ML14178A383

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Insp Rept 50-261/93-18 on 930710-0814.Violations Noted. Major Areas Inspected:Operational Safety Verification, Surveillance Observation & Maint Observation
ML14178A383
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 09/08/1993
From: Ogle C, William Orders
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A381 List:
References
50-261-93-18, NUDOCS 9309280217
Download: ML14178A383 (14)


See also: IR 05000261/1993018

Text

sa REG&

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.: 50-261/93-18

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.:

DPR-23

Facility Name:

H. B. Robinson Unit 2

Inspection Conducted:

July 10 - August 14, 1993

Inspector:

'

W. T. Orders, Senior Resident Inspect r

Date igned

Inspector:

)

.34

/

C.'R. Og e, esident Inspector

Date

igne

Approved by:

'

H. 0. Christensen, Chief

Date Signed

Reactor Projects Section 1A

Division of Reactor Projects

SUMMARY

Scope:

This routine inspection was conducted in the areas of operational safety

verification, surveillance observation, and maintenance observation.

Results:

One violation with three examples of operators failing to follow procedures

was identified involving; inadequate locked valve control (paragraph 3),

failure to adequately monitor equipment alarms (paragraph 3), and failure to

follow procedure during EDG testing (paragraph 4).

Another violation was identified concerning the failure to maintain design

control of the Reactor Auxiliary Building Ventilation System. (paragraph 3)

A third violation was identified concerning the failure to control work on

safety-related equipment. (paragraph 5)

An Inspection Followup Item was identified involving the potential for alarm

conditions to be disguised. (paragraph 3)

9309280217 930910

PDR ADOCK 05000261

PDR

REPORT DETAILS

1.

Persons Contacted

C. Baucom, Senior Specialist, Regulatory Compliance

D. Bauer, Regulatory Compliance Coordinator, Regulatory Compliance

S. Billings, Technical Aide, Regulatory Compliance

  • B. Clark, Manager, Maintenance
  • T. Cleary, Manager, Technical Support

D. Crook, Senior Specialist, Regulatory Compliance

C. Dietz, Vice President, Robinson Nuclear Project

R. Downey, Shift Supervisor, Operations

J. Eaddy, Manager, Environmental and Radiation Support

S. Farmer, Manager -

Engineering Programs, Technical Support

R. Femal, Shift Supervisor, Operations

  • W. Flanagan Jr., Manager, Operations

W. Gainey, Manager, Plant Support

  • J. Harrison, Manager, Regulatory Compliance

P. Jenny, Manager, Emergency Preparedness

D. Knight, Shift Supervisor, Operations

A. McCauley, Manager -

Electrical Systems, Technical Support

D. Morrison, Shift Supervisor, Operations

D. Nelson, Shift Outage Manager, Outages and Modifications

A. Padgett, Manager, Environmental and Radiation Control

0. Seagle, Shift Supervisor, Operations

M. Scott, Manager, Performance Engineering

E. Shoemaker, Manager, Mechanical Systems, Technical Support

W. Stover, Shift Supervisor, Operations

  • D. Waters, Manager, Regulatory Affairs

0. Winters, Shift Supervisor, Operations

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

  • Attended exit interview on August 18, 1993.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Plant Status

The unit operated from July 10 to July 12, 1993, with power at

approximately 70 percent to reduce SW/CW weir discharge temperatures.

Following a power ascension on July 12, 1993, the unit operated at 100

percent until July 16, 1993. A power reduction to 70 percent was again

conducted on July 16 to 70 percent and the unit operated on July 17 and

18 at 70 percent to reduce weir discharge temperatures.

Power was.

raised to 100 percent on July 19 and the unit operated at this power

until a power reduction on July 21.

0C

2

The July 21 power reduction was performed in response to high steam

generator cation conductivity. Following the discovery of elevated

conductivity the unit operated at power levels of 25 percent to 80

percent until the generator chemistry was restored. Following an

increase in power to 100 percent on July 26 the unit operated at 100

percent until the end of the inspection period.

3. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with regulatory

requirements. These activities were confirmed by direct observation,

facility tours, interviews and discussions with licensee personnel and

management, verification of safety system status, and review of facility

records.

To verify equipment operability and compliance with TS, the inspectors

reviewed shift logs, Operation's records, data sheets, instrument

traces, and records of equipment malfunctions. Through work

observations and discussions with Operations staff members, the

inspectors verified the staff was knowledgeable of plant conditions,

responded properly to alarms, adhered to procedures and applicable

administrative controls, cognizant of in-progress surveillance and

maintenance activities, and aware of inoperable equipment status. The

inspectors performed channel verifications and reviewed component status

and safety-related parameters to verify conformance with TS. Shift

changes were routinely observed, verifying that system status continuity

was maintained and that proper control room staffing existed. Access to

the control room was controlled and operations personnel carried out

their assigned duties in an effective manner. Control room demeanor and

communications were appropriate.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment, and to

verify that radiological controls, fire protection controls, physical

protection controls, and equipment tagging procedures were properly

implemented.

Oil Spill In Lake Robinson

At 8:07 a.m. on July 25, 1993, the licensee was advised by the

Darlington County Sheriff's Department, that a vehicle had been found in

Lake Robinson. This resulted in an oil/gasoline slick on the lake

estimated by the licensee to be approximately 60 square feet in size.

At 10:05 a.m., the licensee was informed by the State of South Carolina

Department of Health and Environmental Control that the slick had

dissipated.

As. a result of licensee notifications to the South Carolina Department

of Health and Environmental Control, National Response Center, and the

Darlington County Emergency Planning Organization, thelicensee made a

3

4-hour non-emergency notification to the NRC in accordance with the

requirements of 10 CFR 50.72 (b) (2) (VI), Offsite Notification, at

10:52 a.m. on July 25, 1993. The licensee also notified the Senior

Resident Inspector immediately prior to the 10 CFR 50.72 notification.

Based on their review of this event, the inspectors concluded that the

licensee met the requirements for NRC notification specified in 10 CFR

50.72. The inspectors have no further questions on this event.

Inadequate Locked Valve Control

On the afternoon of July 26, 1993, the resident inspectors were

performing a routine safety system inspection of the motor driven

auxiliary feedwater pumps. During that effort, it was noted that AFW

valves, FCV 1424 and FCV 1425, the discharge flow control valves for the

pumps, were not aligned as required by the applicable Operating

Procedure OP 402, Auxiliary Feedwater System. The procedure requires

that the two hydro-motor actuated valves be closed with the manual

actuator handle disengaged and locked. The inspectors noted that valve

FCV 1424 was completely unsecured with the lock and chain merely wrapped

around the valve actuator body, but not in contact with the handle of

the manual actuator. The inspector also noted that the chain for valve

FCV 1425 was loosely wrapped around the manual actuator handle but could

easily be removed leaving the valve unsecured.

The inspectors brought their observations to the attention of an

auxiliary operator and subsequently discussed the issue with operators

in the control room. The valves were properly secured shortly

thereafter.

Additionally, on July 30, 1993, the inspectors observed that the chain

intended to lock post accident vent valve, PAV-35 was loosely wrapped

around the manual actuator handle but could easily be removed leaving

the valve unsecured. The inspector brought his observations to the

attention of an auxiliary operator who properly secured the valve.

Operations Procedure OP 402, Auxiliary Feedwater System, requires in

section 6.0, Normal Operations, step 6.1.1 that valves FCV-1424 and FCV

1425 be aligned in the closed position with the manual actuators

disengaged and locked when placing the system in standby alignment.

Operations Management Manual OMM-009, Locked Valve List, delineates

those valves within the plant which are required to be locked. OMM-009

states that a properly locked valve will have the chain secured between

the valve operator and'body such that it may not be removed unless the

lock is removed. Attachment 6.1 of OMM-009 contains a listing of those

valves, which are required to be locked and the position of each. OMM

009 lists valves FCV-1424, FCV-1425 and PAV-35 as valves which are to be

locked.

