ML14178A430

From kanterella
Jump to navigation Jump to search
Insp Rept 50-261/93-34 on 931120-1206.No Violations Noted. Major Areas Inspected:Event Description,Core Neutron Flux Anomalies & Broken Fuel Insp Tool During Refueling
ML14178A430
Person / Time
Site: Robinson 
Issue date: 12/28/1993
From: Peebles T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A428 List:
References
50-261-93-34, NUDOCS 9401210109
Download: ML14178A430 (48)


See also: IR 05000261/1993034

Text

tpj

REG'(,

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

AUGMENTED INSPECTION TEAM (AIT) INSPECTION

Report Nos.:

50-261/93-34

Licensee: Carolina Power and Light Company

Docket Nos.:

50-261

License Nos:

DPR-23

Facility Name: H. B. ROBINSON UNIT 2

Inspection Conducted:

November 20-December 6, 1993

Team Leader:

,

_

__

_/,

/

3/k

Thomas A. Peebles, Chief

Date Signed

Operations Branch,

Division of Reactor Safety

Team Members:

M. E. Ernstes, Operator Licensing Examiner

E. D. Kendrick, Nuclear Engineer

S. M. Matthews, Quality Assurance Engineer

C. R. Ogle, Resident Inspector

B. H. Rogers, Reactor Engineer

J. E. Tedrow, Senior Resident Inspector

Approved by

22 1q3

1bert F. G' so

Direc r,

Date Signed

Division of ea tor Safety

9401210109 940105

PDR

ADOCK 05000261

G

PDR

EXECUTIVE SUMMARY

The objectives of the inspection were to determine the scope and the causes of

the events observed during the post refueling startup of H. B. Robinson Unit 2

and to evaluate the licensee's response to these events.

H. B. Robinson Unit 2 went critical on November 12, 1993. Criticality

parameters were within the expected range, and initial physics testing did not

reveal any core anomalies. On November 14, 1993, with the reactor at an

indicated power of 20 percent, a heat balance - done in response to management

questions about diverse power indications - showed that the actual power was

30 percent.

On November 16, 1993, flux mapping indicated core peaking factor problems.

These problems were confirmed by a second flux map. The licensee and the fuel

supplier (Seimens Power Corporation) discovered on November 18, 1993, that six

fuel assemblies had been misconstructed in that asymmetrically loaded,

burnable poison was incorrectly positioned in the core. The reactor had been

shut down November 17, 1993, in order to repair a steam leak in the secondary

plant.

The Augmented Inspection Team was chartered on November 19, 1993, and was

onsite November 20-24 and November 29-December 2, 1993. Additionally, members

of the inspection team were at the Seimens' Richland, Washington facility

.November

29-December 3, 1993, and a public exit meeting was held December 6,

1993.

The principal findings and conclusions of the Augmented Inspection Team were:

1. Licensee oversight and assessment of the fuel constructor, refueling

activities, startup preparations (including the calibration of nuclear

instruments and operator training), and the conduct of operations during

the startup were deficient.

2. Power range nuclear instruments had been mis-calibrated because of an

inadequate understanding of the core geometry, and the operators did not

diagnose the incorrectly reading power range instruments, although there

were sufficient indications available in the control room. Specifically,

lessons learned from an event at another plant in which power range

nuclear instruments were not reading correctly were not effectively

utilized to prevent this occurrence.

3. The plant operated with fuel having mis-positioned burnable poison. This

did not result in fuel damage, but damage could have occurred if the plant

had operated above 30 percent.

4. The six misconstructed fuel assemblies were the result of inadequate

fabrication controls and oversight by the fuel supplier.

5. The licensee's post event review and evaluation were adequate.

TABLE OF CONTENTS

Pagie

1.0

INTRODUCTION - AIT FORMATION AND INITIATION . ... . . . . . . . . .

1

1.1

Background

1.2

AIT Formation

2.0

EVENT DESCRIPTION ....... ... .. ... ... ... ....

2

3.0

MISCALIBRATED NUCLEAR INSTRUMENTS..........

......

. .

6

3.1

Review of root cause of miscalibrated nuclear instruments

identified during startup

3.1.1

AIT Findings and Conclusions

3.2

Assessment of the Adequacy of Nuclear Instrumentation

Calibration Procedures

3.2.1

AIT Findings and Conclusions

3.3

Assessment of operator performance relative to the nuclear

instrumentation miscalibration problem

3.3.1

Operator Interviews

3.3.2

Review of Operator Training

3.3.2

AIT Findings and Conclusions

4.0

CORE NEUTRON FLUX ANOMALIES . ...... ... .. ... ... ..

15

4.1

Assessment of root cause and safety significance of

the core neutron flux anomalies with regard to fuel and

Technical Specification limits

4.1.1

AIT Findings and Conclusions

4.2

Assessment of the cause and extent of fuel manufacturing

errors at Siemens Power Corporation-Nuclear Division Fuel

Manufacturing Facility

4.2.1

AIT Findings and Conclusions

4.3

Assessment of the extent and effectiveness of fuel

assembly verification at Siemens Power Corporation

Nuclear Division

4.3.1

AIT Findings and Conclusions

0

III

4.4

Assessment of the extent and effectiveness of fuel

verification at the site

4.4.1

AIT Findings and Conclusions

4.5

Assessment of the Siemens Power Corporation-Nuclear

Division analysis of the core neutron flux anomalies

4.5.1

AIT Findings and Conclusions

4.6

Assessment of the licensee's oversight of Siemens Power

Corporation- Nuclear Division fuel analysis and Quality

Assurance programs

4.6.1

AIT Findings and Conclusions

5.0

BROKEN FUEL INSPECTION TOOL DURING REFUELING . . . . .......

24

5.1

Determination of the root cause of the broken fuel

inspection tool event

5.1.1

From the On-site Inspection

5.1.2

From the Inspection at Siemens Power Corporation

Nuclear Division

5.1.3

AIT Findings and Conclusions

5.2

Determination of the effectiveness of licensee oversight of

contractor fuel handling activities

5.2.1

AIT Findings and Conclusions

5.3

Assessment of the adequacy of Siemens Power Corporation

Nuclear Divisions Quality Assurance program for the manufacture

of special

fuel tools

5.3.1

AIT Findings and Conclusions

5.4

Assessment of the effectiveness of Siemens Power Corporation

Nuclear Divisions program for notifying licensees of known

deficiencies in either hardware or services provided

5.4.1

AIT Findings and Conclusions

6.0

ASSESSMENT OF THE LICENSEE'S INVESTIGATION OF THESE EVENTS . . . .

34

6.1

Assessment of the effectiveness and thoroughness of the

licensee's investigation of these issues

6.1.1

AIT Review of the licensee's Nuclear Instrumentation

Miscalibration Review Team Assessment

6.1.2. AIT Review of the licensee's Robinson Fuel Loading

Investigation Team Assessment

7.0

EXIT MEETING .. ..... ....

....

...... ....

..

35

APPENDIX A - AIT CHARTER AND SUPPLEMENT

APPENDIX B - THE LICENSEE REVIEW TEAMS

APPENDIX C -

EXIT ATTENDANCE

FIGURE X -

FUEL INSPECTION TOOL

FIGURE Y - GADOLINIUM FUEL ASSEMBLY AS DESIGNED VS AS-BUILT

FIGURE Z - RECOMMENDED ASSEMBLY TO USE FOR NUCLEAR INSTRUMENTATION CALIBRATION

III)i

1.0 INTRODUCTION

1.1

Background

During the restart of H. B. Robinson Unit 2, following the cycle 15 refueling

outage, which refueled the unit with the Cycle 16 core, the NRC was aware of

the following sequence of events:

DATE

TIME

EVENT

11/12/93

12:14 am

Commenced reactor startup.

11/12/93

6:19 am

Reactor critical.

Estimated Critical Position

met.

11/14/93

7:00 am

Reactor at the point of adding heat.

11/14/93

8:00 am

Intermediate Range nuclear instrumentation NI-36

bypassed.

11/14/93

9:22 am

Operations realized that there was a reactor

power mismatch:

30 percent actual; 20 percent

indicated.

11/14/93

9:00 pm

Loose Parts Monitoring System discovered

deenergi zed.

11/14/93

Evening

Site team formed to review startup.

11/16/93

4:00 am

Flux map indicates abnormal peaking factors.

(Core design problem.)

11/16/93

6:15 pm

Leaking weld identified (at FW-13B).

11/16/93

8:40 pm

Second flux map confirms peaking factors.

11/17/93

1:13 am

Started unit shutdown to repair FW-13B.

11/17/93

Morning

Licensee management review team on-site to

investigate.

11/18/93

Afternoon Licensee and fuel vendor decide that core

misloading is the cause of the core peaking

factor problem.

1.2

AlT Formation

On November 19, 1993, senior NRC managers concluded that events surrounding

this startup warranted further independent evaluation; an Augmented Inspection

Team was formed, and a Confirmatory Action Letter was issued by Region II. A

detailed charter was developed to guide the team. In addition to the above

events, loose parts had been identified during fuel handling activities in the

T

wspent

fuel pit.

Inspection of this item was included in the charter (the AlT

III2

Charter is Appendix B).

The team began its inspection on site on November 20,

1993.

2.0

EVENT DESCRIPTION

The following is the detailed sequence of events associated with the

November 12, 1993, startup until Hot Shutdown was reached on November 17,

1993. The team found no major disagreements from the licensee's sequence of

events. A detailed narrative begins at paragraph 3.0.

DATE

TIME

EVENT

11/12/93

12:14 am

Shut reactor trip breakers, commenced

reactor startup per Procedure GP-003.

11/12/93

12:20 am

Commenced Procedure EST-050, Refueling

Startup Procedure. (Control Rod

withdrawal then dilute to criticality.)

11/12/93

6:08 am

Deenergized Source Range Nuclear

Instruments, and NI-32 hung up at 45

cps.

11/12/93

6:18 am

Start Up Rate meter pegged high. Stopped

Procedure EST-050. Power stabilized at

108 amps in the Intermediate Range.

11/12/93

6:19 am

Reactor critical.

11/12/93

11:49 am

Cleaning of Start Up Rate meter selector

switch complete.

11/12/93

1:00 pm

Recommenced Procedure EST-050

11/12/93

2:00 pm

Commenced low power physics testing per

Procedure EST-050.

11/13/93

11:40 am

Completed low power physics testing.

11/13/93

1:28 pm

Reactor at one percent.

11/13/93

2:07 pm

NI-44 returned to service following

Procedure EST-50.

11/14/93

12:52 am

NI-35 Out Of Service for setpoint

changes.

11/14/93

3:12 am

NI-35 returned to service.

3

11/14/93

3:14 am

NI-36 Out Of Service for setpoint

changes.

11/14/93

3:55 am

NI-36 returned to service.

11/14/93

6:39 am

Latched main turbine.

Operator Distractions

Left main turbine stop valve bypass

won't open due to isolated instrument

air valve, IA-3221, shut. Unable to

bypass around and equalize across left

stop valve.

Watchstation turnover.

Turbine rolling approximately 200 rpm

due to leakage past the governor valves.

Operators concerned over Procedure

GP-005 precaution to minimize time

turbine below 200 rpm.

Turbine vibration alarms occurred.

11/14/93

7:47 am

Turbine valve trip test. Number two

intercept reheat valve does not indicate

closed.

11/14/93

7:51 am

Turbine relatched.

11/14/93

7:54 am

Turbine at 1800 rpm.

11/14/93

8:08 am

Unit on line. Power escalation

commenced.

Operator Distractions

Sluggish voltage regulator response.

No Mega Volt Amperes Reactive indication

on gauge board.

Load dispatcher reports telemetry

failure.

All four turbine governor valves

indicate shut.

11/14/93

8:15 am

Intermediate Range NI-36 is bypassed at

Nuclear Instrumentation cabinet to

preclude reactor trip.

  • I

4

Operator Distractions

Low level in "A" Steam Generator.

