ML14181A582

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Insp Rept 50-261/94-17 on 940625-0723.Violations Noted. Major Areas Inspected:Operational Safety Verification, Surveillance & Maint Observation & Followup
ML14181A582
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 08/15/1994
From: Christensen H, Ogle C, William Orders
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A580 List:
References
50-261-94-17, NUDOCS 9408290038
Download: ML14181A582 (17)


See also: IR 05000261/1994017

Text

s

REG(

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

0

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/94-17

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC

27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducted: June 25 - July 23, 1994

Lead Inspector:

ders

enrRs//Ipct

W.

ders

en' r Resident Inspector

Dite'Signed

Other Inspectors:

.

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e,/esi bnt Inspector

Dfte'Signed

Approved by:

H. 0. Christensen, Chief

Date Signed

Reactor Projects Section 1A

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation, and

followup.

Results:

A violation was identified involving inadequate procedures governing equipment

control, paragraph 3.e. A second violation was identified involving the

licensee's failure to correct improperly routed instrument sensing lines,

paragraph 3.b.1. A third violation was identified involving the licensee's

failure to include wide range penetration pressurization flowmeters in a

calibration program, paragraph 4; a non-cited violation was identified

involving an operator's failure to adequately monitor plant status, paragraph

3.d; and an unresolved item was identified involving RHR system flow

indication concerns, paragraph 3.b.2.

9408290038 940815

PDR ADOCK 05000261

0

PDR

REPORT DETAILS

1.

Persons Contacted

  • R. Barnett, Manager, Projects Management

S. Billings, Technical Aide, Regulatory Compliance

  • J. Brown, Manager, Design Engineering

A. Carley, Manager, Site Communications

  • B. Clark, Manager, Maintenance

D. Crook, Senior Specialist, Regulatory Compliance

J. Eaddy, Manager, Environmental and Radiation Support

  • D. Gudger, Specialist Regulatory Affairs

S. Farmer, Manager, Engineering Programs, Technical Support

  • B. Harward, Manager, Engineering Site Support, Nuclear Engineering

Department

  • S. Hinnant, Vice President, Robinson Nuclear Project
  • K. Jury, Manager, Licensing/Regulatory Programs

J. Kozyra, Acting Manager, Licensing/Regulatory Programs

  • R. Krich, Manager, Regulatory Affairs
  • F. Lowery, Manager, Work Control
  • J. Lucas, Instructor, Technical Training

A. McCauley, Manager, Electrical Systems, Technical Support

  • R. Moore, Acting Operations Manager
  • J. Moyer, Manager, Nuclear Assessment
  • D. Nelson, Manager Outage Management
  • M. Pearson, Plant General Manager

M. Scott, Manager, Reactor Systems, Technical Support

E. Shoemaker, Manager, Mechanical Systems, Technical Support

D. Winters, Shift Supervisor, Operations

  • D. Whitehead, Manager, Plant Support Service

L. Woods, Manager, Technical Support

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

NRC Personnel

  • H. Christensen, Acting Chief, Reactor Project Branch 1, was on site

July 22-23, 1994, to tour site and meet with resident inspectors.

  • Attended exit interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Plant Status

The unit operated at or near full power for the duration of the report

period with no major problems.

2

3. Operational Safety Verification (71707)

a.

General

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with

regulatory requirements. These activities were confirmed by

direct observation, facility tours, interviews and discussions

with licensee personnel and management, verification of safety

system status, and review of facility records.

The inspectors reviewed shift logs, Operation's records, data

sheets, instrument traces, and records of equipment malfunctions

to verify equipment operability and compliance with TS. The

inspectors verified the staff was knowledgeable of plant

conditions, responded properly to alarms, adhered to procedures

and applicable administrative controls, cognizant of in-progress

surveillance and maintenance activities, and aware of inoperable

equipment status through work observations and discussions with

Operations staff members. The inspectors performed channel

verifications and reviewed component status and safety-related

parameters to verify conformance with TS. Shift changes were

routinely observed, verifying that system status continuity was

maintained and that proper control room staffing existed. Access

to the control room was controlled and operations personnel

carried out their assigned duties in an effective manner. Control

room demeanor and communications were appropriate.