Technical Specification 6.5.1.1 Procedures, Tests and Experiments

require in part that written procedures be established, implemented and

4

maintained, covering the activities recommended in Appendix A of

Regulatory Guide 1.33, Rev 2. 1978, including the operation of the

auxiliary feedwater system and combatting emergencies/significant

events.

Contrary to the above, on July 26 and July 30, 1993, respectively,

valves FCV-1424, FCV-1425 and PAV-35 were found improperly secured, in

violation of the requirements of procedures OP-402 and OMM-009. This is

one of three examples which in the aggregate comprise a Violation:

Operations Failure To Follow Procedures, Three Examples. 93-18-01.

Failure To Note Deviation In Indicated Rod Position And Average Bank

Position

At 9:32 a.m. on July 27, 1993, an alarm was recorded on the control room

ERFIS printer indicating a rod misalignment in Group 2. It should be

noted that this "alarm" does not have an audible feature, rather, it is

a "silent" alarm typer message. This alarm occurred as a result of a

deviation between the indicated position for rod B-10, a Group 2 rod,

and its average bank position. The alarm was recorded again at 9:47

a.m. and at 10:02 a.m..

At 10:04 a.m., a message was printed indicating

that the rod misalignment had returned to normal.

This occurred despite

the fact that the indicated position of the rod still deviated from the

average bank position by an amount in excess of the limits specified in

TS 3.10.1.5. Commencing with the 10:30 a.m. printout, and every half

hour thereafter, the position of the rod as indicated on the ERFIS

printout, was shown to be in deviation from its average bank position.

Additionally, a data quality of "BAD" was specified for the rod on these

printouts. The operators on shift failed to detect this condition. The

oncoming operator discovered the situation at shift turnover at 7:00

p.m. that evening.

Following this discovery, the licensee entered AOP-001, Malfunction of

Reactor Control System, at 7:15 p.m. The deviation was attributed to an

indication error for the B-10 IRPI. At 9:30 p.m., following an

adjustment to the indicated position for rod, AOP-001 was exited.

The inspectors independently reviewed the ERFIS computer printouts for

July 27, 1993, and interviewed the reactor operator on watch during

dayshift that day. The inspectors concluded that the reactor operator

failed to note repeated indications of a potential rod misalignment in

excess of TS limits for almost 9.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. When questioned by the

inspectors, the reactor operator admitted that he failed to consistently

review the ERFIS printout which recorded rod positions. The failure of

the operator to note the indication of a potential rod misalignment is a

failure to follow procedure OMM-023, which specifies that operators

perform thorough general inspection of assigned spaces and that

operators be knowledgeable of equipment parameters.

Technical Specification 6.5.1.1.1.a, Procedures, Tests, and Experiments,

requires in part that written procedures be established, implemented and

maintained concerning the activities delineated in Appendix A of

5

Regulatory Guide 1.33, Rev. 2, February 1978, including procedures for

log entries, record retention, and procedure review. Operations

Management Manual Procedure, OMM-023, Operator Logs and Rounds, states

that an operator shall perform a thorough, general inspection of his

assigned area and that operators should be knowledgeable of equipment

parameters that are to be monitored.

Contrary to these requirements, on July 27, 1993, the reactor operator

failed to note a deviation between the indicated position for rod B-10

and its average bank position which was in excess of Technical

Specification 3.10.1.5 limits, for a period of approximately 9.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.

This is one of three examples which in the aggregate comprise

Violation: Operations Failure To Follow Procedures, Three Examples. 93

18-01.