No feed flow indication on A & C Steam

Generators.

Steam flow greater than feed flow

alarms.

Feed Water Heater Alarms.

Swap of electro-hydraulic oil pumps due

to A pump not unloading.

Main steam reheater vent to condenser

valve (FCV-1334) indication problem.

Balance of plant operator required to

hold valve switch on gauge board to

open.

System engineer reports turbine

vibrations recorded .in

control room

twice field reading.

Condensate header low pressure alarm due

to condensate pump recirculation valve

FCV-1446 hung open.

System engineer identifies one of four

generator H2 coolers isolated.

11/14/93

8:42 am

Main Feedwater regulating valves in

auto. Power escalation stopped to

stabilize reactor power.

11/14/93

8:57 am

Reactor power stabilized at 20 percent

as indicated by Power Range Nuclear

Instrumentations

11/14/93

9:02 am

Electrical operator questions indicated

Nuclear Instrumentation power based on

turbine first stage pressure equates to

approximately 26 percent power.

11/14/93

9:22 am

Engineering Technical Services manager

questions difference between reactor

power indicated by Power Range Nuclear

Instrumentations and net Mega Watts

electric. Operators estimate 30 percent

reactor power based on loop delta Ts.

5

11/14/93

9:40 am

Generator volt-ampere (mega volt amperes

reactive) knife, switch found open.

Closed switch and restored mega volt

amperes reactive indication.

11/14/93

10:26 am

Initial calorimetric data per Procedure

OST-10 indicates reactor power is 30.26

percent.

11/14/93

10:44 am

Operations Manager and Engineering

Technical Support Manager notified of

initial calorimetric results per

Procedure OST-10

Reactor engineer

support requested.

11/14/93

10:47 am

Decreased reactor power to less than 30

percent.

11/14/93

11:01 am

Procedure OST-10 complete. Calculated

reactor power is 30.26 percent.

11/14/93

12:20 pm

Regulatory affairs notified of potential

TS 3.10.7.1 violation for exceeding

three percent/hr ramp rate immediately

following refueling.

11/14/93

2:00 pm

Procedure EST-53 indicates actual

reactor power is 30.03 percent.

11/14/93

2:57-3:12 pm

Instrumentation and controls personnel

recalibrated Power Range Nuclear

Instrumentati ons.

11/14/93

9:00 pm

Loose parts monitor discovered disabled.

When placed in service, alarm received

on primary side of Steam Generator C.

11/14/93

11:30 pm

Noise from potential loose part on Steam

Generator C subsided.

11/16/93

4:00 am

Operations notified that flux map

results identified peaking factors that

require additional analysis.

11/16/93

6:10 am

NI-35 out of service to reset high flux

trip and rod stop.

11/16/93

5:33 pm

NI-35 high flux trip and rodstop reset.

No retest due to procedural problems and

plant conditions.

  • 6

11/16/93

8:10 pm

Feedwater leak identified on main

feedwater pump "A" discharge. Second

flux map indicates core flux

irregularities.

11/17/93

12:35 am

Feedwater leak traced to weld crack for

feedwater drain valve, (FW-13B).

Crack

growing.

11/17/93

1:13 am

Unit shutdown commenced at one

percent/min per Procedure GP-006.

11/17/93

1:35 am

Station output breakers opened.

11/17/93

4:14 am

Reactor shutdown.

11/17/93

8:39 am

NI-35 failed Procedure OST-001.

11/18/93

11:16 am

Completed Shutdown Procedure GP-006.

3.0

MISCALIBRATED NUCLEAR INSTRUMENTS

3.1

Review of the root cause of the miscalibrated nuclear instruments

identified during startup.

During the plant startup on November 14, 1993, licensee personnel discovered

that power range nuclear instrumentation indicated power readings were

approximately ten percent lower than actual reactor power. The licensee

attributed the cause for this discrepancy to be the effect that the new

reactor core had on the power range nuclear instrument indication and an

improper understanding of core geometry considerations. During the cycle 15

refueling outage, the licensee installed a very low leakage core. The new

core load not only reduced the neutron flux present at the reactor vessel, but

also reduced the neutron flux which reached the nuclear instrument detectors

located on the outside periphery of the vessel. T *o

account for this change in

the neutron flux, the intermediate range and power range nuclear instruments

were recalibrated to adjust the previous cycle instrument currents to

predicted newcycle instrument currents.

The team reviewed the licensee's startup testing which was performed following

the refueling outage and the associated nuclear instrumentation work packages

which documented the calibration of the nuclear instruments with particular

emphasis on the intermediate range and power range detectors. In addition,

the licensee's investigation into this event was reviewed.

Procedure FMP-002, "Nuclear Instrumentations Post Refueling Adjustment

Determination," was implemented by the licensee to quantify the projected

impact on the nuclear instrumentation by the new core loading. The team

verified the licensee's calculations in this procedure for the new power range

100 percent currents and the intermediate range rod block and high level trip

setpoints.

The team reviewed Work Request WR 93BMZw1 and verified that the

100 percent currents were implemented intothe power range channels.

7

Westinghouse issued a letter to the licensee on March 16, 1988, providing

guidance on nuclear instrumentation concerns when implementing a core design

change which reduces the neutron leakage from the core. This letter was

initiated because of core design changes made at the licensee's Harris

facility. The letter recommended a correction factor which was calculated

from the average relative power of four fuel bundles, which comprised the

complete outer diagonal nearest the power detector. This guidance was not

incorporated at plant Robinson even though corporate licensee personnel were

aware of the Westinghouse letter which was implemented at the Harris

facility. Instead, licensee personnel developed the calculations contained in

Procedure FMP-002 based on previous cycle performance data which agreed more

closely with historical core data. These calculation utilized the two nearest

outer diagonal fuel assemblies and a third inner assembly (second diagonal)

for relative power comparisons.

The licensee determined that their method was in error following communication

with the fuel vendor, who stated that the outer fuel assemblies contributed

approximately 16 percent each to the flux indicated on the detector while the

inner assembly contributed only 2-3 percent. The incorrect methodology was

not detected during previous.startups because previous core loadings

fortuitously had fuel assemblies with similar relative power loaded in the

inner position and on the periphery of the outer diagonal, thereby canceling

any mathematical averaging errors. The new, low leakage core on the other

hand, specified that a much higher average relative power assembly be loaded

  • in

the inner position which differed substantially from the outer diagonal

assemblies. When the averaging calculations were performed for the new core

load, the error in methodology caused a discrepancy between predictions of

approximately 90 percent. Based on the information from the licensee's

vendors, the team concluded that the root cause for the nuclear instrument

miscalibration was due to the incorrect methodology used in calculating the

power range currents. This was confirmed by licensee personnel who calculated

the predicted power range indication using the correct methodology. These

calculations indicated that when actual power was 30 percent the correctly

calibrated power range instruments would have indicated approximately 38

percent, which would have been conservative and acceptable.

Also during this outage, both of the source range and intermediate range

nuclear instrument detectors were replaced due to aging. The methodology used

in the intermediate range calculations agreed between Westinghouse and the

licensee and therefore the calculations for intermediate range rod stop and

high level trip setpoints were unaffected.

As part of the startup test program, Procedure EST-050, Refueling Startup

Procedure, was used to establish the high power reactor protection system

trip setpoint at 45 percent. The TS limit for this setpoint is 109 percent

power. The action to reduce this setpoint was taken in response to a similar

nuclear instrument miscalibration which occurred in December 1998 at the

licensee's Harris facility which is similar in design to the Robinson plant.

The team reviewed work request WR 93HUK001 completed on November 9, 1993,

which implemented the 45 percent trip setpoints. The team considered this

action by the licensee to be very beneficial which would have limited a

potential power excursion. The team calculated that a reactor trip would have

  • II8

occurred once actual power reached approximately 67.percent, which is far

below the technical specification limit. The team considered the conservative

action to reduce the high power trip setpoint after refueling outages to be a

program strength which helped reduce the potential consequences of this event.

3.1.1

AIT Findings and Conclusions

The team determined that improper methodology for predicting Power

Range currents was used by Robinson. Inadequate corporate/site

oversight and communications contributed to this use of improper

methodology. The licensee corporate fuels staff was aware of the

Westinghouse recommended method for predicting currents, its basis,

and its implementation from prior experience at the Harris plant.

As a safety precaution, the setting of the Power Range High Power Flux

Trip had been set at 45 percent vice 109 percent prior to startup,

this would have limited any power increase to less than an allowed

value. However, the core flux anomalies coupled with the power range

nuclear instrument misalignment would have resulted in high neutron

flux in localized areas of the core if power had reached the indicated

45 percent.

3.2

Assessment of the adequacy of station nuclear instrumentation

calibration and refueling procedures.

The licensee's nuclear instrument calibration procedures were reviewed as well

as work packages which were performed on the nuclear instruments during the

plant startup. Both of the source range and intermediate range nuclear

instrument detectors were replaced. The team discussed the procedure guidance

with licensee personnel and compared the procedure scope with control wiring

diagrams and the system technical manual to determine completeness. The

following procedures were reviewed:

Nuclear Instrument System Source Range

Nuclear Instrumentations Pulse Amplifier NM-101,

Attenuation, Discrimination and High Voltage Power Supply

NQI1

Nuclear Instrument System Intermediate Range Channels NI-35

& NI-36

Nuclear Instrumentations Power Range Channel NI-41, NI-42,

NI-43, and NI-44

  • PIC-107 Power Level Indication at the Power Range

e PIC-109 Nuclear Instrument System Over Power Trip High Range

Adjustment for the Power Range Flux Detectors

  • PIC-110 Nuclear Instrumentations Intermediate Range (NI-35 & NI-36)

Compensating Voltage Adjustment and Loss of Compensating

Voltage Alarm Adjustment

.The

team found the guidance provided in the licensee's calibration procedures

to be adequate and closely agreed with the system technical manual.

However,

9

the team found a few deficiencies in the data sheets provided in Procedures

LP-704, LP-705, and PIC-109. The data sheets were considered by the team to

be confusing since procedure sections were not specifically identified for

data recording. Further, the team noticed that acceptance criteria was not

included on the data sheets. This information was only included in the body

of the procedure. Although this practice did not prevent successful

completion of the procedure, it hampered supervisory review of the completed

package. Licensee personnel had already identified this matter and

appropriate procedure changes were planned to upgrade the data sheets.

From a review of the work packages, the team identified implementation

problems. The intermediate range nuclear instruments were not calibrated with

the new rod stop and high trip setpoints calculated by Procedure FMP-002 until

after the reactor was critical and at the point of adding heat on November 14,

1993. This situation was contrary to the requirements of Procedure EST-050,

step 3.10, which documented that the Nuclear Instrumentation adjustments per

Procedure FMP-002, had been completed prior to taking the core critical.

The

team discussed with the responsible individual, why this requirement was

initialed as completed without the appropriate adjustments being completed.

The person responsible indicated that due to miscommunication with the

maintenance technicians, he believed that the adjustments had been completed.

The licensee's investigation had also identified this deficiency. The team

reviewed the safety significance of this situation. The intermediate range

rod stop and high level trip setpoints were not required by the licensee's

.technical

specifications. Since the setpoints which were present at the time

of reactor criticality were set at the old cycle values and were lower than

the new predicted currents, startup with the old setpoints was considered to

be conservative by the team.

In addition, the work packages (WR 93-AJTB1, WR 93-AJBG2) associated with the

replacement of the intermediate range NI-35 and NI-36 detectors, were reviewed

by the team. Typically the licensee replaces the source range detectors every

outage due to aging effects, and the intermediate range detectors are likewise

replaced at the same time due to location. No discrepancies were identified.

3.2.1

AIT Findings and Conclusions

Written procedures were generally considered to be adequate.

Deficiencies were noted in some data sheets; for example, acceptance

criteria and tolerance bands were not specified, and procedure

sections were not specifically identified. The licensee had already

identified these issues, and the procedures were included in an

upgrade program but had not been completed prior to startup.

