this functional area. An Unresolved

Item was identified concerning an inadequate equipment clearance.

Maintenance:

Two of three examples of a Violation concerning inadequate control of

contracted services were identified in this functional area. A Violation was

also identified pertaining to an inadequate operations surveillance test

procedure.

9506200304 950612

PDR

ADOCK 05000261

G

PDR

Engineering:

A Non-Cited Violation was identified concerning deficiencies in the fuel pool

inventory process.

Plant Support:

A Non-Cited Violation was identified concerning the failure of a contracted

technician to follow RWP requirements. An unresolved item was identified

pertaining to the administration of the fire protection program.

1. PERSONS CONTACTED

Licensee Employees:

  • B. Baum, Director, Robinson Nuclear Project, Human Resources

W. Brand, Supervisor, Environmental Radiation Control

  • M. Brown, Manager, Design Engineering

A. Carley, Manager, Site Communications

  • A. Canterbury, Project Engineer/Technical Support

G. Castleberry, Manager Plant Electrical Engineering

  • B. Clark, Manager, Maintenance
  • D. Crook, Senior Specialist, Licensing/Regulatory Compliance
  • W. Dorman, Supervisor, Quality Control
  • M. Foerster, Manager, Robinson Engineering Support Section

Administration and Programs

  • A. Garrou, Acting Manager, Licensing Regulatory Programs

C. Gray, Manager, Materials and Contract Services

D. Gudger, Senior Specialist, Licensing/Regulatory Programs

  • C. Hinnant, Vice President, Robinson Nuclear Project

P. Jenny, Manager, Emergency Preparedness

J. Kozyra, Licensing/Regulatory Programs

  • R. Krich, Manager, Regulatory Affairs
  • D. Markle, Senior Specialist, Configuration Control

E. Martin, Manager, Document Services

  • B. Meyer, Manager, Operations

G. Miller, Manager, Robinson Engineering Support Section

  • H. Moyer, Manager, Nuclear Assessment Section
  • E. Rossman, Engineer, Robinson Engineering Support Section

B. Steele, Manager, Shift Operations

  • D. Taylor, Plant Controller

G. Walters, Manager, Support Training

  • R. Warden, Manager, Plant Support Nuclear Assessment Section
  • D. Weber, Senior Specialist, Robinson Engineering Support Section

W. Whelan, Industrial Health and Safety Representative

D. Whitehead, Manager, Plant Support Services

  • T. Wilkerson, Manager, Environmental Control
  • S. Williams, Senior Engineer, Robinson Engineering Support Section

L. Woods, Manager, Technical Support

  • D. Young, Plant General Manager

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

NRC Personnel:

  • W. Orders, Senior Resident Inspector
  • C. Ogle, Resident Inspector
  • Attended exit interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. PLANT STATUS AND ACTIVITIES

a.

Operating Status

The unit began the report period operating at full power, and had

operated at or near full power for 265 days prior to April 28 when

a planned shutdown was begun for refueling outage 16. The report

period ended with the unit in day 15 of a planned 37 day refueling

outage.

b.

Other NRC Inspections and Meetings

One Region II based inspection was conducted during the report

period. The inspection, conducted on May 9 and 10, 1995, was

performed by M. Ernstes. The inspection results are documented in

report 50-261/95-300.

3. OPERATIONS

a.

Plant Operations (71707)

The inspectors evaluated the licensee's performance to determine

if the facility was operated safely and in conformance with

regulatory requirements. These activities were assessed through

direct observation, facility tours, discussions with licensee

personnel, evaluation of equipment status, and review of facility

records.

The inspectors reviewed shift logs, operation's records, data

sheets, instrument traces, and the equipment malfunctions list to

assess equipment operability and compliance with TS. The

inspectors evaluated the operating staff to determine if they were

knowledgeable of plant conditions, responded properly to alarms,

adhered to procedures and applicable administrative controls, and

were cognizant of in-progress surveillance and maintenance

activities. The inspectors performed instrument channel checks,

reviewed component status, and assessed safety-related parameters

to determine conformance with TS. Shift changes were routinely

observed to determine that system status continuity was maintained

and that proper control room staffing existed. It should be noted

that during this report period, a major modification to the

control room was initiated. The modification process had a

dramatic effect on the internal control room boundaries and access

to the active control room area. The inspectors devoted increased

attention to this operator challenge, and determined that access

to the control room was adequately controlled, and operations

personnel carried out their assigned duties in an effective

manner. Control room demeanor and communications were

appropriate.