The inspectors requested the licensee perform an analysis of other alarm

,features provided by ERFIS to determine if there are other cases in

which alarms would clear as a result of input data being assigned a

quality code of "BAD". This analysis will be evaluated by the

inspectors to ensure that alarms will not inadvertently be cleared

during an accident scenario. Pending this evaluation, this item will be

tracked as IFI 93-18-02: Alarm Features Provided By ERFIS Which Can

Inadvertently Clear.

Failure To Maintain Design Control of Reactor Auxiliary Building

Ventilation System

On July 28, 1993, a member of the licensee's staff noted that a tarp

which had been erected as a ventilation boundary where an exterior

auxiliary building door had been removed, was deflected outward

indicating that the pressure inside the auxiliary building was greater

than that outside. It was ultimately concluded that the Reactor

Auxiliary Building Ventilation System was not maintaining the building

at a negative measure as designed.

System Design

As described in the FSAR, the Reactor Auxiliary Building

Ventilation system is designed, in part;

-

to maintain potentially contaminated areas of the Reactor

Auxiliary Building at a negative pressure

-

to route the ventilation exhaust from the potentially

contaminated areas to the plant vent stack to ensure

continuous monitoring by the radiation monitoring system

-

to assure that the air distribution in the building is such

that air movement is from areas of lesser contamination to

areas of higher contamination potential

0II

6

Background

Based on information available at the time, a review of relative

events preceding this issue revealed the following:

Prior to 1979, numerous modifications were made to the

auxiliary building which may have changed the as-built

design of the Reactor Auxiliary Building Ventilation system.

These included but were not limited to sealing cable and

pipe penetrations, the addition of fire doors, and duct work

changes.

In July 1979, a vendor service company was contracted to

correct known pressure problems in the building thought to

have been caused by the aforementioned modifications.

Between 1979 and 1987, the only major engineering work

performed relating to the system, was the initiation of

TAR/PCN 84-002 which was to correct inadequate ventilation

in some areas of the reactor auxiliary building due to the

aforementioned modifications.

In 1987 maintenance work request WR 87-APNK1 installed a new

shaft in fan HVS-1 when the old shaft failed. Testing

indicated that the building was at a positive pressure after

installation. It is not known if the building was at a

positive pressure prior to the maintenance. The system was

adjusted to reduce supply flow to get a negative pressure in

the building. The as-left flowrate was not recorded.

In 1988, MOD 934, which implemented the changes requested by

TAR/PCN 84-002 was approved and started. Actual

installation was scheduled to be completed in 1989 but is

still ongoing. Although not addressed by the MOD, the

system flow balance was affected by the ongoing work yet a

re-balance was not scheduled to be performed until all work

was completed; in this case, a period of five years.

In January of 1990, another vendor service company was

contracted to perform preliminary data collection to prepare

or the performance of the flow balance of the auxiliary

building associated with MOD-934.

In January of 1992 WR 91-AMYN1 was written to clean the

steam heater coils associated with HVS-1. The system

engineer stated that the coils were very dirty which

contributed to a high suction dp. The high suction dp

reduced the supply air flowrate which (it was subsequently

concluded) made the lower level of the building positive.

No post maintenance test was performed to verify that the

system's flow balance had not been affected. The licensee

7

stated that the lower level of the building remained

positive from this time, until July 1993.

-

In February 1993, weatherstripping and door seals were

installed on doors for fans HVE-2A/B and HVS-1. These

modifications decreased the exhaust flow coming from the

upper corridor. No post modification test was performed to

verify that the system's flow balance had not been affected.

According to the licensee, it was at this time that the

upper level of the reactor auxiliary building went positive

and remained in that condition until July 1993.

-

On July 26, 1993, per MOD 934, the aforementioned exterior

auxiliary building doors were removed. A tarp was installed

in their place. Observation of the tarp indicated a

negative pressure did not exist.

Event Details

On July 27, 1993, the operability of the Reactor Auxiliary

Building Ventilation System was questioned due to the work being

performed under Modification 934. One part of this modification

removed the doors serving the north end of the second floor

auxiliary building hallway. A tarp was erected to provide a

ventilation boundary. Licensee personnel observed that the

direction of movement of the tarp indicated that the air movement

through the hallway was toward the outside environment and that a

negative pressure was not being maintained.