Implementation problems were noted in establishing the Intermediate

Range Nuclear Instruments' high level trip and rod stop setpoints

prior to criticality - they were not done until the point-of-adding

heat. Also, source range NI-32 channel was not recalibrated following

detector replacement even though the procedure and technical manual

recommends that this should be done. Procedural and work controls

were lacking; however, the old setpoints were found to be conservative

by the team.

10

3.3

Operator Performance relative to Nuclear Instrumentation

miscalibration problem.

3.3.1 Operator Interviews

At 12:14 a.m. on November 12, 1993, following the completion of Refueling

Outage 15, the licensee commenced a reactor startup. The startup and

subsequent power escalation were performed in accordance with three

procedures:

General Procedure, GP-003, "Normal Plant Startup From Hot

Shutdown to Critical;"

Refueling Startup Procedure, EST-050; and General

Procedure, GP-005, "Power Operation."

Procedure GP-003 established the

initial conditions for the startup. Procedural control was transferred to

EST-050 for initial criticality and zero power physics testing. The

escalation of power into and through the power range was accomplished with

Procedure GP-005. This sequence and other key events of the startup are

documented in Paragraph 2.0. At 9:22 am on November 14, 1993, with power

stabilized at 20 percent on the nuclear instruments, the Manager of

Engineering Technical Support questioned the apparent mismatch between power

range Nuclear Instrumentations and net Mega Watts electric. Estimates of

reactor power by the operators from loop delta Ts, indicated that power was

close to 30 percent. A subsequent calorimetric calculation confirmed this

estimate and the power range Nuclear Instrumentations were set to thirty

percent. The increase in power to 30 percent caused a violation of technical

.specifications

in that the 3 percent per hour rate of power rise limitation

between 20 percent and 100 percent of reactor power specified in Technical

Specification 3.10.7,was exceeded. The actual rate of power increase was

approximately 10 percent in a 15 minute period. A flux map performed at 30

percent power indicated flux tilt and anomalous power levels. The crew

maintained power at 30 percent while efforts were made to resolve the flux

anomalies. A second flux map provided similar results. Following the

discovery of a secondary side steam leak, a reactor shutdown was commenced on

November 17, 1993.

The team attributed the mismatch between the actual power and the Power Range

Nuclear Instrumentation readings to be one result of an inadequate calibration

procedure. This conclusion and its basis are discussed in Paragraph 3.1.

The team reviewed the startup to assess operator performance relative to the

nuclear instrument miscalibration problem. This review consisted of

interviews of control room operators, as well as reviews of instrument traces,

plant computer printouts, the completed startup procedures and the shift

supervisor and reactor operator logs.

Each watchstander interviewed, cited prevention of a plant trip as his major,

if not primary function. None of those interviewed verbally attached a

similar significance to monitoring instrumentation for failure or

inaccuracies. This focus on preventing a trip may have resulted in key

individuals concentrating on a limited range of plant parameters resulting in

11

ineffective oversight by members of the watch section. This reduced the

potential for earlier identification of the power mismatch. Site management

was not aware of this focus and had not provided adequate direction to cause

the shift to be also be observant of the overall plant conditions.

The shift supervisor expressed concern prior to the watch over an Intermediate

Range Nuclear Instrumentation reactor trip. He experienced one during a

startup at Robinson in 1988. Adding to this concern, was an E-mail message

from a reactor engineer sent the previous evening, warning of potential

problems in the response of the Intermediate Range Nuclear Instrumentation

during the power ascension. The memo addressed Intermediate Range Nuclear

Instrumentation detector setpoint adjustments and the potential for achieving

the intermediate range rod stop (20 percent current equivalent on the

Intermediate Range Nuclear Instrumentation) prior to satisfying the P-10

interlock (10 percent on the Power Range Nuclear Instrumentations). The memo

did not mention the adjustments to the Power Range Nuclear Instrumentations

performed during the outage. In essence, the memo led the operators to

believe that the Power Range Nuclear Instrumentations would be a more reliable

indicator of reactor power than the Intermediate Range Nuclear

Instrumentation. Furthermore, the discussion in the memo on satisfying the

intermediate range rod stop at 20 percent prior to satisfying the P-10

interlock at 10 percent, reduced the potential for the operators to question

an apparent 10 percent mismatch between the Intermediate Range Nuclear

Instrumentation and Power Range Nuclear Instrumentations. The memo reinforced

  • the

crew's concern for a trip on the intermediate range high flux prior to

satisfying the P-10 interlock. For these reasons, a shift supervisor,

supplementing the crew, was assigned to monitor the Intermediate Range Nuclear

Instrumentation to ensure that it did not exceed the trip setpoint prior to

bypassing the trip functions.

This assignment prevented this individual from

maintaining an overview of the plant during a portion of the power ascension.

Several watchstanders cited difficulties in control of steam generator level

and Tave as significant distractions during the startup. Review of computer

printouts indicated that severe oscillations occurred in the steam generator

levels until automatic level control was established. These difficulties were

in part complicated by the lack of feed flow indication at low power levels on

two of the steam generators. One reactor operator was dedicated to control of

feed flow and the steam generator water levels. The SRO was also involved

with the steam generator water level control as this was recognized as having

a high potential of causing a reactor trip.

The team was unable to determine categorically if these difficulties in plant

control were more severe than in prior startups or severe enough to mask the

power mismatch. However, the team noted that even if the entire efforts of

the three control board operators were directed at plant control problems,

three shift supervisors and a shift technical advisor were still present to

perform oversight and overview of the startup.

Throughout the interviews, watchstanders identified distractions as detracting

from their efforts during the startup. The major distractions that occurred

at key points in the startup are included in the timeline discussed in

Paragraph 2.0. While it is obvious that any distraction would impact operator

12

performance during the startup, the team was unable to assess the severity of

this impact. The team did note that the operator's self-assessment of the

impact of these distractions covered a broad spectrum from severe to minimal

impact.

A thorough, pre-evolution brief was not conducted coincident with watch relief

immediately prior to the power escalation. The team identified that the crew

did not review the precautions in Procedure GP-005 in detail prior to assuming

the watch. Step 4.22 of Procedure GP-005 was added as a corrective action to

a similar event which occurred at Shearon Harris in 1989. This step states:

"During power ascension, all indications of reactor power level should

be monitored and compared. Periodically, indications such as core

delta T and turbine first-stage pressure should be compared to NI

indications. If all indications do not agree within 5 percent,

Reactor Power should be stabilized and an OST-010 performed."

Application of this precaution would have identified the Power Range Nuclear

Instrumentation mismatch earlier in the startup. Since this need to compare

indicated power with other indications of power was not duplicated in the body

of the procedure, this precaution was not brought to the operators' attention.

Immediately prior to the power escalation, the on-shift crew was relieved with

the turbine latched and rolling. Precaution Step 4.15 of Procedure GP-005,

limits the time that the turbine can be operated below 520 rpm. Concerns with

violating this precaution were cited by at least one watchstander as providing

an impetus for relieving the watch and commencing the power escalation. The

desire to accomplish this expeditiously may have contributed to the less than

adequate pre-evolution preparation.

Finally, the team noted that poor communications contributed to the failure of

the watch section to diagnose the power mismatch. Although the reactor

engineer's E-mail memo, discussed previously, contained specific direction for

the operators to stop the power ascension if the 20 percent current equivalent

rod stop was achieved prior to the P-10 interlock, the memo was not routed

through the Operations Manager. A copy was provided to the Operations

Manager; however, he stated that he was not aware of its existence prior to

the power ascension. A second example of a communications failure was

evidenced when two operators stated that they had raised questions over the

accuracy of the indicated power range after power was stabilized at 20

percent. These concerns resulted from inconsistencies in turbine first stage

pressure and indicated neutron power were made prior to the questioning of the

net Mega Watts electric reading. However, these observations were not

communicated to the entire crew for resolution and were not reflected in the

operator logs.

The team concluded that sufficient information was available to control room

operators to permit diagnosis of a deviation in indicated power and actual

power prior to exceeding an actual power level of 20 percent. An analysis of

control room instrument traces and plant computer records by the team revealed

that several instruments indicated that the operators should have questioned

the Power Range Nuclear Instrumentation readings. Further, these indications

  • II13

were available to the operators prior to exceeding an actual core power level

of 20 percent. Specifically, loop delta Ts, turbine first stage pressure, and

one of the Regulatory Guide 1.97 wide range power level instruments, all

provided clear indication that actual power was greater than that indicated by

the Power Range Nuclear Instrumentations.

The team concluded that watchstander distractions during the power escalation

contributed to the failure to detect the Power Range Nuclear Instrumentation

miscalibration. These distractions were primarily the result of the

following: a focus by key watchstanders on preventing a reactor trip that

overrode maintaining adequate oversight; difficulties in controlling certain

plant parameters; and equipment malfunctions.

The team also concluded that the small magnitude of the Moderator Temperature

Coefficient during the startup increased the necessity for reactivity control

through frequent rod motion. Additionally, these power fluctuations added to

the difficulty in controlling steam generator water levels.

Contributing factors included distraction of watchstanders, an inadequate pre

evolution brief, watch relief with the plant in an other than stable

condition, and poor communications.

3.3.2 Operator Training

.In

1989, the licensee's plant Harris experienced a similar event in which the

Power Range Nuclear Instrumentations were discovered to be miscalibrated

during a reactor startup. Industry Document SOER-90-003 described this event

and corrective actions.

The training on this industry event, at another

facility owned by the same licensee, did not adequately prevent its recurrence

at Robinson. The lessons learned from this event were covered only once

during requalification training after the Harris event. It was not

incorporated into any of the requalification training given after the first

year. The training method did not adequately reflect the problems encountered

in the Harris event; for example, the simulator scenarios did not challenge

the operators with a Power Range Nuclear Instrument that was indicating low

during startup conditions. The scenario had the operating crew detecting the

inaccurate indication at 90 percent power by doing a procedurally required

calorimetric. This did not reinforce the concept of monitoring diverse

indications of power during a startup.

The initial license training program contains a lesson plan with an excellent

description of the Power Range Nuclear Instrumentation miscalibration event at

Harris. This was not used in requalification training. The only operator on

shift who had recently been licensed, received this training but could not

recall the details of it.

Several operators stated that the startup training did not adequately reflect

the actual plant startup. The crew members participated in about four hours

of simulator startup training. This startup contained no malfunctions. The

simulator feedwater controls and instrumentation respond with such precision

that the operators get little training on what is experienced in an actual

startup. There were no distractions which would have required crew

14

prioritization or coordinated oversight. Additionally. the startup training

did not mention the new low leakage core. This would have been helpful in

informing the operators of the expected response by the Nuclear

Instrumentations.

Another contributing factor identified from the operator training was the lack

of management involvement in the training. There was no Operations Department

interface to relay their expectations to the control room operators.

3.3.3 Discussion of the Bypass of Intermediate Range Instrument Nuclear

Instrumentation-36 High Flux Trip.

At 8:15 am on November 14, 1993, the level trip switch on intermediate range

instrument NI-36 was placed in the bypass position to defeat the intermediate

range high flux trip. This trip occurs at a nominal intermediate range

current equivalent to 25 percent reactor power. The trip is not considered in

the plant's safety analysis and is not required by technical specifications.

When the trip was bypassed, NI-36 was indicating approximately 7.6x10-5 amps

with the trip set at 1.3X10 4 amps. This action deviated from Startup

Procedure GP-005 which required that the trips be defeated using the

Intermediate Range "A" and "B" Logic Trip Defeat push-buttons on the gauge

board. This can only be accomplished when the P-10 interlock is satisfied;

i.e., 2 of 4 power range instruments indicated greater than 10 percent. When

questioned on the appropriateness of this action, the watchstander stated that

this evolution had been pre-briefed with the shift supervisor, that the P-10

interlock was satisfied prior to the action, and that the action was taken due

to the tolerances assigned to the trip setpoint. As described by the

watchstander and others, a trip on intermediate range high flux had occurred

during a previous startup with little warning.

