ML14178A499

From kanterella
Jump to navigation Jump to search
Insp Rept 50-261/94-08 on 940226-0326.Violations Noted. Major Areas Inspected:Operational Safety Verification, Surveillance Observation,Maint Observation & Engineered Safety Feature Sys Walkdown
ML14178A499
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 04/15/1994
From: Christensen H, William Orders
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A495 List:
References
50-261-94-08, 50-261-94-8, NUDOCS 9405230019
Download: ML14178A499 (18)


See also: IR 05000261/1994008

Text

61k REGo/

UNITED STATES

0 oNUCLEAR

REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/94-08

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducted:, February 26 - March 26, 1994

Lead Inspector:

,, & ,ff5Jyi

g4

4'/- /

W T. Orders, S hior)Resident Inspector

Date Signed

Accompanying Inspectors:

C. R. Ogle, Resident Inspector

R. C. Haag, Senior Resident Inspector - Summer

P. C. Hopkins, Resident Inspector - Catawba

J. L. Starefos, Project Engineer

M. T. Widmann, Project Engineer

Accompanying Personnel:

E. Carpenter, Project Engineer, NRR

B. Mozafari, Project Manager, NRR

Approved by:

0 -

L-

ZIZ

I

I

-/

1

H. 0. Christensen, Acting Chief

Dite Signed

Reactor Projects Section 1A

Division of Reactor Projects

SUMMARY

Scope:

This routine, unannounced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation,

engineered safety feature system walkdown, plant safety review committee

activities, and followup.

Results:

One violation was identified involving the licensee's failure to follow

procedure when terminating CV purge, paragraph 3.

9405230019 940415

PDR

ADOCK 05000261

a

PDR

2

A second violation with two examples was identified involving the licensee's

failure to take adequate corrective actions pertaining to entry into a high

radiation area without a survey meter, paragraph 3, and inadequate corrective

action pertaining to diesel engine maintenance, paragraph 5.

A non-cited violation was identified involving deficiencies in calibration and

issue of mechanical test equipment, paragraph 5.

REPORT DETAILS

1.

Persons Contacted

R. Barnett, Manager, Projects Management

S. Billings, Technical Aide, Regulatory Compliance

  • A. Carley, Manager, Site Communications

B. Clark, Manager, Maintenance

T. Cleary, Manager, Technical Support

D. Crook, Senior Specialist, Regulatory Compliance

J. Eaddy, Manager, Environmental and Radiation Support

  • D. Gudger, Specialist, Regulatory Affairs

S. Farmer, Manager, Engineering Programs, Technical Support

  • J. Harrison, Manager, E&RC Technical Support

B. Harward, Manager, Engineering Site Support, Nuclear Engineering

Department

  • S. Hinnant, Vice President, Robinson Nuclear Project
  • K. Jury, Manager, Licensing, Regulatory Programs

J. Kozyra, Acting Manager, Licensing/Regulatory Programs

  • R. Krich, Manager, Regulatory Affairs

A. McCauley, Manager, Electrical Systems, Technical Support

R. Moore, Acting Operations Manager

A. Padgett, Manager, Environmental and Radiation Control

  • M. Pearson, Plant General Manager

M. Scott, Manager, Reactor Systems, Technical Support

E. Shoemaker, Manager, Mechanical Systems, Technical Support

D. Winters, Shift Supervisor, Operations

L. Woods, Manager, Technical Support

  • Attended exit interview.

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Plant Status

The unit began the report period in cold shutdown. The licensee

was forced to shut the unit down on February 18, 1994, when the

scavenging air blower on the B EDG failed during a post

maintenance test. The unit remained shut down until March 20,

1994 while the licensee completed repairs on the B EDG, and

retrieved a loose part which had been detected in the C S/G. The

unit was made critical at 7:42 p.m. on March 20, and was placed on

line at 11:55 p.m. on the following day. The report period ended

with the plant stable at 90% power in preparation for reactor

physics testing.

2

3. Operational Safety Verification (71707)

a.

General

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with

regulatory requirements. These activities were confirmed by

direct observation, facility tours, interviews and discussions

with licensee personnel and management, verification of safety

system status, and review of facility records.