Plant tours were conducted to verify equipment operability, assess

the general condition of plant equipment, and to verify that

radiological controls, fire protection controls, physical

protection controls, and equipment tagging procedures were

properly implemented.

b.

Residual Heat Removal Flow Indicator FI-605 Reading Erroneously

At approximately 1:00 p.m. on July 1, 1994, the inspectors

questioned Operations management on the impact of a failed FI-605,

Residual Heat Removal Total Flow Indicator, on Operation's

capability to execute their End Path Procedures. With the RHR

pumps secured, the indicator registered approximately 1000 gpm

flow. The inspectors were concerned that since the instrument is

used during End Path Procedures, EPP-9, Transfer To Cold Leg

Recirculation, and EPP-10, Transfer to Long Term Recirculation,

the erroneous reading could impact the plant's ability to enter

recirculation. This erroneous flow indication had been noted by

Operations following RHR pump operation during OST-251, RHR

Component Test, earlier that morning. In response to the

inspector's question, the plant entered an operability

determination on the RHR system at 2:15 p.m. Additionally,

Maintenance personnel accelerated their efforts to vent FT-605 in

accordance with a work request generated after the instrument

3

failure was noted by Operations personnel.

At 2:35 p.m.

transmitter venting was completed and FI-605 indicated zero flow

with the RHR pumps off. At 8:24 p.m., the operability

determination was completed, concluding that the RHR system was

"...operable with erroneous indication of 1000 gpm on FI-605."

The inspectors reviewed the operability determination, interviewed

personnel involved in its generation, and reviewed the maintenance

history associated with FI-605. Based on this review, the

inspectors concluded that:

-

similar failures of FI-605 had occurred previously

-

neither the engineering evaluation nor the operability

determination specifically addressed the impact that the

erroneous indication would have on the operator's

implementation of the End Path Procedures

-

the engineering memo contained a technical error regarding

the failure of instrument.

Supporting rationale is provided in the following discussion.

1)

FT-605 Maintenance History

The inspectors requested a list of previous WR/JOs

accomplished to correct deficiencies in RHR flow indication

observed on FI-605. Twelve such work requests were

identified in the licensee's electronic database.

(This

database contains maintenance histories for approximately

the last 4 years.)

The inspectors reviewed the 12

completed work packages and noted that 4 of the work

requests described FI-605 anomalies markedly similar to that

observed on July 1, 1994. These 4 WR/JOs, dated May 18,

1991; May 15, 1992; January 23, 1993; and April 21, 1994,

described flow indications as high as 1800 gpm on FI-605

with the RHR pumps secured. In each of these 4 work

requests, the transmitter was equalized or vented to remove

the erroneous flow indication. Three of the WR/JOs

specifically mention air in the sensing lines.

On November 22, 1993, ACR 93-315 was written to address flow

oscillations on FI-605 with RHR in service. The condition

description section of the ACR noted that FT-605 required

its sensing lines to be vented, and that the condition was

repetitive. The ACR evaluation concluded that improperly

sloped sensing lines between the transmitter and the flow

sensing element could exist. The ACR theorized that gas or

air in the lines could be trapped, thereby, causing improper

operation of the transmitter. In response to this

situation, WR/JO 94-ADAIl was generated on February 9, 1994,

to adjust the sensing lines to eliminate any gas or air

4

traps. However, the WR/JO specifically prohibited the

maintenance technicians from moving any sensing line clamps

or fittings. As of July 1, 1994, the WR/JO was scheduled

for performance the following week. On July 8, 1994, the

inspectors independently verified that the sensing lines for

FT-605 failed to rise continuously from the transmitter to

the sensing element. This confirmed licensee observations

made earlier that week. This arrangement was contrary to

the transmitter manufacturer's recommendation that the

sensing lines rise approximately one inch for every foot of

run between the transmitter and the flow sensing element.

At the end of the inspection period, the licensee was making

plans to properly route the sensing lines.

The inspectors noted that the two most recent failures of

FI-605 on April 21, 1994, and July 1, 1994, both occurred

after ACR 93-315 identified gases trapped in improperly

routed FI-605 sensing lines as a potential cause of the

erratic operation of FI-605.