Routine plant tours were conducted to evaluate equipment

operability, assess the general condition of plant equipment, and

to verify that radiological controls, fire protection controls,

physical protection controls, and equipment tagging procedures

were properly implemented.

b.

Unit Shutdown

Between April 28, 1995, and April 30, 1995, the inspectors

witnessed portions of the unit shutdown for refueling outage 16

including reactor and secondary plant shutdown, transition to RHR

cooling, and collapsing the pressurizer bubble. For the most

part, these evolutions were well conducted. Strong procedure

usage was evident. The inspectors also noted increased crew

emphasis in areas which had represented previous challenges;

namely monitoring pressurizer cooldown rates and ensuring that

signatures were appropriately transferred from field copies of

procedures. Pre-evolution briefs were adequate but the inspectors

noted that the quality varied widely.

c.

Inadequate Control Of Contract Refueling Personnel

On May 8, 1995, a refueling crew signed off nineteen steps of

procedure FMP-019, Fuel and Insert Shuffle, indicating that an

equal number of thimble plugs had been moved. In actuality, none

of the plugs had been moved. It was determined that the thimble

plug tool, used by a contracted refueling technician, had been

rotated 90 degrees out of alignment. This had prevented effective

tool engagement. After the tool was realigned and additional

lighting was employed, the crew started over.

The refueling crew consisted of a contracted refueling technician,

two CP&L refueling technicians who were to be trained on the use

of the thimble plug tool, and a licensed RO. The contractor was

to actually perform the relocation of the thimble plugs and train

the CP&L refueling technicians. The RO was responsible for

coordinating the activities and for ensuring adherence to

procedures.

The contractor and the trainees were located on the SFP bridge.

The RO was located on the side of the SFP reading the steps of the

procedure to the contractor and initialing the completion of each

step. He was also updating the fuel location status board in the

SFP area and communicating the moves to the CR.

The first thimble plug was documented as being moved at 2:10 p.m.,

on May 8, 1995. The RO stated that he was able to verify the grid

locations of the fuel assemblies but was unable to see the

assemblies themselves. The RO presumed that the contractor was

actually performing the steps, but the contractor stated that he

also had difficulty seeing. As the evolution proceeded to an area

in the SFP where lighting conditions were better, it was noticed

that a thimble plug that had supposedly already been moved was

still in the assembly. They lowered a light for a closer

S

.

4

inspection and noted that none of the thimble plugs had been

moved. The contractor, after referring to a copy of FHP-001, Fuel

Handling Tools Operating Procedure, discovered that the thimble

plug tool had been rotated 90 degrees out of alignment. The

correct orientation was clearly delineated in FHP-001. It should

be noted that FHP-001 was one of approximately 10 procedures the

contractor had attested to having read on April 18, 1995.

After restarting the evolution and successfully completing two

steps, problems were experienced on step three during the

installation of a thimble plug in a fuel assembly. Investigation

revealed a bent finger on the thimble plug. The crew was

instructed to place the damaged thimble plug in a receptacle in

the SFP. The RO notified the CR of this specific problem but

failed to mention the original problem experienced with the tool.

By this time, it was close to shift turnover and no further steps

of the procedure were performed. During turnover with the

oncoming shift, the personnel communicated to their relief that

they had repeated nineteen steps of the procedure due to the tool

being improperly oriented, but management was not informed.

The contractor failed to follow the instruction afforded in

FHP-001, Fuel Handling Tools Operation, which clearly described

the correct alignment of the thimble plug tool.

The RO failed to

verify that the procedure steps had actually been performed before

signing off the procedure. This event is the first of three

examples which collectively constitute Violation 50-261/95-14-01,

Inadequate Control Of Contractor Services.

d.

Inadequate Clearance For Work On Valve V1-8A

On April 17, 1995, routine preventive maintenance was to be

performed on valve V1-8A, a motor operated valve which supplies

motive steam to the steam driven auxiliary feedwater pump. Due to

an inadequate clearance, valve MS-20 which is immediately

downstream of V1-8A, was left open. As a result, the steam driven

auxiliary feedwater pump started when valve VI-8A was manually

opened. It was also discovered that if valve V1-8A were to be

greater than 96 percent open with the steam driven auxiliary

feedwater pump not running, a close signal would be sent to the

other two valves which supply steam to the pump. That would

result in the pump being inoperable.