Based on the system's design basis, this condition indicated that

the system was inoperable. The licensee initiated compensatory

actions which restored the Reactor Auxiliary Building Ventilation

System to a functional status. These actions included:

-

On July 28, 1993, operability determination 93-010 was

initiated as a result of the positive pressure. NED was

contacted to support the determination. On July 30, 1993,

operability Determination 93-010 was completed, concluding

that facility did not meet the design basis while a positive

pressure existed.

-

On July 29, 1993, the vendor service company completed an

as-found reading of flows. HVS-1 was measured at 52,664 cfm

when converted to STP. Exhaust flows were measured at

53,108 cfm. The licensee stated that exhaust flow was 444

cfm greater than supply, which they said indicated that the

overall building was at a negative pressure, although the

upper level hallway and the lower level of the building were

at a positive pressure.

8

-

On July 29, 1993, the licensee established a negative

pressure condition in the upper level hallway by partially

opening the door to the room which houses fans HVE-2A & B.

This increased the exhaust from the hallway which resulted

in a negative pressure in the area. Later that evening, the

licensee was able to achieve a negative pressure in the

lower level of the building using similar techniques.

-

At approximately 6:30 p.m. on July 30, 1993, the licensee

performed a building walkdown which confirmed that the

building was at a negative pressure. At the end of this

report period, the unit was operating with the

aforementioned compensatory measures in place.

Conclusion

The auxiliary building ventilation system was incapable of

performing its intended safety function for a period of

approximately 18 months preceding July 1993.

10 CFR 50 Appendix B, Criterion III, Design Control, as

implemented by the CP&L Corporate Quality Assurance Program

requires in part that measures be established to assure that

applicable regulatory requirements and the design basis, as

specified in the license application, are correctly translated

into specifications, drawings, procedures, and instructions of the

type to ensure the design integrity of the structure, system or

component; that measures be established to verify the adequacy of

the design such as by suitable testing; and that design changes be

subject to the design control measures commensurate with those

applied to the original design.

Contrary to those requirements,

The licensee failed to implement adequate measures to

maintain the integrity of the Reactor Auxiliary Building

Ventilation System design in that modifications and design

altering maintenance were implemented which degraded the

system yet neither suitable post modification test nor post

maintenance testing was performed to verify the system's

continued operability. This ultimately resulted in the

system being inoperable from January 1992 until July 1993.

This is a Violation: Failure To Maintain Design Control of Reactor

Auxiliary-Building Ventilation System VIO 93-18-03.

This is a Severity Level IV violation (Supplement I).

0II

9

4. Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities

on systems and components to ascertain that these activities were

conducted in accordance with license requirements. For the surveillance

test procedures listed below, the inspectors determined that precautions

and LCOs were adhered to, the required administrative approvals and

tagouts were obtained prior to test initiation, testing was accomplished

by qualified personnel in accordance with an approved test procedure,

test instrumentation was properly calibrated, the tests were completed

at the required frequency, and that the tests conformed to TS

requirements. Upon test completion, the inspectors verified the

recorded test data was complete, accurate, and met TS requirements, test

discrepancies were properly documented and rectified, and that the

systems were properly returned to service. Specifically, the inspectors

witnessed/reviewed portions of the following test activities:

OST-401

Emergency Diesels

(Slow Speed Start)

OP-604

Diesel Generators "A" and "B"

(A EDG Only)

EDG A Inoperability Due To Erroneous RPM Indications

At 1:25 p.m. on August 2, 1993, the licensee declared the A EDG

inoperable and entered TS 3.7.2.. This occurred after it was observed

during OST-401, Emergency Diesel Generator Slow Speed Start, that the A

EDG indicated engine speed could not be raised to the synchronous speed

of 900 RPM. TS 3.7.2 required that the EDG be returned to service

within seven days. During troubleshooting, the licensee determined that

a power supply in the RPM indicating circuitry was malfunctioning,

thereby, resulting in erroneous engine speed indication.