From a review of plant computer printouts, the team noted that at the time the

NI-36 high flux trip was logged as defeated, the P-10 interlock was satisfied.

The team also noted th&t the intermediate range high flux trips were correctly

defeated in accordance

th Procedure GP-005 approximately 1 minute later at

8:16 a.m. Based on their review, the team concluded that though the action

was not in accordance with the startup procedure, the safety significance of

this deviation was minimal.

3.3.4 AIT Findings and Conclusions

Operators had sufficient indications to detect the difference between

power range indications and actual reactor power.

The crew's focus on trip prevention overrode maintaining adequate

oversight.

The operating crew did not trust their Intermediate Range Nuclear

Instrumentation indications.

0,

There was not a pre-evolution brief to adequately emphasize

precautions or expectations of the operating crew.

15

Start up training did not reflect the actual plant start up.

Training on the Harris event was not effective in preventing the

occurrence of a similar event at Robinson.

The potential consequences of this event were minimized since the

initial goal of the power ascension was to stop at about 30 percent.

The power ascension was stopped early with readings of the power range

nuclear instruments indicating about 20 percent, but documentation of

other readings at that time found the power to have been actually at

30.3 percent.

Startup Procedure GP-005 did not prevent reoccurrence of the Harris

event. Although a precaution to monitor diverse indications of power

during power ascension was added, this was not read or implemented by

the crew during this start up. There were no expected values for Mega

Watts electric, delta T, or turbine impulse pressure listed in the

procedure to flag problems at 10 percent and 20 percent power. This

lack of guidance was a significant contributor.

Management did not make their expectations clear as to control room

watchstander duties and responsibilities.

4.0

CORE NEUTRON FLUX ANOMALIES

4.1

Assessment of root cause and safety significance of the core neutron

flux anomalies with regard to fuel and technical specification limits.

Early in the core design turnover process from the fuel vendor to the

licensee, the licensee's Nuclear Fuel Services group noted some computer input

discrepancies (from the INCORE Code) which the fuel vendor then addressed.

After the core was delivered, the final approval was then given by the

licensee's Nuclear Fuel Services for the site to load the core and conduct

startup physics and power ascension tests.

Two in-core maps were taken at 30

percent power between November 14 and 16, 1993. The first map was number 698,

and the latter one was number 699.

An error in different computer core design data (using the PDQ Code) was

detected after the 30 percent power in-core flux maps had been performed. The

fuel vendor's PDQ computer input deck that was part of the in-core analysis

conducted on November 16-18, 1993, did not include two items:

ITEM 1.

The gadolinium rod overlays for the latest core reload batch

(This computed higher predicted individual assembly powers in the

gadolinium rods than if the gadolinium overlays had been used, and

consequently other rods assembly powers were predicted lower.)

ITEM 2.

The six misconstructed asymmetrical gadolinium fuel

assemblies (This item was, of course, not known at the time.)

16

A new computer in-core analysis was rerun the first week of December with the

PDQ computer input corrections.

The new computer input deck (with ITEM 1 fixed and presuming the core

was loaded as-designed with properly configured assemblies) was run by

the licensee's Nuclear Fuel Services for the number 698 and 699 maps

taken at 30 percent power. Results were calculated as follows:

-

The new computer data calculated the predicted relative assembly

power for the original expected design.

-

The in-core maps, numbers 698 and 699, showed the as-measured

condition of the core at 30 percent power and calculated the as

measured relative assembly power.

-

The differences were then computed on an assembly by assembly

basis and showed what should have been the results on November 16,

1993.

This would have been the information available to the site and the

licensee's Nuclear Fuel Services to decide if the as-measured core

contained any anomalies that were significant, and whether the

misconstructed assemblies would have been detected.

This analysis found that in-core map indications would have been present and,

if the original computer data had been correct, would have led engineering to

detect the misconstructed assemblies when the first maps were analyzed.

Another computer input deck (with ITEM 1 fixed and the core loaded as

built, with the six misconstructed assemblies) was run by the

licensee's Nuclear Fuel Services for the number 698 and 699 maps.

This calculated the actual November 16, 1993, F-delta H and showed

that the technical specification limit was exceeded by less than 0.5

percent.

-

The new computer data calculated the predicted relative assembly

power in the as-built core.

-

The in-core maps, numbers 698 and 699, showed the as-measured

condition of the core at 30 percent power and calculated the as

measured relative assembly power.

-

The differences were then computed on an assembly by assembly

basis and simulated what could have been the results on

November 16, 1993, if the core had been loaded correctly. This

allowed the in-core map to be analyzed for any other

discrepancies.

No other anomalies were observed in this analysis and discrepancies are not

expected to be seen after the core is reloaded with the misconstructed

assemblies in the proper locations.

4.1.1 AIT Findings and Conclusions

The.team reviewed the Cycle 16 analysis, that was run with the correct design

parameters, and found:

17

The F-delta H technical specification limit was exceeded by less than

0.5 percent on one in-core map and the other map did not show a

technical specification violation. This shows that the limit may have

been exceeded by a small amount.

The core radial tilt resulting from the misconstructed fuel assemblies

was observable once the corrections were made to the computer data.

The Cycle 16 fuel had operated well within the Departure from Nuclear

Boiling limits and no damage to the fuel should have occurred.

Reactor coolant chemistry data analysis also showed no fuel damage.

4.2

Assessment of the cause and extent of the fuel manufacturing errors at

the Siemens Power Corporation-Nuclear Division fuel manufacturing facility.

On November 18, 1993, during cycle-16 plant start-up, it was determined that a

manufacturing error had occurred and six misconstructed fuel assemblies had

been installed in the Robinson core. The fuel assemblies had been built 90

degrees out of the correct orientation because incorrect load map drawing

information had been entered into the manufacturing computer system. Two

subsequent Quality Control overchecks failed to detect the error.

Fuel assembly manufacturing was controlled by the Bundle Assembly Data Logger

computer system. The computer program compiled information associated with

the fuel assemblies and provided technicians with manufacturing control

instructions which indicated which rods to place in which position of the fuel

assembly and in what sequence to do so.

Fuel assembly information was loaded into the computer program by a Production

Control Clerk (clerk) who performed this function to assist the Production

Control Specialist (specialist) who typically performed the task. The clerk

used the specialist's identification and password to access the computer to

perform this task. The fuel vendor indicated that the common use of the

identification and password was not prohibited and that separate

identification was not set up specifically for the clerk because he performed

a variety of tasks. The process of entering the fuel assembly information

into the computer program was not specified by procedure, and the clerk had

only an informal document available for guidance. In addition, the clerk

performed the task of loading the fuel assembly information into the computer

program at a remote computer terminal, between other employees' work stations,

with little work space to accommodate the required documentation.

The computer program was configured so that a specific set of information

(header information) appeared at the top of the screen. The header

information included the fuel assembly (bundle) item (part) number and drawing

number, the load map item (part) number and drawing number, the manufacturing

order number, and the project title. When entering the information for fuel

assembly item number 140148, the clerk entered an incorrect load map drawing

18

number 308181 (the correct load map drawing number was 308180 for fuel

assembly item number 140148). When entering the information for fuel assembly

item number 140150 the clerk entered the incorrect load map drawing number

308180 (the correct load map drawing number was 308181 for fuel assembly item

number 140150).

The fuel vendor determined that the clerk had worked on fuel assemblies 140148

and 140150 during the same session at the computer program computer terminal

and that it appeared that the load maps and the attached insertion sequences

were swapped between the two packages.

The computer then provided a series of prompts to allow the clerk to enter the

location of the fuel rods within the fuel assembly. The documents used to

load in the fuel assembly information included the parts list (a reviewed and

approved design document), the load map drawing (a reviewed and approved

design document), and the insertion sequence (an informal document which

indicated the order in which the assembly table placed fuel rods into the fuel

assembly, a manufacturing document). The clerk defined a set of "find

numbers" used to identify rod types and then entered the insertion sequence

using the find numbers. This information was obtained from the load maps and

insertion sequences which were incorrectly specified for fuel assembly numbers

140148 and 140150. As a result, the computer program was loaded with design

information and manufacturing instructions which would place the fuel rods in

incorrect positions when the fuel assemblies were manufactured.

After entry of the fuel assembly information was completed, the computer

program produced a bundle proof map (the header information, a matrix of find

numbers representing the fuel assembly, and the find number definitions) for

each fuel assembly. The bundle proof maps for fuel assembly numbers 140148

and 140150 were verified by Quality Control Engineering by comparing the

matrix of find numbers and the find number definitions to the load map drawing

specified in the header information for each fuel assembly. However, the

Quality Control Engineering person did not verify that the load map drawing

number listed in the header information was correct (it was incorrect for fuel

assemblies 140148 and 140150).

The team reviewed the procedure governing the

quality control activities, "Fuel Bundle Map Verification," Revision 0, dated

August 3, 1990, and noted that it did not clearly specify the basis for the

checks but only specified that the checks be made against a "hard copy."

Following completion of the-manufacturing process, the computer program

provided an as-built bundle map of each fuel assembly which listed the part

number (or no load) which was located in each coordinate of the fuel assembly.

A Quality Control Inspection Technician reviewed the as-built bundle maps for

fuel assemblies 140148 and 140150 against the load map drawings which were

specified in the computer program header information; however, the technician

did not verify that the load map drawing number listed in the header

information was correct (it was incorrect for fuel assemblies 140148 and

140150).

As a result of the error made in the Robinson fuel assemblies, the fuel vendor

reviewed the as-built lists and records for ROB-13 (Robinson's Cycle 16

refueling) and the remaining assemblies in the Robinson core and approximately

19

1000 additional fuel assemblies the fuel vendor had previously manufactured.

The fuel vendor determined that no other misconfigurations existed. The team

reviewed the documentation of the ROB-13 review and determined that this

method had credibility and that the extent of the problem appeared to apply

only to the six Robinson fuel assemblies in question.

4.2.1 AIT Findings and Conclusions

The team concluded that the control of design information (i.e., the

required location of 'the fuel rods within the fuel assemblies) as it

was translated into the computer system was inadequate; that the level

of responsibility, accountability, supervision, and review associated

with this critical task was inadequate; that the performance of the

quality control overchecks of the computer program information was

inadequate; and that the procedures used to govern the activities were

inadequate.

On November 22, the fuel vendor stated that they had verified 100

percent of the current core load. They compared the as-built

documentation to the core design documents and stated that no other

error was made. the licensee independently verified this

documentation. The team verified that this method had credibility.

The failure of Quality Control to compare as-built information to

design documents was the basic flaw that resulted in the misassembly

of the fuel.

4.3

Assessment of the extent and effectiveness of fuel assembly

verification at the Siemens Power Corporation-Nuclear Division.

The team determined that the fuel vendor used several methods to maintain

accountability of the fuel assemblies and their subcomponents. The methods

included computer-readable bar codes, man-readable serial numbers, hard copy

travellers, and Quality Control overchecks. At the initial stage of fuel rod

manufacture, a serial number was engraved on the lower end cap in the form of

a computer-readable bar code and man-readable number. This serial number was

entered into the Rod Serialization System computer system which tracked the

fuel rod through the assembly process, from manufacture of the lower end caps

through storage of the completed fuel rods.

The lower end cap was welded to the tube of cladding and the lower end cap

serial number was scanned to associate the lower end cap serial number with

the manufacturing order number, the fuel rod group number, the fuel rod part

number, and the clad part number. The fuel rod was further assembled by

loading the fuel pellets, the load spring, out-gassing the fuel rod and

welding the upper end cap to the fuel rod. Following assembly, a leak check,

a uniformity check, a through rod x-ray, and a final inspection for color,

straightness, length, and weld quality was performed. During each step in the

process the lower end cap serial number was computer scanned at the work

station to maintain accountability for completion of the particular portion of

the fuel rod manufacture. At the end of the fabrication process, the fuel

rods were placed in storage bins near the fuel assembly manufacturing area.