At the end of this report period, the inspectors had not completed

their review of the circumstances associated with this event.

Accordingly, pending the completion of these efforts, this issue

will be tracked as Unresolved Item URI 50-261/95-14-02,

Inadequate Clearance For Work On Valve V1-8A.

Unresolved items are matters about which more information is

required to determine whether they are acceptable or may involve

violations or deviations.

5

MAINTENANCE

a.

Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on

systems and components to ascertain that these activities were

conducted in accordance with TS, approved procedures, and

appropriate industry codes and standards. The inspectors

determined that these activities did not violate -LCOs and that

required redundant components were operable. The inspectors

verified that required administrative, material, testing,

radiological, and fire prevention controls were adhered to. In

particular, the inspectors observed/reviewed the following

maintenance activities detailed below:

WR/JO 95FXU002

Disassemble, Inspect, and Reassemble MS

VI-3C

WR/JO 95AGUQ001

Perform MST-925 Molded Case Circuit

Breakers Thermal and Instantaneous Trips

Test (MCC-10 Feed Only)

WR/JO 95ACDIO01

Fabricate Hydro Rig For SI-856A/B Testing

WR/JO 95AGF002

El Circuit Breaker Inspection and Test

(Partial)

Inadequate Control Of Contract Crane Operators

Collision of Polar Crane And Manipulator Crane Event

At approximately 7:20 p.m., on May 3, 1995, the Robinson

containment polar crane collided with the refueling manipulator

crane. A contracted refueling technician had moved the

manipulator crane into the path of the polar crane. Subsequently,

a contracted polar crane operator, began moving the polar crane

without verifying the position of the manipulator crane. The

polar crane impacted a cross piece on the manipulator crane's

monorail.

The top of the manipulator crane was bent approximately

two or three feet which broke welds in three places. Some of the

broken welds were repairs from a previous, similar collision that

occurred in the late 1970s. The manipulator crane was repaired

and returned to service.

An investigation of the event revealed that the refueling

technician had apparently not received CP&L crane operator

training; the contracted organization, which had the

responsibility for coordinating and operating the cranes, did not

have a formal coordination process to use when multiple cranes

were being used simultaneously; the polar crane operator had not

been trained on MI-510 which contains a requirement to check the

manipulator crane's position prior to polar crane movement; a copy

of MI-510, Polar Crane General Instructions, was not posted in the

polar crane cab as required; and the polar crane operator did not

6

receive a cogent proficiency verification on the polar crane's

operation.

This event is indicative of inadequate measures to control the

quality of contracted services. This constitutes the second of

three examples which collectively comprise Violation 50-261/

95-14-01, Inadequate Control of Contractor Services.

Polar Crane Auxiliary Hook Strikes Steam Generator Cubicle

At approximately 10:00 p.m., on May 4, 1995, the polar crane

auxiliary hook struck the concrete cubicle surrounding the "C"

steam generator. The polar crane's operator had been operating

the crane from the refueling floor, using the remote control. He

had lowered the auxiliary hook for a planned lift. Before that

lift could be made, the priorities for the polar crane changed.

The polar crane operator left the auxiliary hook down (6 to 8 feet

off the floor) and began moving the polar crane into position for

the next lift. He did so from his position on the floor, from

which he could not see the auxiliary hook. Furthermore, the

operator began the repositioning of the polar crane on his own

initiative, with no communication or direction from the signalman.

The polar crane's auxiliary hook hit the north side of the

concrete cubicle around steam generator "C", causing superficial

damage.

The contract polar crane operator was the same operator involved

in the collision of the polar crane and manipulator crane.

Therefore, the aforementioned deficiencies delineated in the

previous section will not be reiterated.

This constitutes the third of three examples which collectively

comprise Violation 50-261/95-14-01, Inadequate Control Of

Contractor Services.

OST-156 Valve Lineup Improperly Established

On May 8, 1995, the inspectors questioned the valve lineup for

Operations Surveillance Test, OST-156, Safety Injection and

Containment Spray Systems Suction Lines Leak Test. This test is

used to qualify the atmospheric leakage of portions of the safety

injection, residual heat removal, and containment spray systems in

accordance with license condition 3.G.(2). During a plant tour,

the inspectors noted that SI-887, the RHR Pump Discharge to SI and

CV Spray Suction valve was closed. The inspectors concluded that

with this valve closed, test pressure would not be applied to the

piping between valves SI-887 and the SI-863 A and B. The licensee

confirmed the inspectors observation on May 8, 1995, and revised

OST-156 to require SI-887 be open during the test. The licensee

also added additional valves to the procedure in a subsequent

temporary procedure change on May 8, 1995.