10 CFR 50 Appendix B, Criterion XVI requires in part that

measures be established to ensure that conditions adverse to

quality are promptly identified and corrected. Furthermore,

Criterion XVI requires that corrective action be taken to

preclude repetition of significant conditions adverse to

quality.

Contrary to the above, the licensee failed to take

corrective action for repetitive failures of Flow Indicator,

FI-605, Residual Heat Removal Total Flow, between May 18,

1991; and July 1, 1994. A proposed corrective action to

reroute the associated transmitters sensing line was

identified in February 1994, but was not implemented before

the two most recent failures of the instrument on July 1,

1994; and April 21, 1994. This is identified as a

violation, VIO: 94-17-02, Failure To Correct Improperly

Routed Instrument Sensing Lines While Troubleshooting

Repetitive Gas Binding of RHR Flow Indicator.

On July 15, 1994, the inspectors requested that the licensee

evaluate the potential that the previous instances of

venting FT-605 may be symptomatic of air trapped in the dead

leg of RHR piping immediately downstream of flow element.

This request was based on the inspectors concern that the

upwardly sloping RHR line and lack of a high point vent on

the RHR piping downstream of the flow element could create a

potential water hammer situation. The licensee stated that

this would be evaluated in their ACR addressing the July 1,

1994, failure of FI-605. The inspectors will monitor this

effort as an unresolved item, URI: 94-17-03, RHR System

Concerns Resulting From FI-605 Inspection Effort.

  • 0

5

2)

RHR System Operability

The inspectors reviewed an engineering memo dated July 1,

1994, which evaluated the erroneous FI-605 flow indication

on RHR system operability. The memo, which served as the

technical basis for Operability Determination, OD# 94-26,

concluded that the system was operable despite the 1000 gpm

flow indicated in the idle RHR system.

The inspectors noted that neither the engineering memo nor

the operability determination explicitly discussed the

potential impact the erroneously reading instrument would

have on the operator's ability to implement emergency

procedures. Instead, focusing on the Regulatory Guide 1.97

designation of FI-605, the memo concludes that FI-605's only

function is to provide an indication that the RHR system is

operating. Further, it concludes that Regulatory Guide 1.97

instruments with a higher ranking of significance, such as

core exit thermocouples and loop temperatures would provide

this same information. The inspectors concluded that this

argument was mis-focused, and neglected steps in EPP-9 and

EPP-10 which specifically require the operators to take

actions based on numerical values taken from FI-605. The

inspectors acknowledge licensee arguments that degraded or

improperly adjusted ECCS flows would eventually result in

inadequate core cooling and hence, elevated primary

temperatures and would thus call for the use of functional

restoration procedures which exist to counter this

situation. However, the inspectors concluded that this

approach was less conservative than using properly

operating, installed plant instrumentation to progress

through the pre-defined End Path Procedures. On July 6,

1994, after inspector discussions with the licensee,

Operations management issued a memo to the operators on

these concerns. This memo outlined the potential that

FI-605 could read erroneously following RHR pump

recirculation and that the operators should consult

alternate confirmatory indications of RHR pump performance.

The engineering memo also contained a technical error. It

states that while FI-605 was reading erroneously, ERFIS

indicated the actual flow of zero gpm. The memo attributes

this purported divergence in readings to the operation of a

square-root extractor in the circuit which only modifies the

transmitter signal to the indicator. The engineering memo

notes that the square root extractor is not involved in

other circuit functions such as the RHR pump low flow alarm

annunciator or control of the RHR heat exchanger bypass flow

control valve, FCV-605. Based on this, the memo concluded,

the erroneous reading would not impact RHR system operation

in the cooldown mode.

6

In fact, an ERFIS printout requested by the inspectors,

revealed that the ERFIS input from the FT-605 transmitter

was also approximately 1000 gpm for almost 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> on

June 30, 1994; and July 1, 1994. A significant portion of

this period overlapped the period when FI-605 also indicated

1000 gpm. The inspectors determined from a review of the

shift supervisor logs, that Operations personnel questioned

the divergent ERFIS/FI-605 statement in the Engineering memo

on July 1 and July 2, 1994. When apprised of this error,

the log states that engineering management determined that

the engineering memo conclusions on RHR system operability

remained valid. The inspectors were informed that this

error was not subsequently corrected in the engineering

memo, but would be evaluated in the ACR review of this

issue.