The inspectors reviewed shift logs, Operation's records, data

sheets, instrument traces, and records of equipment malfunctions

to verify equipment operability and compliance with TS.

The

inspectors verified the staff was knowledgeable of plant

conditions, responded properly to alarms, adhered to procedures

and applicable administrative controls, cognizant of in-progress

surveillance and maintenance activities, and aware of inoperable

equipment status through work observations and discussions with

Operations staff members. The inspectors performed channel

verifications and reviewed component status and safety-related

parameters to verify conformance with TS. Shift changes were

routinely observed, verifying that system status continuity was

maintained and that proper control room staffing existed. Access

to the control room was controlled and operations personnel

carried out their assigned duties in an effective manner. Control

room demeanor and communications were appropriate.

Plant tours were conducted to verify equipment operability, assess

the general condition of plant equipment, and to verify that

radiological controls, fire protection controls, physical

protection controls, and equipment tagging procedures were

properly implemented.

b.

Mid-Loop Operation

The inspectors reviewed the licensee's preparations for RCS

draindown and subsequent mid-loop operation to support an eddy

current inspection of the C SG. Eddy current inspection was

implemented following the discovery of 2 loose parts on the

generator secondary side and is discussed in Inspection Report

94-10. The inspectors also attended the PLP-37, Conduct Of

Infrequently Performed Tests Or Evolutions, brief for the first

crew involved in the draindown; verified the calibration of

selected instruments used for the draindown; and witnessed a

portion of the operator training provided for the evolution.

Additionally, the inspectors were in attendance for key portions

of the draindown commencing on March 3, 1994. The inspectors were

also present for the termination of the draindown at approximately

-66 inches below the vessel flange on March 4, 1994.

3

Overall, the inspectors concluded that the licensee's preparations

and subsequent control of the inventory reduction were good.

Particular strengths were noted in control room communications;

awareness of RCS water level and deviations between redundant

instruments; and control of maintenance which could impact the

plant or distract watchstanders.

On March 5, 1994, with the RCS in mid-loop, a noise was detected

by the licensee coming from the operating RHR pump. The noise was

depicted in the shift supervisor's log as an unusual noise perhaps

like gas in solution. RHR system flows, pump discharge pressures,

vibration readings, and RHR motor currents were all evaluated as

normal by the licensee. The licensee concluded that the condition

was probably moderate but acceptable vortexing or flow

oscillations in the system. The licensee stated that contact with

the pump vendor revealed that the noise was not an immediate

concern but could lead to increased seal leakage if extended

operation with the noise was conducted.

The inspectors entered the RHR pit to monitor the noise firsthand.

The inspectors heard a low frequency rumbling noise coming from

the suction of the pump. The noise was cyclic in nature and

occurred approximately every 10-15 seconds. No vibrations or

movement of the A RHR pump-or its associated piping was observed

by the inspectors coincident with the noise. Based on these

observations and the licensee's evaluation, the inspectors have no

further questions on this noise.

While in the RHR pit, the inspectors noted several minor material

deficiencies such as duct tape on the B RHR motor junction box and

missing air intake screens for A RHR motor. These were identified

to the licensee for resolution.

On March 8, 1994, while reviewing GP-008, Draining the Reactor

Coolant System, the inspectors noted that the procedure as

written, deviated from the licensee's commitment to Generic Letter 88-17. Section 5.5 of the procedure required that 4 core exit

thermocouples from ICCM "A" or 4 core exit thermocouples from ICCM

"B" be operable with the RCS less than -36 inches. The licensee's

response to Generic Letter 88-17 stated that 8 core exit

thermocouples, 4 per train, would be available for this evolution.

This discrepancy was identified to the licensee.

On March 9, 1994, the inspectors noted that GP-008 had been

revised to reflect that 4 core exit thermocouples from each train

were required. The inspectors reviewed the shift supervisor's log

for the draindown and noted that the licensee did not take

advantage of the procedural authorization to reduce the

temperature monitoring to 4 thermocouples. Both trains of

thermocouples remained operable for the evolution. Therefore, the

licensee did not deviate from their commitment to the NRC during

this particular evolution. The inspectors did not review

4

documentation for any prior entries into mid-loop to see if the

same was true due to the infrequent performance of this evolution

and the difficulty in recovering information related to

thermocouple operability. However, a review of previous revisions

to GP-008 by the inspectors revealed that this procedural

capability to reduce the thermocouples required was carried

forward from the revision which originally incorporated the GL 88-17 guidance.