20

The Bundle Assembly Data Logger (the computer program) computer system then

tracked the fabrication of the fuel assembly from removal of the fuels rods

from storage through completion of the assembly process.

Fuel assembly manufacturing occurred when a manufacturing order created a

demand and the Quality Control checks had been performed of the fuel assembly

information in the computer program, which had been entered by the clerk, and

Quality Control Engineering had electronically enabled the computer program to

allow the manufacture of a fuel assembly.

Fuel rods were moved from storage onto the order picker by an elevator. The

order picker had 12 trays divisible by 3 to allow for a total of 36 types of

rods to be on the machine at a given time. The computer system was tied to

the order picker which provided a signal light to indicate from which section

rods were to be removed in accordance with the insertion sequence. As the

rods were removed from the order picker, the lower end caps were scanned into

the computer program and the order picker decremented the count of the rods in

the. applicable section.

The fuel rods were moved from the order picker to the loading section of the

insertion table. The fuel rods were scanned as they were placed on the

downward slope of the insertion table in the order of the insertion sequence.

The fuel rods were picked up from the slope of the insertion table by a set of

notched wheels, scanned while in the wheel to verify the insertion sequence,

.and

dumped into a feed trough. The assembler then moved to the proper "x-y"

coordinates, based on the insertion sequence, and the fuel rods were pushed

into the specified "x-y" coordinates of the fuel assembly located on the

assembler table where the fuel rods were then fixed into place.

After completion of the manufacture of the fuel assembly, the computer program

printed out the as-built bundle map, a sequential list of the fuel assembly

"x-y" coordinates and the part numbers and serial numbers of the items which

filled the coordinates (such as fuel rods).

The Quality Control Inspection

Technician compared the as-built bundle map to the load map specified in the

computer program header data to verify that the assembly had been correctly

manufactured.

4.3.1 AIT Findings and Conclusions

The team concluded that the fuel vendor appeared to have an effective program

for assembly verification in most areas. However, the team did conclude that

the fuel vendor performance in the area of entering design information (the

load map fuel assembly pattern) into the computer program computer system and

the subsequent Quality Control overchecks of this process were less than

adequate (See paragraph 4.2 of this report).

In addition, the fuel vendor

indicated that the level of complexity of the fuel assemblies being

manufactured had increased since the manufacturing system had been implemented

in 1984. The team determined that the manufacturing machines and computer

systems involved did not appear to have been worked beyond capacity; however,

.there

did appear to have been an increasing level of complexity of the

information required to be manipulated and verified by the personnel involved

in the manufacturing process.

II

21

4.4

Assessment of the extent and effectiveness of fuel verification at the

site.

Fuel verification at the site consisted of a visual inspection upon receipt.

This included a visual inspection of the assembly externals and the assembly

serial number. This type of inspection is similar to the industry standard.

4.4.1

AIT Conclusion

No method is reasonably available at the site for more detailed verification.

4.5

Assessment of the Siemens Power Corporation-Nuclear Division analysis

of the core neutron flux anomalies.

The team reviewed and evaluated the fuel vendor's performance and response to

the observed core flux anomalies at Robinson during power ascension testing.

The fuel vendor had no role in the Robinson miscalibration of the excore

nuclear power range instrumentation. Their only involvement was to provide

confirming data for the re-calibration procedure, after the incident,

including reasonable weighing factors for edge bundles adjacent to the excore

Nuclear Instruments.

The team assessed the fuel vendor's analysis of the Robinson core power tilt

.and

bundle power anomalies. These were observed at the 30 percent power level

testing, after processing of the in-core flux map measurements, with the

licensee version of the Westinghouse INCORE program using the fuel vendor

provided input files. An interactive licensee and fuel vendor analysis of the

30 percent power measurement results, including rerunning the in-core map, led

to suspension of power ascension until the anomalies could be resolved. The

fuel vendor performed an independent analysis of the in-core measurements

(with their INPAX-W program), confirming that the Cycle-16 core was not

performing as designed. The fuel vendor, after an extensive Quality Assurance

record review, then reported their discovery that six fuel bundles had been

misbuilt, which had resulted in a reload core misconfiguration. The fuel

vendor provided revised INCORE input decks for the as-built condition,

allowing the core power distribution to be evaluated against the design

peaking factors. However, the fuel vendor later discovered an INCORE input

error for all fresh, burnable poison bundle types, after noting an in-core

flux anomaly in other than the misbuilt bundles.

4.5.1

AIT Findings and Conclusions.

The team determined that the fuel vendor's Pressurized Water Reactor

Nuclear Engineering (NE) support, after the observed INCORE anomaly

indication, was appropriate and adequate in confirming the core mis

loading. However, the initial licensee discovery and subsequent fuel

vendor correction of earlier INCORE input file errors should have

triggered a complete deck review by the fuel vendor and could have

alerted both the licensee and the fuel vendor management to potential

problems in the core design process.

22

The team determined that deficiencies in the fuel vendor's analysis

and verification procedures caused the input errors in the in-core

flux mapping computer program (INCORE).

Also,.the fuel vendor's

regeneration of INCORE computer input for the as-built core should

have included a complete deck review, which might have discovered the

computer input errors earlier. The fuel vendor's response after their

INCORE computer input error discovery was appropriate and supplied the

proper level of support.

4.6

Assessment of the licensee's oversight of Siemens Power Corporation

Nuclear Division's fuel analysis and Quality Assurance programs.

The team reviewed selected areas from the fuel vendor reload design analyses

from Robinson cycles-14, -15, and -16 core reloads. The fuel vendor's core

reload design activities began approximately 18 months prior to fuel delivery

upon receipt of the Tentative Scheduled Delivery Date - notification from the

licensee. This includes the projected end-of-cycle performance of the current

cycle, and the estimated energy requirements for the target cycle. Based on

this notification and discussions with the licensee, the fuel vendor's Nuclear

Engineering provided the licensee's Nuclear Fuel Services with a preliminary

fuel bundle and core design. This tentative design, including the number of

bundles and rod types, was also provided to the fuel vendor's Product

Mechanical Engineering for mechanical design and material requirements

development.

Approximately 12 months prior to fuel delivery, the licensee's Nuclear Fuel

Services provided the Final Scheduled Delivery Date - notification to the fuel

vendor, along with the final cycle energy requirement and an upper and lower

energy generation window for the current end-of-cycle. Based on this data,

the fuel vendor provided the final fuel bundle and core design to the licensee

and delivered a Characteristic Specifications document to their Product

Mechanical Engineering for the development of the detailed parts list. The

licensee reviewed the design and provided approval.

At this point, the reload

core design was considered final; however, the fuel vendor documentation had

not undergone Quality Assurance review and approval.

For the Robinson cycle-16 core reload, the original "final" design utilized a

48-bundle split-enrichment batch to achieve a 430 equivalent full power day

operating cycle. At the licensee's request, a further design change was

developed by the licensee and the fuel vendor (November 1992) to allow the 48

bundle reload batch to be reduced to 44 bundles. This was achieved by going

to a low leakage loading core and utilizing a single enrichment bundle design

with more burnable poison fuel types. At this time, the effect of the low

leakage loading pattern to reduce excore detector response was noted by the

licensee.

Based on the changed design, the fuel vendor's Nuclear Engineering revised the

Characteristic Specifications documentation and provided updated load map data

to Product Mechanical Engineering for development of the final parts list and

23

bundle ID core maps. Following their standard Quality Assurance procedure,

the fuel vendor then began the preparation and review process for their formal

documentation packages and provided them to the licensee during the four

months prior to fuel delivery.

The Robinson cycle-16 Reload Batch Design Report, signifying the fuel vendor

Quality Assurance review and approval of the reload design, was issued to the

licensee in April 1993. The Safety Analysis Report was issued in August 1993

and the Startup and Operations Report was issued in September 1993.

The

INCORE monitoring input file (deck) was officially transmitted by letter with

a diskette in October 1993. Several corrections were noted by the licensee

and the fuel vendor provided revisions to the INCORE input file between the

end-of-cycle 15 shutdown and before Cycle 16 startup.

The team's assessment of the licensee activities are as follows:

There was less than adequate licensee oversight of the fuel vendor

cycle-16 core reload design implementation and verification activities

and of the quality assurance procedures concerning the calculation

notebooks.

The licensee conducted independent calculation reviews of the fuel

vendor reload design parameters at their Raleigh offices and primarily

judged design adequacy based on agreement between the two design

models.

The licensee did not conduct onsite audits of the fuel vendor Nuclear

Engineering and Product Mechanical Engineering design activities and

interfaces for the cycle-16 core reload.

The last known Robinson audit that covered neutronic areas was during

the cycle-12 reload design period.

The licensee conducted in-house reviews of the fuel vendor generated

INCORE computer input file; first by processing the file through a

data curve plotting routine, and then by making test runs using

predicted in-core flux measurement data. For the cycle-16 deck, this

process revealed incomplete data and several errors in the initial

fuel vendor transmittal.

Corrective actions did not include a broader

review of the total reload design process.

4.6.1 AIT Findings and Conclusions

The team determined that the licensee's oversight process was inadequate

because the licensee's Nuclear Fuel Section:

failed to review or observe any of the fuel vendor's fuel bundle

assembly manufacturing activities (due to fabrication schedule changes

that occurred during Nuclear Fuel Service's surveillance activities);

and

  • I

24

failed to compare the fuel vendor's fuel bundle assembly records to

the characteristic specifications for Robinson's cycle-16 fuel load.

The licensee's Independent Assessment Team investigation of the

Robinson cycle-16 fuel and core reloading problems also concluded that

its oversight of the fuel vendor's fuel manufacturing activities was

less that adequate.

5.0

BROKEN FUEL INSPECTION TOOL DURING REFUELING

5.1

Determination of the Root Cause of the Broken Fuel Inspection Tool

Event.

5.1.1

From the inspection on-site.

On October 11, 1993, licensee personnel discovered that the control rod for

fuel assembly U-24 would not completely insert into the assembly. The control

rod stopped with approximately two feet of full insertion remaining. An

inspection of selected fuel assemblies in the spent fuel pool was in progress

by the licensee's fuel vendor, Siemens Power Corporation, to measure fuel

assembly and fuel rod lengths. These measurements had routinely been made at

other nuclear facilities using similar tools. Further investigation and

conversation between the licensee and the fuel vendor revealed that loose

parts from a damaged fuel inspection tool had been dropped into a control rod

guide tube of assembly U-24.

The team reviewed the fuel vendor site activity log for the conduct of these

measurements and also reviewed the licensee's log of these activities to

determine and verify the sequence of events. Also the vendor's incident

review board report and licensee's self assessment report were reviewed. The

team discussed these activities with licensee oversight personnel and the fuel

vendor team leader who was responsible for the performance of the fuel

measurements. Both the licensee's and the vendor's log books were very brief

and did not provide any detailed information. Neither party had developed any

standards for these logs.

Special Procedure SP-1258, "Fuel Assembly Inspection and Repair," provided

guidance for the conduct of these measurements. This procedure was reviewed

by the team. As part of the procedure guidance for the fuel inspection, the

fuel assembly upper tie plate was removed and a reference plate installed.

This reference plate was held in position by the use of three expandable

anchors which inserted into three guide tube locations. The 'anchors were hand

tightened to secure the plate into position. Although the tool had been used

before, new anchors had recently been fabricated and installed for this

inspection.

From a review of the logs and discussions with personnel, the team developed

the following sequence of events. The fuel vendor personnel measured assembly

S-15H on October 6, 1993.

Following this inspection, the tool (including the

reference plate) was removed from the assembly and placed in a temporary three

foot storage area on the side of the spent fuel pool.

On October 9 at

approximately 9:00 pm, the tool was utilized again on assembly U-24. The fuel

vendor personnel.noted that only two of the expandable anchors engaged and no

25

resistance was noticed when tightening the third anchor. This information was

not included in the fuel vendor site activity log or communicated to licensee

personnel.