ACR 93-315 made reference to RHR system flow anomalies

documented in a 1990 engineering analysis by Horace Cofer

Associates. The ACR further stated that RHR system

enhancements recommended by the study were not implemented

but instead, alternate improvements were pursued. Near the

end of the inspection period, the inspectors requested that

the licensee provide additional information on historical

RHR system performance problems and efforts implemented to

correct them. At the conclusion of the inspection period

this effort was not complete. The inspectors will track

this effort as part of URI 94-17-03.

c.

Failure To Complete Area Fire Watch Inspection Log

At 2:30 p.m. on July 5, 1994, the inspectors observed that The

Area Fire Watch Hourly Inspection Log posted on the blocked open

EDG A fire door had not been initialled since 10:00 a.m. that

morning. The door had been blocked open to facilitate maintenance

efforts on the EDG earlier that day. The inspectors noted four

initials to document the performance of the hourly fire watches

required by FP-12, Fire Protection Systems Minimum Equipment and

Compensatory Actions, were missing. Following notification of

this observation, the licensee alerted fire protection personnel

and updated the log to reflect the previously undocumented hourly

entries.

The licensee generated an ACR regarding the event and

the plant's Human Performance section also performed an

investigation.

The inspectors reviewed the licensee's investigation and

interviewed one of the maintenance technicians present for the

ongoing maintenance in the EDG A room. Based on this, the

inspectors concluded that the EDG A room probably remained

occupied throughout the 10:00 a.m. to 2:30 p.m. timeframe in

question.

(Since the EDG A room is not a unique security zone,

this conclusion was based upon the ACR and maintenance technician

interview.)

7

The inspectors conclude that the safety significance of the

observation was minimal and most probably reflected a failure to

document the continuous presence of an area fire watch in the

room. The ACR concludes that the failure to designate a single

individual the responsibility for the sheet was a key contributor

to this event. The inspectors concur with this assessment. In

addition to training and counseling on the event, the ACR also

states that the log will be revised to designate a responsible

individual for the hourly reviews.

d.

Operator Failure To Adequately Monitor Plant Status

At 2:19 p.m. on July 7, RCS Loop 2 Flow Indicator, FI-424, failed

to "0".

No annunciator alarms or bi-stable indicator lights were

received. At approximately 2:40 p.m. the Reactor Operator (RO)

started his review of control room indications per Operations

Directive 93-016, Control Room Indicator Review. After completing

his review at approximately 3:15 p.m. he initialed the cover sheet

of the ERFIS printout and initialed the Hot Operation Log. He did

not detect that FT-424 was indicating "0", or that the ERFIS

"Current Quality" code for the ERFIS ID Point Number for FI-424

had printed out as "BAD", or that the 3:00 p.m. ERFIS reading for

that point had printed out as "0".

While doing the 4:00 p.m. Control Room Indicator review, the same

Reactor Operator found FI-424 reading "0"

and asked the Senior

Control Operator (SCO) if he knew of any reason for the "0"

reading. The Reactor Operator checked the 4:00 p.m. ERFIS

printouts and found the quality code for 3:00 p.m. indicating

"BAD" and the reading for FI-424 to be "0".

The Shift Supervisor

was notified of the failed indicator. The Reactor Operator then

went back to the 3:00 p.m. ERFIS printout and found that the

quality code for the point had printed out "BAD" at that time, and

that it was also indicating "0".

He initialed the 3:00 p.m. "BAD"

indication at this time, but did not document that it was a late

entry. After management reviewed the event, the Reactor Operator

was relieved of his watch at 5:40 p.m., and was subsequently

terminated.

Work Request 94-AJNL1 was written and I&C was notified. FT-424

was taken out of service (bi-stable tripped) per Operations Work

Procedure, OWP-31-LFT-4, at 4:25 p.m. A blown fuse was found in

the isolation amplifier for FI-424. All protective functions

remained operable for the channel before and after the bi-stable

was tripped. FI-424 was placed back in service at 7:19 p.m. that

evening.