On March 10, 1994, the licensee filled the RCS in accordance with

GP-008, Draining the Reactor Coolant System and GP-001, Fill and

Vent of the Reactor Coolant System, thereby, exiting the mid-loop

and reduced inventory conditions. The inspectors witnessed the

increase in RCS inventory from -6 inches to the indicating range

of the pressurizer. The evolution was adequately controlled. The

inspectors have no further questions on this evolution.

c.

Incorrect Radiation Monitor Setpoints

On March 14, 1994, E&RC technician sampling the plant vent,

recognized that an incorrect setpoint was entered in R-14C, Plant

Stack, Noble Gas Radiation Monitor. Following discussions with

control room personnel, the setpoints of R-14C as well as R-11 and

R-12, CV Air Or Plant Stack Particulate Radiation Monitor and CV

Air Or Plant Stack Noble Gas Radiation Monitor respectively, were

restored to the proper values.

Subsequent licensee investigation revealed that the incorrect

setpoints occurred while securing a continuous CV purge earlier

that day. As required by step 8.1.2.12 of Operating Procedure,

OP-921, Containment Air Handling, adjustments to the radiation

monitor setpoints were made when the purge was terminated.

However, the setpoints were incorrectly taken from release permit

GRW 94-050. This release permit had expired two weeks earlier on

February 26, 1994. However, at the time the continuous CV purge

was secured, the control room copy of this permit had not been

administratively closed out nor had it been purged from the RO's

desk. Thus, it incorrectly remained in the active release folder

and was available for use by the operator. The licensee's

investigation concluded that only R-14C was set non

conservatively. It further concluded that due to inherent safety

margins associated with the instrument setpoint calculations, at

"..no time was a setpoint used that would not have caused an alarm

if a 10 CFR 20 concentration [had] been exceeded."

The inspectors reviewed the licensees ACR evaluation generated in

response to this event. Additionally, the inspectors reviewed OP 921 and key release forms associated with the incident. The

inspectors also interviewed the reactor operator who used the

incorrect release form.

5

Overall, the inspectors concluded that the reactor operator failed

to follow OP-921 when securing the continuous CV purge. As a

result, an expired release permit was used to set three radiation

monitor setpoints. Technical Specification 6.5.1.1, Procedures,

Tests, and Experiments, requires in part, that written procedures

be established, implemented, and maintained, covering the

activities recommended in Appendix A of Regulatory Guide 1.33,

Rev. 2, 1978, including procedures for operation of the reactor

building ventilation and gaseous effluent monitoring systems.

Operating Procedure, OP-921, Containment Air Handling, requires

that radiation monitor setpoints be properly established following

the termination of a continuous containment vessel purge.

Contrary to the above, three radiation monitor setpoints were

improperly established following the termination of a continuous

containment vessel purge on March 14, 1994. As a result, a non

conservative setpoint existed for approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> on

radiation monitor R-14C, Plant Stack, Noble Gas Radiation Monitor.

This is identified as a violation, VIO: 94-08-01, Failure to

Follow Procedure When Terminating CV Purge.

d.

High Radiation Area Entry Without Survey Meter

On March 17, 1994, four individuals entered the non-regenerative

heat exchanger room, a posted high radiation area without a survey

meter as required by TS 6.13.1.A.

This was discovered when a licensee chemistry instructor observed

the individuals in the area without a survey meter. The three

contractors and one NED engineer had entered the non-regenerative

heat exchanger room as part of a modification walkdown of the

auxiliary building ventilation system. In response to this event,

the licensee denied RCA access to the individuals involved,

generated an ACR, and subsequently modified the controls of HRAs.

This included locking HRA doors where possible and increased

-postings and warning signs.

The inspectors reviewed the licensee's ACR generated for the

event, interviewed the licensee engineer and lead contractor

involved, and interviewed the cognizant E&RC manager involved.

The inspectors also reviewed written statement obtained from

individuals involved in the entry.

-- Overall, the inspectors concluded that the individuals entered the

room, despite the posting, as a result of a non-cognitive error on

the part of the individuals conducting the walkdown. As described

by one of the individuals involved, the walkdown team was so

engrossed with following the ventilation system that they did not

observe the high rad area posting at the door.