A temporary change to OST-401 was made to permit the use of a strobotach

to measure engine speed. The OST was successfully completed and the

licensee exited TS 3.7.2 at 4:10 a.m. of August 3, 1993.

After interviewing the system engineer and independently reviewing the

EDG electrical schematic, the inspectors determined that the RPM

indicating circuitry is not used for automatic control of the EDG. It

is used during manual starts of both EDGs. The inspectors concluded that

the unavailability of the RPM device did not render the EDG inoperable.

The inspectors noted that an operator assigned to operate the A EDG

during the troubleshooting flashed the field with an indicated engine

speed less than 900 RPM. This was done in an effort to determine the

actual engine speed by using the installed frequency meter as a check

for the RPM instrument. This is contrary to the requirements of

Operating Procedure, OPP-604, Diesel Generators "A" and "B", which

10

requires that the engine speed be raised to synchronous speed (900 RPM)

prior to flashing the field.

Technical Specification 6.5.1.1.a, Procedures, Tests, and Experiments

requires in part that written procedures be established, implemented,

and maintained concerning the activities outlined in Appendix A of

Regulatory Guide 1.33, Rev 2, February 1978. Appendix A, Item 4.1.2 (a)

requires procedure for operation of the EDGs. Operating Procedure, OP 604, Diesel Generators "A" and "B", requires that the engine speed be

raised to 900 RPM prior to flashing the field. Additionally, OP-604

contains a prohibition against operating an EDG at less than 900 RPM

with field excitation in service.

Contrary to these requirements, on August 2, 1993, the EDG A field was

flashed with an indicated engine speed of approximately 750 RPM. This

is one of three examples which in the aggregate comprise a Violation:

Operations Failure To Follow Procedures, Three Examples, 93-18-01.

Based on the troubleshooting witnessed by the inspectors, it is likely

that the EDG was operating at speeds in excess of 900 RPM while the

speed sensing circuit was inoperable. Hence, the safety significance of

flashing the EDG field was minimal.

5. Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

accordance with TS, approved procedures, and appropriate industry codes

and standards. The inspectors determined that these activities did not

violate LCOs and that required redundant components were operable. The

inspectors verified that required administrative, material, testing,

radiological, and fire prevention controls were adhered to. In

particular, the inspectors observed/reviewed the following maintenance

activities:

W/R JO 93-ADFY1

Receipt And Storage Of New Fuel

W/R JO 93-AHJB1

Adjust Door Latches To Provide Adequate

Seals For HVE-1 Fitter Housing

WR/JO 93-AHAWI

Repair of EDG A Fuel Oil Pump Indicator

Pegged High

WR/JO 93-AHWA1

Repair Governor On A EDG

WR/JO 93-AEE004

Check Brush Tension OnSpeed Change Motor

For EDG

11

Unauthorized Maintenance On Control Room Door

On August 2, 1993, during a routine tour, the inspectors observed

ongoing maintenance on the striker plate for door 49, the south control

room door. The door could not have been secured due to a partially

removed striker plate screw. At 2:23 p.m., as a result of the

inspector's questions to the shift supervisor on this observation, the

door, as well as the control room ventilation system, were declared

inoperable. Accordingly, the licensee entered TS 3.15.1.b. which

required that the inoperable door be returned to service in 48-hours or

the plant be placed in hot shutdown in 8-hours and cold shutdown in the

following 30-hours. Coincidentally , the A EDG was also inoperable due

to having failed OST-401 (see paragraph 4).

With an inoperable control

room ventilation system, the licensee was unable to satisfy the

requirements of TS 3.7.2.d for continued operation with one operable

EDG. As a result, the licensee entered TS 3.0. which required that the

unit be shutdown within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> and placed in cold shutdown within the

next 30-hours. The door was repaired and following successful

completion of OST-750, Emergency Ventilation System Bi-Weekly Test, and

OST-625, Fire Door Inspection, the licensee exited TS 3.0 and TS 3.15.1.b at 5:39 p.m. that afternoon.