The Control Room Indicator Review includes monitoring of the RTGB

indicators, recorders, lighted annunciators, Control Room panels,

scheduled ERFIS printouts, alarm printouts, and the Fire Alarm

Computer display. The operator stated that several activities

were in progress at the time of the review, including the

8

performance of MST-021, "Reactor Protection Logic Train "B" at

Power", and maintenance work on feedwater heater level control

switches. He also stated that two individuals were standing at

the RTGB recording information related to FI-605, and that he

stepped around them to continue his review. FI-605 is located in

the same area of the RTGB as FI-424. It appears that the RO

missed reading the indicator as he moved around the individuals at

the RTGB. In any case, the review was inadequate.

Once the RO completed his 3:00 p.m. RTGB review, he started his

review of the ERFIS printouts. The printout is typically 10-12

pages.

On the Hourly Hot Log there were two indications that

problems existed with the FI-424 reading. This log provides a

"Current Quality" code for each of the data points and the actual

hourly reading of each indicator over the last 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period.

The report listed the Current Quality code as "BAD"" and the

3:00 p.m. reading as "0" for FI-424.

The RO indicated that his normal method of reviewing the log was

to check the quality codes and then compare the current reading to

the previous hours. He was uncertain as to how both indications

could have been missed during his review.

Operations Directive 93-016 requires the individual performing the

review to initial the Hot Operations Log Sheet once the hourly

Control Indicator Review is complete. While no other initials are

required, there is a standard practice of initialing the ERFIS

printout cover sheet to indicate that the logs have been reviewed.

The RO indicated that he typically initials the first time that an

indication is "BAD". In this particular case the RO did not

identify that FI-424 had failed to "0" until he performed his

4:00 p.m. RTGB review. Once he noted the failed indicator, he

asked the Senior Reactor Operator if there was any reason the

indicator should be reading "0".

He also reviewed the 4:00 p.m.

ERFIS printout and noted that the indicator read "0" at 3:00 p.m.

and 4:00 p.m. He then retrieved the 3:00 p.m. ERFIS printouts and

determined that the printout indicated that the FI-424 Current

Quality code had been "BAD" and the reading had been "0".

He then

initialed the 3:00 p.m. printout to indicate that this was the

first time that code was listed as "BAD". In an interview with

the Operations Manager and Shift Operations Manager immediately

following the event he admitted that he did not detect the bad

indication at 3:00 p.m., but initialed the 3:00 p.m. quality code

after it was identified during the 4:00 p.m. review. Licensee

management, after reviewing the circumstances of the event,

relieved the Reactor Operator of his watch at 5:40 p.m., and

subsequently terminated him.

Technical Specification 6.5.1.1, Procedures, Tests and

Experiments, requires in part, that written procedures be

established, implemented and maintained covering the activities

9

specified in Appendix A of Regulatory Guide 1.33, Rev. 2, February

1972, including power operation and process control.

Operations Directive 93-016, Control Room Indicator Review

provides instruction to the operators concerning the performance

of control room indication review. Implicit in this requisite is

the expectation that the operators know the status of the plant.

Contrary to the above, at 2:19 p.m. on July 7, 1994, RCS Loop 2

Flow Indicator, FI-424, failed to "0".

At 3:15 p.m., the operator

completed a control room indicator review per Operations Directive 93-016, Control Room Indicator Review. The operator failed to

detect that FI-424 was indicating "0", that the ERFIS "Current

Quality" code for the ERFIS ID Point Number for FI-424 had printed

out as "BAD", or that the 3:00 p.m. ERFIS reading for that point

had printed out as "0".

After careful consideration of the circumstances associated with

this event, foremost being the safety significance, this violation

will not be subject to enforcement action because the licensee's

efforts in identifying and correcting the violation meet the

criteria specified in Section VII.B of the Enforcement Policy.

This event will be tracked as NCV: 94-17-04, Operator Failure To

Adequately Monitor Plant Status.

e.

Followup on Previous Operation Findings

(Closed) URI 94-16-02 Inoperable Post Accident Containment Vent

Path.

As reported in Inspection Report 5-261/94-16, on May 31, 1994,

during a routine tour of the BIT room, the inspectors observed

that the inlet and outlet dampers for the B PACV filter were

closed with clearance tags attached. The inspectors questioned

the shift supervisor on the operability of the system since the

dampers blocked flow through the B train PACV flowpath.