The inspectors noted that this occurrence was similar to a

November 1, 1993, event in which two mechanics entered the

6

mechanical penetration area, a high radiation area, without a

survey meter. Though an ACR was generated, the corrective

actions identified failed to prevent this occurrence.

10 CFR 50, Appendix B, Criterion XVI, requires that corrective

actions be taken to preclude repetition of conditions adverse to

quality.

Contrary to the above, the licensee failed to take adequate

corrective action to a November 1, 1993, entry into a high

radiation area by two maintenance technicians without a survey

meter in that a similar event occurred on March 17, 1994. This is

one of two examples which in the aggregate constitute Violation

94-08-02, Inadequate Corrective Action To Preclude Repetitive

Entry Into A High Radiation Area Without A Survey Meter, And

Inadequate Corrective Action To Preclude Recurring Diesel Engine

Failure.

Two violations were identified in this area.

4.

Followup of NOUE - RCS Leakage Greater Than 10 GPM (93702)

At 5:15 a.m. on March 18, 1994, a NOUE was declared, in accordance with

EAL-2 flowchart criteria, for RCS leakage greater than 10 gpm. The leak

had been recognized at approximately 2:15 a.m. earlier that morning

while in the process of removing the RHR system from service and

restoring it to a normal standby injection mode. The leak was

terminated at approximately 2:45 a.m. when the RHR to letdown line

valve, HCV-142 was isolated. A subsequent leak rate calculation at 4:08

a.m. in accordance with OST-051 established that the post-leak leakage

rate was 0.36 gpm. The NOUE was terminated at 5:39 a.m..

The inspectors were notified of the event from a phone call by the shift

supervisor at 5:43 a.m. and via the licensee's beeper notification

system at approximately 5:50 a.m..

The inspectors reported to the site

and monitored the licensee's post-leak activities from approximately

7:15 a.m. to 9:00 a.m..

In response to the event, the licensee formed an incident investigation

team to review the event. The team's report (Final, Rev 1) identified

the leakpath as from the CVCS to RHR system through HCV-142, and then

through the RHR system minimum flow recirculation line and RWST to RHR

valves to the RWST. The report established that the leak occurred as a

result of seat leakage past HCV-142, RHR to letdown line valve, and

commenced when the RWST to RHR valves, SI-862 A & B, were opened at

approximately 1:17 a.m..

The report stated that the leak rate was

between 14 and 22 gpm and leakage was stopped when the leaking HCV-142

was isolated. The report also identified that the seat leakage of HCV

142 was a known, documented material deficiency, the repairs to which

had been deferred.

7

In response to this event, the inspectors reviewed the incident review

team's (Final, Rev 1) report as well as selected ERFIS data used in its

preparation. The inspectors also reviewed log entries for the event and

interviewed key individuals involved.

Based on this inspection effort, the inspectors concurred with the

review team's identification of the leak path and start time. The

inspectors independently calculated an RCS leak rate of approximately 12

gpm and hence, concluded that the licensee's NOUE declaration was

appropriate. However, the inspectors were troubled by the delay which

occurred between the recognition of the leak by the on-shift operators

and the NOUE declaration. According to log entries, the operators

become concerned about the potential for an RCS leak at approximately

2:15 a.m. based on excessive makeups. Log entries and operator

interviews revealed that the licensee continued to pursue these

indications and by about 2:45 a.m. had identified and isolated the

leaking HCV-142. However, the NOUE declaration was delayed until 5:15

a.m.; approximately 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after the leak was terminated. The

inspectors interviewed key individuals involved in the decision making

process for the NOUE declaration to better understand the basis for this

delay.

From these interviews, the inspectors determined that the operating crew

was unable to accurately establish whether the RCS leak rate exceeded

the 10 gpm threshold for the NOUE. This was attributed to inconclusive

data gathered on plant parameters even after the leak was isolated. The

shift supervisor indicated to the inspectors that he was aware of the

leak and understood the 10 gpm NOUE threshold. However, he indicated a

strong desire to determine the leak rate accurately prior to declaring

the NOUE. Faced with this situation, and after consultation with

management, the shift supervisor requested the STA manager come to the

site to assist in the leak rate determination. After this decision was

made, the onsite NAD manager contacted the Plant General Manager and

informed him of the onshift control room NAD observer's estimate of RCS

leakage in excess of the NOUE threshold. At 5:15 a.m., after additional

consultation with the plant general manager, the shift supervisor

declared the NOUE.