7

In response to this issue, the inspectors scrutinized OST-156 and

interviewed the coordinator involved in its initial performance.

The inspectors were advised that SI-887 was closed as the result

of a clearance on the valve, and the impact of this mis

positioning had not been previously recognized. The inspectors

noted that SI-887 is a normally locked open valve and it was not

included in the valve lineup contained in OST-156.

On May 15, 1995, while conducting a post-test review, the

inspectors detected another deficiency in OST-156. The OST valve

lineup requires that SI-862A, RWST to RHR valve be closed. In

that configuration, the piping between SI-862A and SI-862B would

not be tested. However, End Path Procedure, EPP-9, Transfer To

Cold Leg Recirculation permits the operators to close either SI

862A or SI-862B while establishing the CV sump recirculation valve

lineup. The inspectors were concerned that OST-156 as conducted,

failed to test all portions of piping which could be in contact

with highly radioactive fluids during an accident. This was

identified to the licensee for resolution. After confirming the

inspectors' observation, the licensee stated that a condition

report would be generated and that the piping between SI-862A and

SI-862B would be tested.

The inspectors concluded that procedure OST-156 was inadequate.

This is contrary to the requirements of TS 6.5.1.1 and is

identified as a violation, VIO 95-14-03, OST-156 Valve Lineup

Improperly Established.

Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance

activities on systems and components to ascertain that these

activities were conducted in accordance with license requirements.

On a selective basis, the inspectors determined that precautions

and LCOs were adhered to, the required administrative approvals

and tagouts were obtained prior to test initiation, testing was

accomplished by qualified personnel in accordance with approved

test procedures, test instrumentation was properly calibrated, the

tests were completed at the required frequency, and that the tests

conformed to TS requirements. Upon test completion, the

inspectors verified the recorded test data was complete, accurate,

and met TS requirements, test discrepancies were properly

documented and rectified, and that the systems were properly

returned to service. One such test was SP-1353, Leak Test SI-864A

and B and SI-856A and B.

Leak Test Of RWST Isolation Valves

On May 8, 1995, the inspectors witnessed portions of Special

Procedure, SP-1353, Leak Test SI-864A and B and SI-856A and B.

This procedure was performed to quantify individual seat leakage

through SI-864A, SI-864B, SI-856A, and SI-856B, to demonstrate

compliance with license condition 3.G (2).

Overall, the conduct

of the test was satisfactory. Anomalies associated with the

initial test performance were recognized by the licensee and

resolved. Applicable portions of the test were performed again

with satisfactory results on May 10, 1995.

(Closed) URI 94-12-02, Basis For Closed System Outside

Containment, documents inspectors' concerns with the licensee's

basis for closed systems outside containment which are normally

vented to the RWST. The testing accomplished by SP-1353 provides

reasonable assurance that significant flow past these valves would

not occur in the event of sump recirculation. Based on this, URI

94-12-02 is closed.

5. ENGINEERING

Onsite Engineering (37551)

Fuel Pool Inventory Discrepancy

On April 19, 1995, during fuel movement within the SFP, a fuel

assembly could not be fully lowered into its planned storage

position, MM-24. The assembly was withdrawn and returned to its

original storage location. A visual examination revealed an

undocumented filter canister stored in rack position MM-24. The

fuel movement was subsequently completed without incident. The

licensee generated a CR in response to this event.

As a followup to this event, the inspectors reviewed Fuel

Management Procedure, FMP-021, Control of Materials in the Spent

Fuel Pit, interviewed an operator involved in the fuel movement,

and the spent fuel pool system engineer.

The inspectors determined that the filter canister was not

documented as having been stored in MM-24 on the spent fuel pool

storage log sheet which is maintained in accordance with procedure

FMP-021. Hence, nothing precluded the reactor engineering staff

from utilizing MM-24 as a fuel storage location during the SFP

fuel movement. The inspectors concluded that this error was the

result of an administrative oversight on the part of the system

engineer while implementing FMP-021. The inspectors also noted

that the licensees implementation of the spent fuel pool inventory

process failed to include basic safeguards to preclude fundamental

administrative errors such as the one described.