Specifically, the inspectors were concerned that access to these

dampers would be restricted following a LOCA due to prohibitive

radiation levels from adjacent piping in the room which would

contain reactor coolant. Later that day, the clearance tags were

removed and the dampers were returned to the open position.

On June 8, 1994, the inspectors were advised that licensee

analysis indicated that calculated radiation exposures would not

have precluded restoring the system to service following a LOCA.

Based on times obtained to restore the dampers during trial runs

and calculated radiation levels, the licensee stated that the

train could be returned to service with an exposure of about 150

mRem.

During this report period, the inspectors reviewed the regulatory

requirements associated with the PACV system as well as the

description of the system's function and design basis as

delineated in the UFSAR.

The Post-Accident Venting System consists of two full capacity

supply lines through which hydrogen-free air can be admitted to

the containment, two full capacity exhaust lines through which

hydrogen bearing gases may be vented from the containment, and

associated valving and instrumentation.

Operation of the Post-Accident Venting System does not require the

use of fans during venting. Rather, based on the containment

hydrogen concentration and on the hydrogen generation rate, the

operator will determine the flow rate required to maintain the

hydrogen concentration at three percent by volume by venting the

containment. The operator will determine the containment pressure

necessary to obtain the required vent flow, and hydrogen-free air

will be pumped into the containment, using either the station air

compressor or one of the two instrument air compressors, until the

required containment pressure is reached. The air supply will

then be stopped and the supply line isolated. Venting will then

be started by opening the containment exhaust line to the plant

vent through the B train of PACV, and adjusting the throttling

valve to obtain the required flow. Operation will continue as

required to maintain the hydrogen concentration at approximately

three percent by volume.

Operation of the Post-Accident Venting System is performed via

Operating Procedure OP-922, Post Accident Containment Hydrogen

Reduction/Venting System. Although the preferred method of

hydrogen abatement is through the use of a shared hydrogen

recombiner which is normally stored at another facility, in the

event the recombiner was not available, the technique described

above would be employed. In such an event, OP-922 directs the

operators to align the system such that containment would be

vented through the B PACV filter unit, which during the time in

question, would have been isolated by the aforementioned dampers.

The inspectors reviewed the circumstances which lead the operators

to render the PACV filter unit inoperable, yet take no

compensatory measures, or limit the time the system would be

inoperable.

The applicable Technical Specification 3.3.5, requires only that

the valves in the system be operable before the unit is critical.

Although it could be argued that implicit in this requirement is

the requisite that the system be maintained operable during the

operation of the plant, the licensee disagrees. The licensee

stated that the PACV system would not be required to be used until

approximately 30 days after the accident, and that time would be

sufficient to make any necessary repairs to the system if needed.

The inspectors do not totally disagree with the licensee's

position, but surmised that the position was predicated on the

belief that the portions of the system in need of repair would be

readily accessible in the post LOCA environment. This may not be

the case, depending on the component in need of repair.

The inspectors reviewed OMM-005, Clearance And Test Request,

OMM-004, Operations Work Procedure, OMM-007, Equipment Inoperable

Record and OMM-008, Minimum Equipment List And Shift Relief and

interviewed a number of Senior Reactor Operators to

comprehensively evaluate the means employed by the operators in

removing equipment from service. From this review, the inspectors

concluded that there exists no procedural guidance to assist the

operators in properly evaluating and/or removing a piece of

equipment from service if that piece of equipment does not have a

specific TS action statement associated with its removal.

This is

true even if the equipment may be called upon to function during

or after an accident. Two examples of such equipment are the

AMSAC and PACV systems.

10 CFR 50 Appendix B Criterion V requires that activities

affecting quality shall be prescribed by documented instructions,

procedures, or drawings of a type appropriate to the

circumstances, that these instructions, procedures or drawings

include appropriate acceptance criteria, and that the activities

be performed in accordance with these instructions, procedures, or

drawings.

On May 31, 1994, the inspectors concluded that there exists no

procedural guidance to assist the operators in properly evaluating

and/or removing a piece of equipment from service if that piece of

equipment does not have a specific TS action statement associated

with its removal, (examples are fire protection equipment, RETS

equipment, and dedicated shutdown equipment), even though the

equipment in question may be called upon to function during or

after an accident.