The fuel vendor personnel decided the tool could still function in

this condition and continued using the tool.

Following the measurements on

assembly U-24, the tool was used again on assembly U-23.

Fuel assembly

measurements were completed at 7:20 am on October 10, 1993. On October 11,

1993, at approximately 2:00 am, the tool was removed from the spent fuel pool

and the fuel vendor personnel noted damage to the reference plate and missing

parts from the expandable anchor. Specifically, the missing parts included an

expander nut, expander tube, two roll pins, and a portion of the clamp shaft

(see figure X).

Damage to the clamp shaft was also observed which appeared to

be slightly bent. This information was also not recorded in the fuel vendor

site activity log nor communicated to licensee personnel.

Later that same day

at approximately 9:00 pm, licensee personnel experienced difficulty while

inserting the control rod for assembly U-24 at which time the fuel vendor

personnel reported the missing parts from the tool to licensee personnel.

The

licensee performed a visual examination of the control rod and found the

expander tube lodged on the tip of a control rod finger. The licensee

considers the other missing parts to likewise be in the same guide tube where

the expander tube was found based on the construction of the anchor which

would not provide any support for the tube or roll pins once the expander nut

was removed. Licensee personnel examined the guide tube with a plug gage and

found blockage evident near the dash pot region of the guide tube. This also

indicated that the expander nut was still in the guide tube.

Due to the damage noted on the clamp shaft, the fuel vendor believes that the

tool was damaged by an impact from another tool while placed in temporary

storage in the spent fuel pool for the approximate four days between tool

usage. The small, three foot area allocated was congested with many tools

(approximately 13).

Several other tools were moved to this same storage area

during the time frame involved. The licensee's investigation did not reach a

conclusion on how the tool was damaged. Due to the small amount of force

which would be required to overtighten and break the anchor, the team

concluded that the tool could have been damaged either by an impact while in

the storage area or from overtightening.

The team discussed with the vendor the delay in vendor personnel reporting the

missing tool parts to the licensee. Both the licensee and the vendor incident

review board determined that this omission was not a deliberate act but rather

a significant error in judgement by vendor personnel.

Past experience of the

vendor personnel indicated that at other facilities where loose parts were

dropped in the spent fuel pools, licensee personnel had been informed shortly

afterwards. The vendor team had considered that the lost material could be

resolved at a later time and the missing parts were thought to be on the

bottom of the pool and not in a fuel assembly. Although the vendor did not

have a procedure on foreign material exclusion, vendor personnel were trained

by the licensee on the requirements of Procedure PLP-047, Foreign Material

Exclusion Area Program. Access to the foreign material exclusion area was

strictly controlled by licensee personnel and logs were required to document

entering the area or bringing in material.

The vendor was further requested

by the licensee to remove debris from several fuel assemblies prior to fuel

load in the core indicating the sensitivity of this subject. The team

26

concluded that the fuel vendor personnel should have been aware of the

importance that a loose part in the spent fuel pool would have. The

investigative reports also mentioned the poor fitness.for duty of personnel

during this time frame due to illness and being physically tired following

several 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shifts of work. This poor physical condition could have

contributed to the poor judgement of contractor personnel who failed to

promptly notify licensee personnel of the missing parts/damaged tool.

Due to

these facts, and discussions with the vendor team leader, the team agreed with

the vendor's determination that the failure to promptly report the missing

parts was not a deliberate act.

The licensee performed an engineering evaluation for the continued use of the

fuel assembly with the loose parts inside the guide tube. This evaluation

concluded that this action would be acceptable based upon chemical, thermal,

and mechanical compatibility of the loose parts with the rest of the assembly.

Therefore, licensee personnel installed a thimble plug over the guide tubes

for this assembly. However, as a result of this action, eight fuel assemblies

had to be repositioned in the core loading to substitute a rodded fuel

assembly for the plugged assembly.

5.1.2 Determination of the root cause of the broken fuel inspection tool

event from the fuel vendor Inspection.

Siemens Power Corporation-Nuclear Division Fuel Services department conducted

.fuel

examinations in the spent fuel pool during Robinson's cycle-16 refueling

outage. As part of its fuel examinations, the fuel vendor's site team

measured the length of the assembly and the fuel rods of three fuel assemblies

that were examined in the following order: S-15H, U-24, and U-23. The length

measurements require removal of the upper tie plate from the fuel assembly

followed by the attachment of a reference length plate. The reference length

plate is designed to be attached to the fuel assembly at three guide tube

locations using a remotely activated expandable anchor inserted in each guide

tube. The expandable anchor consist of a clamp shaft with an expander nut

(collet) on each end of a slotted expander tube and two roll pins (one is a

backup) inserted through the clamp shaft below the bottom expander nut. The

expander nuts are drawn into a slotted expander tube by remotely turning the

clamp shaft.

The length measurements of fuel assembly S-15H were completed without incident

on October 6, 1993. On October 10, 1993, during the attachment of the

reference length plate on fuel assembly U-24, the expandable anchor inserted

in guide tube location E-11 failed to tighten within the guide tube. Siemens

Power Corporation-Nuclear Division site team determined that the length

measurements and examinations of fuel assembly U-24 could be completed without

utilizing the malfunctioning expandable anchor. The length measurements of

fuel assembly U-23 were also completed on October 10, 1993, using only two

functioning expandable anchors. On October 11, 1993, as part of its general

pack-up activity, the fuel vendor site team removed the reference length plate

0II

9

27

from the spent fuel pool for the first time since the fuel assembly length

measurement examinations began on October 5, 1993. Once the reference length

plate was removed from the spent fuel pool, the fuel vendor site team

discovered that the malfunctioning expandable anchor clamp shaft was broken,

bent, and missing the following parts:

lower expander nut

expander tube

two roll pins

a portion of the clamp shaft

Upon discovery of the broken expander anchor at Robinson, Siemens Power

Corporation-Nuclear Division Fuel Services Engineering staff destructively

tested an identical expandable anchor and found that the clamp shaft failed in

the region of the uppermost 0.1574-cm (0.062-inch) diameter roll pin with an

applied torsional load of approximately 4.324-N (35-lbin or 0.972-lbf).

In Siemens Power Corporation-Nuclear Division Incident Review Board report

EMF-93-195(P), "H. B. Robinson Fuel Examination, September 21-October 14,

1993, Investigation of Failure to Report Loose Parts," issued on November 5,

1993, the fuel vendor stated, in part, that the issues summarized below were

identified by the Incident Review Board as the root cause/causal factors for

the loose parts event at Robinson:

The applicable Standard Operating Procedure, Fuel Performance, EMF

P71,129, "Fuel Rod and Assembly Length," Revision 0, March 27, 1992,

did not reference the reference length plate Drawing No. ANF-306,200,

"Rod Length Measuring Tool," Revision 0, September 4, 1987.

  • .

The fuel vendor's Fuel Services equipment technicians prepared the

reference length plate tool and shipped it to Robinson without

referring to the reference length plate drawing to verify its

configuration. Siemens Power Corporation-Nuclear Division failure to

verify the tool's configuration resulted in placing a tool in service

that was in less than adequate condition because the reference length

plate was designed with four guide pins and it was shipped to Robinson

with only three. The guide pins were designed to aid in orienting the

tool to the fuel assembly by inserting them into the guide tubes. In

addition to its orienting function, each guide pin also served to

protect the expandable anchors.

The fuel vendor concluded that the expandable anchor design was poor

and found no documented engineering review of the expandable anchor

design. According to the fuel vendor,,the design of the expandable

anchor is inconsistent with its design philosophy which dictates that

tool failure will not result in loose parts.

Siemens Power Corporation-Nuclear Division Incident Review Board

concluded that the reference length plate and expandable anchor were

most probably struck from the side and that the impact was likely from

another tool or hardware in the spent fuel pool.

The fuel vendor

added that the difficult handling of heavy tools, crowded conditions,

28

and inadequate preparation of the work area contributed to the

potential for such an impact. Additionally, the fuel vendor noted

that the absence of the forth guide pin reduced the physical

protection of the expandable anchor from external damage.

On November 30, 1993, the NRC's team at the fuel vendor's facility inspected

the reference length plate used at Robinson by the fuel vendor's site team.

The broken expandable anchor clamp shaft and upper expander nut were found in

their original as-built location on the reference length plate.

I

The fuel vendor agreed to perform additional examinations of the fracture

surfaces of the broken clamp shaft and compare its appearance to the fracture

surfaces of the expandable anchor clamp shaft from the destructively tested

expandable anchor. The additional examinations were performed on the two

clamp shafts using both low magnification micrographs taken with an optical

stereo-microscope and scanning electron micrograph mosaics of the fracture

surfaces.

From the results of these examinations, the team determined that the root

cause of the broken expandable anchor was a ductile overload of the clamp

shaft at the upper roll pin location that was induced through multiple

incremental overtorquing events. Siemens Power Corporation-Nuclear Division

analysis of the fracture surfaces and the results of these examinations

(documented in DTP:93:033, "Analysis of Fuel Services Component Failure,"

dated December 3, 1993) reached the same conclusion. The team also determined

-that the location where the expandable anchor overtorquing events occurred

(including the event that resulted in the 2* bend of the clamp shaft) is

indeterminate in that these events may have occurred during functional testing

of the reference length plate in the fuel vendor's mock-up pool, prior to its

shipment to Robinson, or during the fuel assembly examinations performed at

Robinson.

The team also determined that the fuel vendor's original root cause analysis

of the failed expandable anchor (documented in Incident Review Board report

EMF-93-195(P), "H. B. Robinson Fuel Examination, September 21-October 14,

1993, Investigation of Failure to Report Loose Parts," issued on November 5,

1993) was less than adequate because it did not determine the mechanical

failure mechanism of the broken clamp shaft.

5.1.3 AIT Findings and Conclusions

During fuel preparation for core load, loose parts had been found in a fuel

assembly as a result of a fuel inspection reference tool breaking. The fuel

vendor had been conducting fuel inspections in the Robinson spent fuel pit.

The root cause of the broken fuel inspection tool was attributed to the fuel

vendor design control problems and inadequate licensee oversight. The current

fuel vendor design control system had been set up in 1988 with no requirement

to use this methodology on items constructed after this date but built to an

.earlier

design. This particular design was completed in 1987 and the tool

constructed in 1992 and refitted in 1993.

29

The licensee's analysis of the small, unrecovered parts found that they were

confined to the fuel assembly guide tube and presented no future threat to

fuel integrity. The team agreed with this finding.

5.2

Effectiveness of Licensee Oversight of Contractor Fuel Handling

Activities

The team reviewed the involvement of licensee personnel during the fuel

measurements performed by the fuel vendor. This item was discussed with the

licensee and contractor personnel involved. Also the team reviewed the

licensee's assessment report..

According to licensee plant personnel, oversight of this activity included 24

hour coverage using 2 12-hour shift rotations. Licensee personnel were

present on the fuel handling floor during the fuel assembly inspections. Only

verbal guidance was provided to licensee personnel on their responsibilities

for oversight functions which consisted of assuring that vendor personnel

adhered to the licensee's procedures.

The team discussed this coverage with licensee personnel and was informed that

in some cases, concurrent activities occurred in the pool. This interfered

with direct oversight of the vendor activities. This occurred during the tool

removal, when licensee personnel were concurrently inspecting fuel assemblies

.for

debris. Licensee involvement in observing the video display for the

debris inspection prevented the direct oversight of contractor personnel when

the tool was removed.

The licensee's independent assessment report of this event concluded that

licensee personnel were not always present during the fuel measurements. This

contributed to the poor communication between the licensee and the vendor.

The team could not determine from the logs how long licensee personnel were

actually present for the fuel inspections.