As corrective action, the licensee conducted a visual inspection

of all SFP locations involved in the SFP fuel shuffle and fuel

offload. No additional undocumented material was identified.

Additionally, the licensee committed to revising FMP-021 to

require a second party verification of the SFP storage log sheets

and SFP location data sheets.

The failure to properly control the material stored in the SFP is

contrary to the requirements of FMP-021.

However, this violation

will not be subject to enforcement action because the licensee's

efforts in identifying and correcting the violation meet the

criteria specified in section VII.B of the Enforcement Policy.

This is identified as a Non-Cited Violation, NCV 50-261/95-14-04,

Fuel Pool Inventory Not Properly Maintained.

6. PLANT SUPPORT

a.

Plant Support Activities (71750)

CO2 Bottle Explosion

Event Summary

On April 30, 1995, a 5 lb. CO2 cylinder, which had been stored in

a compressed gas storage shed, exploded. The explosion destroyed

a storage cage, the cylinder ricocheted off one of six stationary

hydrogen storage cylinders used as emergency make-up for the

Unit 2 hydrogen supply system, and ultimately came to rest some 20

feet from the shed. The hydrogen cylinder was torn from its

mounts and came to rest approximately 10 feet from its original

location. The hydrogen manifold tubing was severed, creating an

unrestricted leak path for the remaining five hydrogen cylinders.

The hydrogen gas ignited, engulfing the immediate area. The Site

Fire Brigade responded and the fire was out within seven minutes.

No off-site fire assistance was required. Damage was restricted

to the CO2 cylinder, the six hydrogen cylinders, associated

piping, and the storage cage.

Event Details

At approximately 1:55 p.m., on the afternoon of April 30, 1995, a

Unit 2 outside auxiliary operator heard an explosion in the

vicinity of the compressed gas shed. This shed is located

approximately 70 feet east of the perimeter of the Unit 2

Protected Area. Upon investigating, the operator observed a

hydrogen cylinder laying on the ground, about 10 feet west of the

shed. He also heard a loud "blow down" noise being emitted from

the same general area. The operator notified Unit 2 Control Room

personnel who in turn dispatched the Fire Brigade. As previously

mentioned, the Fire Brigade responded and the fire was out within

seven minutes.

The licensee sent the ruptured CO2 cylinder to the metallurgy lab

at their E&E Center. Preliminary results indicated that the

rupture was caused by tensile strength overload, and that there

was no apparent flaw in the cylinder. The licensee's analysts

indicated that over-filling the cylinder would be strongly

suspected as the cause of the cylinder failure.

10

It was determined that the CO2 cylinder which failed and another

5 lb. CO2 cylinder had been taken off site for vendor servicing on

April 24, 1995, and were returned the following day. Licensee

personnel performed OST-621, Diesel Generator CO2 Cylinder Weight

Test later that day. The test revealed that the cylinder which

failed was charged to 180 percent of full weight and the other CO2

cylinder was charged to 131 percent of full weight. The latter

cylinder was placed in service at approximately 2:00 p.m. that

same day as the control cylinder for the Diesel Generator CO2

System. The cylinder which failed was placed in the storage area

of the Unit 1 gas shed. The licensee's surveillance procedure,

OST-621, did not limit the maximum quantity of charge on the

cylinders, only the minimum quantity of charge.

These cylinders were originally fitted with a rupture disk

designed to prevent cylinder over-pressurization. The original

rupture disks were designed to relieve at approximately 3000 psi.

The licensee determined that the cylinder which failed had three

rupture disks installed in series. The licensee removed the other

CO2 cylinder from service to determine if a similar situation

existed. The licensee found two rupture disks installed on that

cylinder. With multiple rupture disks installed, the cylinders

could be pressurized to pressures exceeding their rating. The

licensee determined that due to the cylinder being overfilled and

the negation of the overpressure protection, the cylinder which

failed had been pressurized to approximately 6,583 psi.

At the

end of this report period, the inspectors have not completed their

review of the circumstances associated with this event.

Accordingly, pending the completion of these efforts, this issue

will be tracked as an Unresolved Item, URI 50-261/95-14-05,

Operations Surveillance Test 621 Deficiency.

Unresolved items are matters about which more information is

required to determine whether they are acceptable or may involve

violations or deviations.