The inspectors reviewed data available to the operators to assist in the

determination of the leak rate. Eleven, near continuous makeups of

approximately 75 gallons each occurred between about 1:50 a.m. and 2:45

a.m..

These makeups occurred despite no net change in pressurizer level

and a 6 inch decrease in VCT level.

The change in RCS temperature

during these makeups was about 0.6F. While the RHR system was being

cooled down and realigned during a portion of this interval, the

inspectors noted that the vast majority of this cooldown was complete by

2:15 a.m.. While RHR contraction may have added to the apparent RCS leak

rate, the inspectors noted that VCT level continued to decrease even

after the RHR system cooldown was completed.

Based upon this information the inspectors concluded that the operating

shift had sufficient information available to allow a more timely NOUE

8

declaration. The failure of the operating crew to properly determine

the leak rate in an expeditious fashion is considered a weakness.

After additional investigation, and after the end of the inspection

period, the licensee issued a supplement to the incident review team's

report. This supplement primarily examined issues regarding the

timeliness of the declaration of the NOUE. It concluded that the shift

supervisor had sufficient information to declare the event prior to the

termination of the leak. Furthermore, the supplement stated that 3

supervisory/oversight personnel external to the crew, but present in the

control room, all recommended a more timely NOUE declaration. It also

revised the report's leak rate estimate to 10.8 gpm. The inspectors

reviewed the supplemental report and have no further questions on this

event.

During their review of the ERFIS data the inspectors noted that the VCT

level control system was terminating makeup prematurely. This was

identified to the licensee for resolution.

5.

Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

--accordance with TS, approved procedures, and appropriate industry codes

and standards. The inspectors determined that these activities did not

violate LCOs and that required redundant components were operable. The

inspectors verified that required administrative, material, testing,

radiological, and fire prevention controls were adhered to.

In particular, the inspectors observed/reviewed the following

maintenance activities detailed below:

WR/JO 94-AERJI

Troubleshoot the Speed Sensing Switch For

LSR/EER Contact On A EDG

WR/JO 94-ADXZ6

Steam Generator C Manway Installation

WR/JO 94-AEMW1

Check Closing Time On RHR Pump A Breaker

WR/JO 94-AERK1

Calibration Of EDG A Cylinder Number

8 Thermocouple

WR/JO 94-AEQZ1

Camera Inspection Of EDG A Cylinder Number

8

a.

Inadequate Corrective Actions To Repair EDG "B"

On Saturday, February 12, 1994, the licensee formed a team to

investigate problems that caused the EDG "B" to fail to start

during a routine surveillance test.

9

On February 17, a mechanic identified that the pin on the

counterweight side of the air flapper valve was missing.

Replacing the valve internals was evaluated but it was determined

that replacement parts for the valve were not in stock.

The pin was subsequently found wedged between the valve body and

the diffuser plate below the flapper valve. It was visually

inspected and evaluated as being in good shape.

The team members discussed several repair options:

Replacing the pin with a new one.

This was ruled out because there was not a replacement pin

in stock.

Performing a test to determine if the pin could be tack

welded or duplicated.

This was ruled out because the valve was made of aluminum

and could not be welded; and there was not enough time to

duplicate the pin and meet the time requirements of the TS

action statement.

.

Replacing the pin with a bolt.

This was ruled out because the drawing for the diesel

indicated a pin was used in the original design. To replace

the pin with a bolt would require a Engineering Evaluation

(EE) and the team did not believe this could be accomplished

within the remaining TS action statement time.

Reusing the old pin and staking the flapper valve.

This option was chosen. Maintenance was to put 4 indentions

in the end of the pin to increase the "interference" fit.

At approximately 9:45 a.m. that morning a mechanic reinstalled

the pin and made two stakes on the flapper using a hammer and

center punch. The mechanic was concerned about making any

additional stakes believing it would weaken the metal.

The

opposite end of the pin was not staked.