Contractor activities for this fuel inspection were controlled by licensee

Procedure SP-1258. This procedure included attachments with the vendor's

procedure for the ultrasonic inspection, repair, and examination of fuel

assemblies (EMF-1576). The completed procedure was reviewed by the team as

well as the licensee's safety evaluation package of the procedure. The team

noted that the attached vendor procedure contained references to detailed

vendor procedures for the performance of the fuel rod and assembly length

measurement (EMF-P71,129) and for the upper tie plate removal/reinstallation

(ANF-P71,032). These two procedures were utilized by the vendor and involved

partial disassembly of the fuel assemblies for the inspections including tie

plate removal and the removal of fuel rods from the assembly. The team noted

that these quality activities were not encompassed by the licensee's safety

review of Procedure SP-1258.

The licensee provided training for the contract personnel on the implementing

procedure and requirements of Procedure PLP-037. Procedure SP-1258, section

O6.2,

contained a specific precaution on the requirements for foreign material

exclusion areas. The training consisted of handing out the procedures and

allowing contractor personnel to "self study" the handouts. The contractor

30

personnel acknowledged by signature the accomplishment of this training. The

licensee's assessment report concluded that the contractor indoctrination for

foreign material exclusion requirements was not effective.

The licensee's self-assessment report also identified that planning and

coordination for this activity was inadequate based on insufficient space

availability and availability of support services. This report also stated

  • that the responsibilities of licensee personnel who provided the oversight

function were not clearly defined.

The team noted from log book entries that both contractor and licensee

personnel were physically tired and in some cases ill.

This condition was not

noted in subsequent licensee investigations.

5.2.1

AIT Findings and Conclusions

The team concluded that the licensee oversight of contractor activities was

considered to be less than adequate; this was verified by interviews with

personnel and review of logs. The contributing causes were:

Poor planning and coordination of fuel inspection.

Failure to identify and adjust staffing of personnel when conditions

changed.

Lack of clearly defined responsibilities.

Poor safety review of vendor procedures for fuel inspection.

A review of the licensee's assessment report revealed their causes of the

event to be:

the poor planning and coordination of the fuel inspection

activities, lack of licensee management to identify and adjust staffing of

personnel when degradation of physical conditions was indicated, lack of

clearly defined responsibilities for licensee personnel overseeing this

activity, and a poor safety review of procedures utilized by the contractor in

performing these inspections.

5.3

Assess the adequacy of Siemens Power Corporation-Nuclear Division

Quality Assurance program for the manufacture of special fuel tools.

The reference length plate used at Robinson was designed in September 1987 and

has been used several times at Robinson and Tihange in Belgium (both plants

have 15 x 15 Pressurized Water Reactor fuel assemblies).

However, the

reference length plate design depicted on Drawing No. ANF-306,200, Revision 0,

had not been reviewed in accordance with the fuel vendor's design review and

design control measures established by the Quality Assurance program in 1988.

Siemens Power Corporation-Nuclear Division failure to evaluate the reference

length plate design in accordance with its Quality Assurance program is

considered by the team to be a significant contributing factor in the loose

parts event at Robinson.

In November 1990, Siemens Power Corporation-Nuclear Division Fuel Services

Engineering apparently recognized the poor design of the expandable anchor

that failed at Robinson. Drawing No. ANF-306,200, Revision 1, approved on

31

November 14, 1990, revised the expandable anchor design by (a) increasing the

diameter of the clamp shaft, (b) threading the end of the clamp shaft and

providing a threaded locking sleeve to retain the lower expander nut, and

(c) inserting a roll pin through the threaded locking sleeve and shaft to

ensure the locking sleeve would not loosen and back-off. Implementation of

these design changes would have prevented the loose parts event at Robinson.

However, the revised expandable anchor design was not manufactured or ever

utilized by the fuel vendor. Siemens Power Corporation-Nuclear Division's

failure to incorporate the enhanced expandable anchor design in the reference

length plate was a missed opportunity that contributed to the loose parts

event at Robinson.

Moreover, during its preparation of the reference length plate for shipment to

Robinson, the fuel vendor missed another opportunity to prevent the loose

parts event at Robinson. In September 1993, when the Fuel Services personnel

retrieved the reference length plate from storage in preparation for its

shipment to Robinson, it was discovered that one of the expandable anchors had

missing parts (the lower expander nut, expander tube, and the roll pins).

The

fuel vendor responded to the discovery of missing parts by fabricating three

new expandable anchors to the old, 1987 design. The fuel vendor failed to (a)

determine what had happened to the missing parts (i.e., were the parts lost

during the reference length plate's last usage, which was at Robinson during

its cycle-15 refueling outage, and if so, can the missing parts be located),

(b)

fabricate the replacement expandable anchors in accordance with the

revised 1990 design, and (c) perform an engineering evaluation of the newly

fabricated expandable anchors' design in accordance with the requirements of

the Quality Assurance program.

Subsequent to the team's identification of Siemens Power Corporation-Nuclear

Division's less than adequate actions regarding the missing parts, the

licensee at Robinson investigated the potential that the missing parts may

have entered Robinson's spent fuel pool or core during Robinson's cycle-15

refueling outage. Although it was not possible to establish with certainty

what happened to the missing parts, the licensee, on the basis of all

available information, determined that the missing parts were not located in

the Robinson spent fuel pool or core. The team reviewed the licensee's

evaluation and accepted its conclusion.

5.3.1 AIT Findings and Conclusions

From its review of Siemens Power Corporation-Nuclear Division's Quality

Assurance program, the team determined that for those fuel tools developed

since the implementation of the Quality Assurance program, the Quality

Assurance program appeared to be adequate. Siemens Power Corporation-Nuclear

Division's Quality Assurance program for the manufacture of special fuel tools

began in 1988 when the Fuel Services department first implemented Siemens

Power Corporation-Nuclear Division's Quality Assurance Manual EMF-1.

However, for those fuel handling tools that were developed by the Fuel

.Services

department before the implementation of Siemens Power Corporation

Nuclear Division's Quality Assurance program, Siemens Power Corporation-

32

Nuclear Division efforts to incorporate those tools into the Quality Assurance

program's design review and design control measures appear to be less than

adequate; as demonstrated by the reference length plate (Drawing No. ANF

306,200, "Rod Length Measuring Tool," Revision 0, September 4, 1987),

described above.

5.4

Assessment of the effectiveness of Siemens Power Corporation-Nuclear

Division's program for notifying licensees of known deficiencies in either

hardware or services provided.

The team reviewed Siemens Power Corporation-Nuclear Division's program for

review and notification to customers of identified deficiencies in hardware or

services, with particularly interest in the three deficiencies identified

during the Robinson event. The identified deficiencies were, (a) the presence

of loose parts in the fuel pool, (b) the incorrect manufacturing of six fuel

assemblies, and (c) the potential error in the generation of transport

correction factors used in the generation of the INCORE code.

Siemens Power Corporation-Nuclear Division's program is controlled by Policy

Guide 10.2, "Nuclear Safety Hazards Reporting," dated December 17, 1991.

Policy Guide 10.2 was previously reviewed during a February 1992 NRC

inspection at Siemens Power Corporation-Nuclear Division (see Inspection

Report 99900081/92-01). During the 1992 inspection, the team found the Policy

OGuide contained all necessary requirements of 10 CFR Part 21.

However, the

1992 inspection did identify an area of concern regarding the language

relating to who has responsibility for performing evaluations. This concern

was again raised to Siemens Power Corporation-Nuclear Division's management

during this inspection.

As previously discussed, the fuel vendor Fuel Services personnel failed to

report the presence of loose parts in the spent fuel pool to Robinson's staff

in a timely manner. The loose parts resulted from a failure of the reference

length plate expandable anchor. The licensee was not notified of the failure

until Robinson personnel were unsuccessful in loading a control rod into fuel

assembly U-24, approximately 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> after the fuel vendor site team first

identified the parts as missing. The fuel vendor convened an Incident Review

Board to investigate the circumstances surrounding the event and to determine

10 CFR Part 21 applicability. Incident Review Board report EMF-93-195(P),

"Incident Review Board Report, H. B. Robinson Fuel Examination, September 21

October 14, 1993, Investigation of Failure to Report Loose Parts," concluded

that there were no 10 CFR Part 21 implications from this event. The Incident

Review Board report based its conclusion on justifying the use of assembly

U-24 using a thimble plug device and moving its location in the core. The

team questioned the adequacy of this conclusion in light of potential generic

considerations regarding the use of the fuel tool at other facilities and the

potential for loose parts escaping the guide tube and damaging other

assemblies in the core. The fuel vendor provided the team with engineering

evaluation, "H. B. Robinson - Project Variance Evaluation of a Piece of a Tool

End in a Guide Tube of Assembly U-24," which was provided to the licensee in

an October 13, 1993, letter (RAC:93:165). The engineering evaluation provided

sufficient evidence that the loose parts in assembly U-24's guide tube (E-11)

33

could not escape from the tube. The fuel vendor also informed the team that

the tool was only used at Robinson and one foreign plant (Tihange in Belgium).

Since Robinson is the only U.S. commercial facility that has used the tool,

and they were notified approximately 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> after the fuel vendor site team

identified the missing parts, further notification by the fuel vendor was

unnecessary.

The problem with the incorrect manufacturing of six fuel assemblies was

identified by the licensee during power distribution mapping at Robinson at

approximately 30 percent power on November 18, 1993. The fuel vendor was

notified of the power distribution anomalies and convened a Hazards Review

Board the same day. The board concluded that the manufacturing error

constituted a defect under 10 CFR Part 21 which could potentially pose a

significant safety hazard and recommended that the condition be reported to

the NRC. The fuel vendor further recommended that the licensee make the

initial notification to the NRC. The licensee fulfilled the notification

requirement later on November 18, 1993. Both Siemens Power Corporation

Nuclear Division and the licensee's actions regarding 10 CFR Part 21 were

appropriate and in accordance with regulatory requirements.

The team further examined Siemens Power Corporation-Nuclear Division actions

associated with the incorrect manufacturing of the fuel assemblies with regard

to the identification of potential generic aspects. The fuel vendor formed an

Incident Review Board to investigate this matter on November 19, 1993. The

team reviewed draft Incident Review Board report EMF-93-209(P), "Incident

Review Board Report, Misconfigured Fuel Assemblies at Robinson," dated

December 1993. The report includes a review of reload records for Robinson,

Susquehanna, Dresden, Grand Gulf, Peach Bottom, Kuosheng 2, WNP-2,

Comanche Peak, and Laguna Verde to assure that each rod was located in the

correct position in each assembly. The review encompassed approximately 1240

fuel assemblies. The fuel vendor did not identify any other mispositioned

rods.

The team reviewed an internal memorandum of November 28, 1993, Siemens Power

Corporation, subject "Potential Error in Generation of the Transport

Correction Factors Used to Generate INCORE Analytic Factors" (KCS:93:016).

The anomalies were identified during an examination of the INCORE 30 percent

power maps for Robinson. In accordance with ANF-POO,002, Quality Assurance

Procedure No. 3, "Design Control for Nuclear Fuel," the fuel vendor began an

assessment of the potential error's impact on the Robinson cycle-16 fuel load.

The assessment is scheduled to be completed by December 15, 1993. The team

discussed the potential generic implications of the error with the fuel

vendor. The fuel vendor indicated that the INCORE Computer Code was a

Westinghouse Code and had only been used by the fuel vendor for Robinson and

that Robinson had been informed of the potential error (the fuel vendor did

indicate that they intended to use the code for a future reload of Shearon

Harris).

The team concluded that 10 CFR Part 21 requirements had been met.

The team also discussed the potential for the error being applicable to other

facilities which use the INCORE Computer Code. The fuel vendor stated that

the error had been made by the fuel vendor personnel and was not inherent in

the code. Since the fuel vendor evaluation of this issue was not complete,

this item should be examined during a future inspection.

.34

5.4.1

AIT Conclusion

The team concluded that 10 CFR Part 21 requirements had been met.

6.0

ASSESSMENT OF LICENSEE INVESTIGATION OF THESE EVENTS

6.1

Assess the effectiveness and thoroughness of the licensee's

investigation of these issues.