Two examples of such equipment are the AMSAC and PACV systems.

This lead operators to render the B train of the PACV system

inoperable with no time limit on the time the equipment could

remain inoperable or if the equipment could be returned to

service, during or after an accident. This is identified as a

violation, VIO: 94-17-01, Inadequate Procedures Governing

Equipment Control.

URI 94-16-02, Inoperable Post-Accident

Containment Vent Path, is closed.

4.

Maintenance Observation (62703)

a.

General

The inspectors observed safety-related maintenance activities on

systems and components to ascertain that these activities were

conducted in accordance with TSs and approved procedures. The

inspectors determined that these activities did not violate LCOs

12

and that required redundant components were operable. The

inspectors verified that required administrative, material,

testing, radiological, and fire prevention controls were followed.

In particular, the inspectors observed/reviewed the following

maintenance activities detailed below:

WR/JO 94-BYG191

Calibrate Narrow Range PPS Flow

Transmitters

WR/JO 94-ABAW1

Repair Air Leak On Solenoid For

EDG B

WR/JO 94-AJCQ1

Repair Air Leak Between DA-19B and

DA-20B

b.

PPS Wide Range Flow Instruments

The inspectors witnessed performance of a portion of WR/JO 94

BYG191 Calibration Of Narrow Range Flow Transmitters on June 23,

1994. The conduct of the calibration was satisfactory.

During the post-maintenance review of the work, the inspectors

questioned the licensee on why no calibration was performed on the

wide range flow indicators. These wide range rotameters were

installed in May 1992 by MOD-1094 to expand the range of PPS flow

rates which could be monitored by installed plant instrumentation.

Though the "C" train PPS wide range instrument had been in service

at least since the end of RFO-15 (in

excess of three months),

neither it nor any of the other wide range PPS flow instruments

were included in the licensee's calibration program. Given that

the licensee utilizes the PPS system to accomplish 10 CFR 50

Appendix J and Sensitive Leak Rate Testing per TS 4.4.1.2.a, the

inspectors were concerned that required testing was being

accomplished using instruments outside the calibration program.

In response to their questions, the inspectors were provided

Engineering Evaluation 93-065, Rotameter Calibration and Range

Evaluation dated July 26, 1993.

This EE concluded that

calibration of the wide range PPS rotameters was not necessary

unless improper operation of the instruments was suspected.

Instead, the EE recommended an inspection of the rotameters at

least every refueling outage.

The inspectors reviewed the EE and concluded that the logic

presented to not routinely calibrate the wide range flow

transmitters was weak. Specifically, the EE:

-

cited contacts with other utilities, many of which

calibrated rotameters used in alternate applications

-

failed to address the implications of a TS 4.4 bases

sentence which states that the PPS flow measurement

13

accuracy is within plus or minus one percent.

(This

was noted in a licensee review of the EE but dismissed

by stating that the PNSC had approved a then proposed

TS basis change.)

-

failed to resolve a conflict with a requirement in

Section 8 of the corporate QA manual that instruments

used to verify data points required by TS be in a

calibration program. (This issue was also raised by a

licensee review of the EE but no clear rebuttal was

made by the NED author.)

-

failed to document consideration of the fact that

ANSI/ANS 56.8-1987, Containment System Leakage Testing

Requirements, recommends specific calibration

frequencies for flow instruments used in Type B

testing.

(The licensee is not committed to this

standard.)

10 CFR 50 Appendix B Criterion XII requires that measures be

established to assure that instruments used in activities

affecting quality are properly controlled and calibrated.

Contrary to the above, on June 23, 1994, the penetration

pressurization system wide range flowmeters were not included in

the licensee's calibration program. At the time of this

observation, the C train penetration pressurization system

flowrate was being monitored by the wide range instrument. This

is a violation, VIO 94-17-05: Failure To Include Wide Range

Penetration Pressurization Flowmeters In Calibration Program.

The inspectors were advised at the end of the inspection period,

that the an engineering evaluation will be performed to address

the appropriate calibration interval for the PPS wide range

flowmeters. Additionally, the licensee stated their intention to

generate an ACR to review this event.

5. Surveillance Observation (61726)

a.