RWP Requirements For Protective Clothing Not Followed

On May 11, 1995, during a routine tour of containment, the

inspectors observed a contract worker involved in MOD-1074, work

which required full anti-Cs, yet the worker was not wearing an

anti-contamination head covering. The inspectors questioned the

HP assigned to coverage of the first level of the CV on the

appropriateness of this observed dress. After examining the

situation, the HP advised the inspectors that the worker's outfit

was incomplete and not in compliance with the assigned RWP. The

worker was subsequently escorted from containment and a condition

report was generated.

The inspectors reviewed the appropriate RWP, interviewed the lead

HP, and reviewed Plant Program Procedure, PLP-016, Radiation Work

Permit Program.

The inspectors noted that the RWP required a cloth hat or single

cloth hood. The inspectors were advised that the worker had

entered the CV with a cloth hat beneath a hard hat. The cloth hat

was inadvertently removed with the hard hat when the worker put on

a phone headset. The licensee stated that the worker did not

recognize this error at the time. As corrective action, the

licensee counselled personnel involved in the modification on the

need to comply with RWP requirements.

Overall, the inspectors concluded that the worker's failure to

comply with the RWP was contrary to the requirements of PLP-016.

However, this NRC identified violation is not being cited because

criteria specified in Section VII.B of the NRC Enforcement Policy

were satisfied. This is identified as a Non-Cited Violation, NCV

50-261/95-14-06, RWP Requirement For Protective Clothing Not

Followed.

It should be noted that since the start of the refueling outage

the inspectors have noted several isolated incidents involving HP

work practices that fall short of established plant practices.

All of these observations have been relatively minor and involved

personnel not permanently assigned to the facility. The

inspectors have discussed these observations with licensee

management. Based on these observations, the inspectors concluded

that additional emphasis on routine HP practices by contract

workers may be required.

At the exit, the licensee stated that their trending program had

also detected a similar trend in contractor performance in the

radiological controls area. Furthermore, the licensee advised the

inspectors that they had implemented corrective actions to resolve

these concerns. The licensee subsequently provided the inspectors

a copy of the CR generated in response to this effort. The

inspectors reviewed the CR and have no further questions on this

issue.

7. EXIT INTERVIEW

The inspectors met with licensee representatives (denoted in

paragraph 1) at the conclusion of the inspection on May 19, 1995.

During this meeting, the inspectors summarized the scope and findings of

the inspection as they are detailed in this report. The licensee

representatives acknowledged the inspector's comments and did not

identify as proprietary any of the materials provided to or reviewed by

the inspectors during this inspection. No dissenting comments from the

licensee were received.

Item Number

Status

Description/Reference Paragraph

VIO 95-14-01

Opened

Inadequate Control Of Contractor

Services/paragraphs 3, 4

URI 95-14-02

Opened

Inadequate Clearance For Work On

Valve VI-8A/paragraph 3

VIO 95-14-03

Opened

OST-156 Valve Lineup Improperly

Establ ished/paragraph 4

NCV 95-14-04

Opened/Closed

Fuel Pool Inventory Not Properly

Maintained/paragraph 5

URI 95-14-05

Opened

Operations Surveillance Test 621

Deficiency/paragraph 6

NCV 95-14-06

Opened/Closed

RWP Requirement For Protective

Clothing Not Followed/paragraph 6

URI 94-12-02

Closed

Basis For Closed System Outside

Containment/paragraph 4

.8.

ACRONYMS AND INITIALISMS

CFR

Code of Federal Regulations

CP&L

Carolina Power and Light

CR

Condition Report, Control Room

CV

Containment Vessel

E&E

Energy And Environmental

EPP

End Path Procedure

FHP

Fuel Handling Procedure

FMP

Fuel Management Procedure

HP

Health Physics

LCO

Limiting Condition For Operation

MCC

Motor Control Center

NCV

Noncited Violation

NRC

Nuclear Regulatory Commission

0P&

Operations Surveillance Test

PDR

Public Document Room

PLP

Plant Program Procedure

psi

Pounds Per Square Inch

RFO

Refueling Outage

RHR

Residual Heat Removal

RO

Reactor Operator

RWP

Radiation Work Permit

RWST

Refueling Water Storage Tank

SFP

Spent Fuel Pit

'I

Safety Injection

TS

Technical Specification

URI

Unresolved Item

VIO

Violation

WR/J

Work Request/Job Order