At approximately 10:00 a.m., the installation of the pin was

complete. Upon completion of the job, the mechanical maintenance

foreman inspected the job and indicated that he felt the staking

was adequate to hold the pin in place.

Several members of the team and management visually inspected the

repair and found no problem. Permission to reassemble the valve

90

was given.

10

At approximately 1:13 p.m. that afternoon, the diesel was started

and loaded to 2500 kw and ran for an hour without incident. At

approximately 3:00 p.m. a fast speed start was performed. The EDG

was secured at 5:07 p.m..

At 6:10 p.m. a PNSC meeting convened to discuss the "B" EDG

problems and repair efforts. The PNSC discussed the fact that the

pin had been replaced and that slow and fast speed starts had been

completed. The resident inspectors brought to the PNSC's

attention that neither of the starts had been conducted at normal

standby system conditions. The PNSC agreed to that a cold start

at ambient condition should be successfully completed prior to

declaring the EDG operable.

At 11:56 p.m. that evening, the licensee started the EDG per OST

409. The engine start was considered normal.

At 12:01 a.m., the

output breaker was closed and engine was loaded to 11 kw. A few

minutes later, a clanging noise was heard in the blower inlet

piping immediately followed by a loud noise in the scavenging air

blower. The operator shutdown the engine.

Subsequent maintenance activities located the aforementioned air

flapper valve pin. It had fallen out of the valve, had been

ingested by the scavenging air blower, and had inflicted

catastrophic damage to both the blower and both turbochargers.

The air flapper valve failure demonstrates inadequate corrective

actions taken in response to a malfunction.

10 CFR 50 Appendix B, Criterion XVI, Corrective Action, requires

in part that measures be established to assure that conditions

adverse to quality, such as failures, malfunctions, defective

material and equipment, are promptly identified and corrected

including the measures to assure that the cause of the condition

is determined and corrective action taken to preclude repetition.

Contrary to the above, on February 17, 1994, the licensee's

corrective actions to repair the B EDG air flapper valve was

inadequate to assure that the cause of the condition was

determined and preclude recurrence in that the valve pin was

improperly secured, a fact which led to extensive engine damage.

This is one of two examples which in the aggregate constitute

Violation 94-08-02, Inadequate Corrective Action To Preclude

Repetitive Entry Into A High Radiation Area Without A Survey

Meter, And Inadequate Corrective Action To Preclude Recurring

Diesel Engine Failure.

b.

Primary Manway Installation

On the evening of March 9 and early morning of March 10, 1994, the

inspectors witnessed the installation of the hot and cold leg

primary manways on steam generator C. This was accomplished in

11

accordance with CM-206, Removal And Reinstallation of the Steam

Generator Primary Manway Covers.

Overall, the conduct of this maintenance evolution was

satisfactory. Noteworthy was the strong performance on the part

of the mechanical maintenance technicians assigned to this effort.

Despite the fact that manway installations are typically performed

by contractor personnel at H. B. Robinson, the work was

accomplished smoothly in the high dose, confined work area of the

steam generator platform.

However, the inspectors did note several items which may have

distracted from the smoothest possible performance of the task.

These included a cluttered laydown area immediately adjacent to

the crane wall; ineffective communications headsets; and a 400

mR/hr hot spot on the manway insert shielded container which went

undetected until well into the evolution. The inspectors also

noted a minor inconsistency in the manway stud installation

technique between the two manways. The hot leg team used speed

wrenches to install them, the cold leg team performed the same

activity by hand. The speed wrenches allowed for quicker stud

installation in the high dose environment. While none of these

items rose to the level of a safety concern, they were discussed

with the cognizant management personnel.

The inspectors have no

further questions on this activity.

No violations or deviations were identified. Based on the

information obtained during the inspection, the area/program was

adequately implemented.

c.

Deficiencies In Calibration And Issue Of Mechanical Test Equipment

On March 10, 1994, the licensee's Nuclear Assessment Department

(NAD) discovered significant deficiencies in the calibration and

issue of mechanical test equipment (M&TE). Specifically, these

deficiencies were:

1)

Calibration standard were being incorrectly utilized

resulting in the issuance of non-calibrated torque

wrenches.