The inspectors interviewed the fire technician and shift supervisor

involved and reviewed the OSTs completed prior to declaring door 49

operable. The inspectors concluded that maintenance had been conducted

on the door beyond that approved by the shift supervisor. The fire

protection technician recognized that the supplemental maintenance

rendered the door inoperable, but did not communicate this information

to the control room.

Technical Specification 6.5.1.1.1a., Procedures, Tests, and Experiments

requires in part that written procedures be established, implemented,

and maintained concerning the activities delineated in Appendix A of

Regulatory Guide 1.33, Rev. 2, February 1978. Appendix A, Item 9.e.

requires general procedures for the control of maintenance work. Plant

Program, PAP-013, Maintenance Program, requires that shift supervisor

permission be obtained before maintenance is performed on plant safety

system. On August 2, 1993, maintenance personnel initiated repairs on

the south control room door without having obtained the shift

supervisor's permission. This resulted in the door, as well as the

control room ventilation system, being declared inoperable.

This is considered to be a violation, Failure To Follow Procedure

Resulting In Unauthorized Maintenance (93-18-04).

Following the restoration of the door to service, the licensee reviewed

the requirements of TS 3.15. As a result of this review, the licensee

concluded that the entry into TS 3.0 was unwarranted and that the 48

hour LCO associated with TS 3.15 was the limiting requirement. The

licensee indicated that appropriate annotations would be made in the

plant records to reflect this subsequent decision. The inspectors have

no further questions of this event.

12

6. Exit Interview (71701)

The inspection scope and findings were summarized on August 18, 1993,

with those persons indicated in paragraph 1. The inspectors described

the areas inspected and discussed in detail the inspection findings

listed below and in the summary. Dissenting comments were not received

from the licensee. The licensee did not identify as proprietary any of

the materials provided to or reviewed by the inspectors during this

inspection.

Item Number

Description/Reference Paragraph

93-18-01

VIO: Operations Failure To Follow Procedure,

Three Examples ( Paragraphs 3, and 4).

93-18-02

IFI: Alarm Features Provided By ERFIS Which Can

Inadvertently Clear (Paragraph 3)

93-18-03

VIO: Failure To Maintain Design Control of

Reactor Auxiliary Building Ventilation System

(Paragraph 3)

93-18-04

VIO: Failure To Follow Procedure Resulting In

Unauthorized Maintenance (Paragraph 5).

7. List of Acronyms and Initialisms

AFW

Auxiliary Feedwater

AOP

Abnormal Operating Procedure

cfm

Cubic Feet Per Minute

CFR

Code of Federal Regulations

DBD

Design Basis Documentation

EDG

Emergency Diesel Generator

ERFIS

Emergency Response Facility Information System

FCV

Flow Control Valve

FSAR

Final Safety Analysis Report

HEPA

High Efficiency Particulate Airborne

HVE

Heating Ventilation Exhaust

HVS

Heating Ventilation Supply

IFI

Inspector Followup Item

IRPI

Individual Rod Position Indication

LCO

Limiting Condition for Operation

MOD

Modification and Design Control

NED

Nuclear Engineering Department

NRC

Nuclear Regulatory Commission

OMM

Operations Management Manual

OP

Operations Procedure

OST

Operations Surveillance Test

PAP

Personnel Access Portal

PAV

Post Accident Venting

PMT

Post Maintenance Test

13

RPM

Revolutions Per Minute

STP

Standard Temperature Pressure

SW/CW

Service Water/Circulation Water

SWBP

Service Water Booster Pump

TAR/PCN

Task Assistance Request/Plant Change Notice

TS

Technical Specification

W/R

Work Request

WR/JO

Work Request/Job Order