The team reviewed their independent evaluation of the events and root causes

against the licensee and the fuel vendor findings. The team concluded that

the licensee and its fuel supplier have done a thorough job of review and

their root cause determinations are reasonable. The licensee's and the fuel

vendor's level of management involvement in their investigations and in their

internal critiques of their investigations has been indepth and involved the

highest levels of their respective organizations. The AIT findings basically

agree with that of the licensee as noted below and in specific places in the

report.

6.1.1

AIT Review of the licensee Nuclear Instrumentation Miscalibration

Review Team Assessment

The licensee's investigation attributed the root cause for the nuclear

instrumentation miscalibration event to be the inadequate implementation of

.corrective

action following similar industry events. A casual factor for the

event was determined to be an improper methodology used in calculating the

power range currents.

Their investigation found that the licensee calculated a correction factor to

apply to the previous cycle's 100 percent Power Range Nuclear Instrumentation

currents by multiplying the previous current by a ratio of previous cycle

average relative power for three fuel bundles to predicted average relative

power for fuel bundles in the new core load. In this calculation, the two

nearest, outer diagonal fuel assemblies and a third inner assembly (second

diagonal) were used for relative power comparisons. This methodology differed

from that recommended by the Nuclear Steam Supply System vendor Westinghouse

(see figure Z).

This licensee assessment was issued on December 3, 1993. The members and

their scope are outlined in Appendix C.

The AIT agreed with these findings and conclusions and in addition, found that

the Nuclear Instrumentation miscalibration was the result of an incomplete

understanding of the core geometry considerations by the procedure writer and

inadequate review by the corporate fuels group.

6.1.2. AIT Review of Licensee's Robinson Fuel Loading Investigation Team

Assessment

The licensee team considered the fuel vendor errors and their not being

detected by the licensee as Principal Causes.

35

The licensee's investigation attributed contributing causes for the

failure of a fuel inspection tool and consequent loose parts event to

be:

a. inadequate tool design

b. inadequately defined roles and responsibilities

c. failure to follow proper foreign material exclusion practices.

The AIT agreed with the above findings and conclusions with the addition of

the contribution of the poor physical condition of contractor and licensee

personnel.

The licensee's investigation attributed the contributing causes of the

misconstructed fuel bundles to be:

a. the licensee's failure to ensure fabricated fuel meets design

requirements because of a lack of management direction and

inadequacies in review and evaluation programs; and

b. the fuel supplier's fabrication of bundles with incorrect

Gadolinium rod placement, caused by inadequacies in procedures,

accountability, training and overchecks.

The AIT agreed with the above findings and conclusions.

The licensee's investigation attributed the contributing causes of the

core design data problem to be:

a. Fuel supplier errors in producing the input due to the work being

hurriedly done, inadequate procedures and inadequate data checkout

tools.

b. Inadequate licensee oversight and review of the supplier analyses.

The AIT agreed with the above findings and conclusions.

This assessment was issued on December 8, 1993. The membership and their

scope are outlined in Appendix C.

7.0

EXIT MEETING.

On December 6, 1993, the team, accompanied by the Deputy Regional

Administrator for Region II, conducted a public exit meeting at the Robinson

site. The licensee and NRC personnel attending this meeting are listed in

Appendix D. Proprietary material has not been included in this inspection

report. During the exit, the team summarized the scope and findings of the

inspection. There were no dissenting comments from the licensee of the

findings.

APPENDIX A

H. B. ROBINSON AUGMENTED INSPECTION TEAM (AIT) CHARTER

A.

Basis

On November 16, 1993, during startup of H.B.Robinson Unit 2, reactor core flux

anomalies were identified during flux mapping at approximately 30 percent power.

A second flux map confirmed core design problems. Other problems were identified

during the startup including the Power Range Nuclear Instruments reading 10

percent below the actual power level of 30 percent.

B.

Scope

1. Develop and validate the sequence of events associated with the

November 12, 1993, startup until Hot Shutdown was reached on

November 17, 1993.

2. Assess the root cause and safety significance of the core neutron flux

anomalies with regard to fuel and technical specification limits.

3. Determine the root cause of the miscalibrated nuclear instruments identified

during startup.

4. Assess operator performance relative to the nuclear instrumentation

miscalibration problem.

5. Assess the adequacy of station nuclear instrumentation calibration and

refueling procedures.

6. Determine the root cause of the broken fuel handling tool event, and the

effectiveness of licensee oversight of contractor fuel handling activities.

7. Assess the effectiveness and thoroughness of the licensee's investigation of

these issues.

8. Assess the cause and extent of the fuel manufacturing errors at Siemens Fuel

Manufacturing Facility and the extent and effectiveness of fuel verification

at the site.

9. Assess the adequacy of the licensee's oversight of Siemens' fuel analysis and

Quality Assurance programs.

10. Prepare a special inspection report documenting the results of the above

activities within 30 days of the inspection completion.

C.

Team Members

Team members will include:

Team Leader, Senior Resident Inspector, Robinson

Resident Inspector, Reactor Physics Specialist, License Examiner, and

Vendor/Quality Assurance Inspectors to inspect at the Robinson Site; follow-up at

the Siemens Fuel Manufacturing Facility will be conducted by the Reactor Physics.

Specialist and the Vendor/Quality Assurance inspectors.

Appendix A

2

SUPPLEMENT TO AUGMENTED INSPECTION TEAM (AIT) CHARTER FOR H. B. ROBINSON AND SIEMENS FUEL

MANUFACTURING FACILITY

A.

Basis

On November 16, 1993, during startup of H. B. Robinson Unit 2, reactor core flux

anomalies were identified during flux mapping at approximately 30 percent power. A

second flux map confirmed core design problems.

Other problems were identified which

included the Power Range Nuclear Instruments reading 10 percent below the actual power

level of 30 percent and a broken fuel handling tool.

B.

Scope

1. Determine the root cause of the broken fuel handling tool event.

2. Assess the adequacy of Siemens' Quality Assurance program for the manufacture of

special fuel tools.

3. Assess the cause and extent of the fuel manufacturing errors at Siemens Fuel

Manufacturing Facility and the extent and effectiveness of fuel

assembly

verification at Siemens.

4. Assess the adequacy of the licensee's oversight of Siemens' fuel analysis and

Siemens' Quality Assurance programs.

5. Assess the Siemens analysis of the core neutron flux anomalies.

6. Assess the effectiveness of Siemens' program for notifying licensees of known

deficiencies in either hardware or services provided.

7. Prior to exiting the Siemens'

facility brief the AIT team leader of the

preliminary inspection findings via telephone.

8. Provide inspection results in writing to AIT team leader within one week of

exiting the Siemens' facility.

C.

Team Members

Team members will include:

Reactor Physics Specialist -

Edward D. Kendrick and

Vendor/Quality Assurance Inspectors -

Steven Matthews and W. H. Rogers.

APPENDIX B

AIT REVIEW TEAM

Corrective Action Assessment Team

Warren Dorman

Team Leader, RNP CAP/0EF

Franklin Murray

HPES RNP

BND

HNP

SCOPE:

Review past RBN performance (NAD,

INPO, NRC,

and other assessments) and evaluate

effectiveness of RBN CAP program in correcting previously identified performance

issues and predicting areas requiring additional attention.

Robinson Fuel Loading Investigation Team

Lou Martin

Team Leader

Bob Toth

INPO, Assistant Team Leader

Dave Waters

(Misconfiguration Focus)

John Eads

(Inspection Tool Failure Focus)

Jim Thompson

(Power Escalation Recommendation Focus)

tside Member

(Assist With Fuel Fabrication Focus)

OPE:

(1) Conduct a detailed root cause analysis of the core loading problems

of the following:

-

The Siemens inspection tool failure and the resulting fuel assembly

relocation.

-

The misconfiguration of fuel assemblies.

-

The adequacy of the licensee's oversight of Siemens activities both

onsite refueling and the core analysis activities.

(2) Review documentation and interview personnel at HBR,

Fuels,

and

Siemens to determine root cause and why not identified by the

licensee and Siemens prior to fuel load.

(3) Evaluate casual factors for other impact.

(4) Complete tasks prior to head replacement.

pendix B

2

Nuclear Fuels Instrumentation Investigation Team

C. S. Hinnant

Team Leader

Chip Moon

Operations

Bryan Waldsmith

Operations

Danny LaBelle

Fuels

Jo Ellen Westmoreland

Reactor Engineer

Franklin Murray

HPES

Dick Cady

CAP/Maintenance

Brian O'Donnell

INPO

David Coates

Training

SCOPE:

Conduct investigations following the following guidelines:

(1) Operations:

time line; events and casual factor;

ERFIS data;

Operations logs; plant data; -and power ascension coordination

(2) Fuels:

fuel vendor data; corporate fuel design data; fuels/plant

interface.

(3) Reactor engineering interface with fuels and operations and

comparison of Harris lessons learned with HBR corrective actions.

(4) HPES:

Event analysis using "yellow sticky" method and HBR actions

from similar O.E. identified events.

(5) CAP/Maintenance:

PL-026 and format of/process to develop final

report.

(6) INPO:

Industry experiences.

(7) Training:

Reactivity management training, and startup from RFO

training.

APPENDIX C

ATTENDANCE LIST AT EXIT DECEMBER 6, 1993

S. A. Bilings

Regulatory Affairs

T. A. Peebles

AIT Leader, RIH

L. A. Reyes

Deputy Regional Administrator, RIH

E. D. Kendrick

Nuclear Engineer, NRR

C. R. Ogle

AIT Member, RI

B. H. Rogers

Reactor Engineer/UIB, NRR

S. M. Matthews

Quality Assurance Engineer DRIL/VIB, NRR

D. Waters

Manager, Regulatory Affairs, CPO

S. Zimmerman

Manager, Nuclear Fuel Management & Safety Analysis

M. Pearson

Plant General Manager, Robinson

C. R. Dietz

VP, RNPD, CP&L

H. W. Habermeyer, Jr.

VP, NSD, CP&L

W. S. Orser

Exec VP, Nuclear Generation

R. E. Rogan

Manager, CP&L, Licensing

B. H. Clark

Manager, Maintenance

A. R. Wallace

Manager, Licensing/Regulatory Programs

M. Herrell

Manager, Training

T. P. Cleary

Manager, Technical Support

J. Guibert

Consultant to CP&L

D. G. McAlees

Sr. VP & GM, Siemens, Nuclear Division

N. Morgan

VP Engineering, SPC-ND

Watts

Electrical Dept-SCPSC

S. Stancil

Nuclear Bus. Oper., CP&L

S. Singh Bajwa

NRC, NRR, Projects

B. L. Mozafari

NRC, NRR, PDII-1

P. J. Jordan

Manager, Nuclear Human Resources, CP&L

W. S. Baum

Nuclear Employee Relation, CP&L

G. Newsome

Nuclear Engineer, CP&L

W. Pridgen

CP&L, Manager

C. S. Olexik

Manager, Plant Assessment, CP&L

K. Clark

Public Affairs, NRC, RII

H.B. ROBINSON CORE

AS-rDESIGNED

AS -BUIL TN

03

03

05

06

06

07

07.I

Itlot

112

$

0V

14

14.

15

1

P H M LK

J

C

F E 0C

A

R PN M L KJ

OCC

0A

Q UAIDRA

cowr..ii

GDOMJA RODS

4 000-

-2

50

0

a IE

E Fl'.E

-'?I)

I.IC 2A

-01-11C-2

50 0 "D

L I

HA

-

LEF T HAND/

CL

AMPSHAFT0:125

06 D1A0.

EXPANDER

TU~fE-j

I

LENGTH PLATE-L..I

IREF)~ral

Cacat@

_____________

____

Il~

LEGT

MEASURIN

TOO

(H ROBISON

FIGURE Z

RECOMMENDED ASSEMBLY TO USE FOR NI CALIBRATION

Igo

180*

Rf PNM

LK

J

S

F

EDC

A

.3

6

7

90*--8

4300-.

-2-70

A

CCC

A

Thre Loop Plant