2)

Qualification of personnel calibrating and issuing torque

wrenches was determined to be unsatisfactory. This was

evidenced by improper calibration techniques as well as a

lack of documentation certifying personnel qualification.

The calibration, control, and issue of M&TE at RNP is the

responsibility of Materials and Contract Services (M&CS).

At approximately 6:00 p.m. on March 10, 1994, NAD issued a "Stop

Work" order, suspending the issuance of M&TE. Parameters for

rescinding the "Stop Work" order were specified as follows:

12

1)

Personnel calibrating and issuing torque wrenches were

to be appropriately qualified.

2)

Short term compensatory measures were to be established to

provide reasonable assurance that mechanical M&TE provide

reasonable assurance that mechanical M&TE calibration and

issues were being properly conducted.

At approximately 4:00 P.M. on March 11, 1994, the Manager

Materials and Contract Services presented a letter to the Plant

Manager and the Manager of RNP, NAD, outlining compensatory

measures that had been implemented. Based on these measures, the

"Stop Work" order was rescinded.

Three primary concerns were identified - 1) inadequate

documentation relative to the training of personnel, 2) suspect

calibration capabilities of "Qualified" personnel, 3) the validity

of torque wrench calibrations prior to work stoppage.

The issue of inadequate documentation of training focused on the

inability of the NAD team to locate training records and

qualification certificates in the HBR Training Section's records.

The training records were located in the supervisors desk. In

three instances he had failed to sign the qualification sheets for

individuals and in numerous cases failed to forward the training

records to the HBR training Section as required. All of the

employees had received the required training.

The capability of the responsible personnel to accurately perform

calibrations was questioned by NAD personnel.

It was determined

that four factors tend to mitigate these concerns:

1)

Independent review of paperwork - M&TE is calibration

checked prior to issuance to the field and upon return to

the issue area. The calibration certificates are reviewed

by a third party prior to close-out. Any unresolved

discrepancies-or abnormalities are addressed at this time.

2)

Ongoing calibrations by various individuals - Typically the

pre-check of M&TE and the post-check are performed by

different individuals. Subsequent issues are likely to be

performed by different individuals still.

Any problems in

performing the calibrations would be quickly discovered due

to the ongoing process by different individuals.

3)

Rechecks of equipment using the newly implemented standards

have failed to reveal any problems with the equipment or

out-of-spec calibrated equipment.

4)

Requalification testing of individuals did not reveal any

areas of concern relative to the calibration and checking of

M&TE.

13

An overriding concern involved the validity of torque wrench

calibrations prior to the work stoppage and the consequences with

regard to plant equipment operability. A multi-disciplined team

was formed to determine the answer to this question.

The team determined that there were approximately 2200 Certificate

of Calibration sheets completed since 1991, in which improperly

certified torque wrenches (a torque wrench certified with a

transducer below 20 percent of full scale) were used in the plant.

Testing performed by a contractor lab indicated that the

transducers were actually acceptable to approximately one percent

of scale. This reduced the number to 26 calibration sheets where

torque wrenches were certified with a transducer below one percent

of scale. All 26 instances were reviewed and the licensee

concluded that the plant equipment was not affected by the

improper torque wrench calibration check.

10 CFR 50, Appendix B, Criterion XII, Control Of Measuring And

Test Equipment requires that measures be established to assure

that tools, gages, instruments, and other measuring and testing

devices used in activities affecting quality be properly

controlled, calibrated, and adjusted at specified periods to

maintain accuracy within necessary limits.

Contrary to the above, measures established were inadequate in

0

that:

1)

Calibration standards were being incorrectly utilized

resulting in the issuance of non-calibrated torque wrenches.

2)

Qualification of personnel calibrating and issuing torque

wrenches was inadequate as evidenced by improper calibration

techniques as well as a lack of documentation certifying

personnel qualification.

The failure to establish adequate M&TE control measures is a

violation. This violation will not be subject to enforcement

action however, because the licensee's effort in identifying and

correcting the violation meet the criteria specified in Section

VII.B of the Enforcement Policy.

This is identified as a non-cited violation, NCV: 94-08-03 Failure To

Establish Adequate M&TE Control Measures.

d.

Diesel Generator Room Cooler Operability

In report 94-04, the inspectors identified an Unresolved Item, 94

04-03, involving the evaporative air coolers which were installed

to cool the emergency diesel generator rooms.