General

The inspectors observed certain safety-related surveillance

activities on systems and components to ascertain that these

activities were conducted in accordance with license requirements.

For the surveillance test procedure listed below, the inspectors

determined that precautions and LCOs were adhered to, the required

administrative approvals and tagouts were obtained prior to test

initiation, testing was accomplished by qualified personnel in

accordance with an approved test procedure, and test

14

instrumentation was properly calibrated. Specifically, the

inspectors witnessed/reviewed portions of the following test

activity:

OST-252

RHR Component Test (Quarterly)

b.

RHR System Component Test

On July 6, 1994, the inspectors witnessed performance of

Operations Surveillance Test, OST-252, RHR Component Test

(Quarterly). This test cycles various RHR system related valves

to assess their performance and operational readiness.

Overall, the inspectors concluded that the performance of the test

was satisfactory. Strengths noted included consistent use of the

licensee's self-check program by the operators, identification and

documentation of procedural deficiencies by control room

watchstanders, and involvement of the SCO and STA in overseeing

and monitoring the test.

During performance of the test, the inspectors questioned the

shift supervisor on the need to declare an entry into a TS LCO

action statement based on the cycling of the RHR-752 A and B and

RHR-759 A and B valves. These valves isolate the appropriate RHR

pump suction and RHR heat exchanger discharges, respectively. The

valves are normally open and do not receive a signal to open when

an SI is initiated. The inspectors were concerned that if an SI

signal were actuated with any of the 4 valves shut, a train of RHR

would be unavailable for automatic injection. Following this

discussion and after a review of the system drawing, the SS

entered and exited the appropriate TS LCO action statement prior

to cycling these valves.

The inspectors noted that entry into a TS LCO action statement was

not documented for the last two performance of this surveillance

test contained in the vault. However, the inspectors are aware

that action statements are routinely entered for some other safety

system surveillances. During followup discussions on this issue

on July 7, 1994, licensee management indicated they had generated

an ACR to evaluate the need for a consistent approach to TS LCO

action statement entry for surveillance testing as a result of a

recent, similar NAD finding. The inspectors will monitor licensee

efforts in this area during monitoring of surveillance testing.

6.

Exit Interview (71701)

The inspection scope and findings were summarized on July 22, 1994, with

those persons indicated in paragraph 1. The inspectors described the

areas inspected and discussed in detail the inspection findings listed

15

below and in the summary. Dissenting comments were not received from

the licensee. The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

Item Number

Description/Reference Paragraph

VIO: 94-17-01

Inadequate Procedures Governing Equipment

Control/paragraph 3.e.

VIO: 94-17-02

Failure To Correct Improperly Routed Instrument

Sensing Lines/paragaph 3.b.1.

URI: 94-17-03

RHR System Concerns Resulting From FI-605

Inspection Effort/paragraph 3.b.2.

NCV: 94-17-04

Operator Failure To Adequately Monitor Plant

Status/paragraph 3.d.

VIO: 94-17-05

Failure To Include Wide Range Penetration

Pressurization Flowmeters In Calibration

Program/paragraph 4.

. 7. List of Acronyms and Initialisms

ACR

Adverse Weather Condition

AMSAC

ATWS Mitigating System Actuation Circuitry

AWC

Adverse Condition Report

ATWS

Anticipated Transient Without Scram

BIT

Boron Injection Tank

ECCS

Equipment Core Cooling System

EDG

Emergency Diesel Generator

EE

Engineering Evaluation

EPP

End Path Procedure

ERFIS

Emergency Response Facility Information System

FI

Flow Indication

FT

Flow Transmitter

gpm

Gallons Per Minute

I&C

Instrument & Control

LCO

Limiting Condition For Operation

LOCA

Loss of Coolant Accident

MST

Maintenance Surveillance Test

NAD

Nuclear Assessment Department

NCV

Non-Cited Violation

NED

Nuclear Engineering Department

OMM

Operation Management Manual

PACV

Post Accident Containment Vent

PPS

Penetration Pressurization System

QA

Quality Assurance

RETS

Radiological Environmental Technical Specifications

RHR

Residual Heat Removal

RTGB

Reactor Turbine Gage Board

16

STA

Shift Technical Adviser

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

WR/JO

Work Request/Job Order