In that report, the inspectors documented that on January 20,

1994, the service water supply to one of the coolers failed due to

14

freezing. A review of the system's design determined that the

service water piping was installed as non-Q/non-seismic. The

licensee's immediate corrective action entailed isolating service

water to the coolers.

The inspectors asked the licensee to determine if the coolers are

required diesel generator support equipment. Current design

documentation is not specific in that regard. The licensee's

initial opinion was that the coolers are not required for diesel

operability. At the end of report period 94-04, the licensee had

not completed the analysis to support their contention. Pending

completion of that analysis, the issue was carried as an

Unresolved Item, 94-04-03, Evaporative air Cooler/Diesel Support.

During the current report period, the inspectors were provided a

copy of Engineering Evaluation 94-023, Rev. 0. On page 1 of 2 of

that evaluation, the licensee states in part, that during normal

plant operation, with the diesels not operating, temperature

maintenance of the diesel rooms is provided by the reactor

auxiliary building normal ventilation system. At diesel start-up,

the diesel room cooling function is provided by the respective

diesel generator room ventilation systems. At the time of diesel

start-up, the diesel generator room ventilation system supply fan,

cooler, and the exhaust fan are required to maintain the room

below the specified design limit of 104*F on a design basis summer

day of 950F.

Contrary to the above information, the inspectors noted in

memorandum dated March 28, 1994, that "There is no evidence that

cooling beyond that provided by the room supply and exhaust fans

is required for operability. Therefore, EAC-1 & 2 coolers are not

required and are appropriately designated non-Q."

The inspectors brought the conflicting information to the

licensee's attention and requested that adequate technical

justification be supplied to support continued diesel operability.

Pending the receipt of this analysis, this issue will remain

Unresolved.

One violation and one non-cited violation were identified in this

area.

6.

Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities

on systems and components to ascertain that these activities were

conducted in accordance with license requirements. For the surveillance

test procedures listed below, the inspectors determined that precautions

and LCOs were adhered to, the required administrative approvals and

tagouts were obtained prior to test initiation, and testing was

accomplished by qualified personnel in accordance with an approved test

procedure. Upon test completion, the inspectors verified the recorded

15

test data was complete, and test discrepancies were properly documented

and rectified, and that the systems were properly returned to service.

Specifically, the inspectors witnessed/reviewed portions of the

following test activities:

OP-604

Diesel Generators "A" and "B" (A EDG only)

EST-109

Auxiliary Feedwater Pumps Flow Testing

(Refueling)

No violations or deviations were identified in this area.

7.

Exit Interview (71701)

The inspection scope and findings were summarized on April 5, 1994 with

those persons indicated in paragraph 1. The inspectors described the

areas inspected and discussed in detail the inspection findings listed

below and in the summary. There were no dissenting comments nor did the

licensee identify any of the materials provided to or reviewed by the

inspectors during this inspection as proprietary.

Item Number

Description/Reference Paragraph

VIO: 94-08-01

Failure to Follow Procedure When

Terminating CV Purge.(paragraph 3)

VIG: 94-08-02

Inadequate Corrective Action To Preclude

Repetitive Entry Into A High Radiation Area

Without A Survey Meter, And Inadequate

Corrective Action To Preclude Diesel

Engine Failure.

(paragraphs 3 & 5)

NCV: 94-08-03

Failure To Establish Adequate M&TE Control

Measures. (paragraph 5)

8.

List of Acronyms and Initialisms

ACR

Adverse Condition Report

E&RC

Environmental and Radiation Control

EAL

Emergency Action Level

EE

Engineering Evaluation

ERFIS

Emergency Response Facility Information System

GL

Generic Letter

GP

General Procedure

gpm

gallons per minute

HCV

Hand Control Valve

HRA

High Radiation Area

M&TE

Maintenance and Test Equipment

M&CS

Materials and Contract Services

NAD

Nuclear Assessment Department

NOUE

Notice of Unusual Event

RCA

Radiation Control Area

16

RCS

Reactor Coolant System

RHR

Residual Heat Removal

RNP

Robinson Nuclear Project

RWST

Refueling Water Storage Tank

SG

Steam Generator

SI

Safety Injection

VCT

Volume Control Tank

0