ML14178A079

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Insp Rept 50-261/90-30 on 901211-910110.Violation Noted. Major Areas Inspected:Operational Safety Verification, Surveillance/Maint Observation,Refueling Activities & Action on Previous Insp Findings
ML14178A079
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 02/01/1991
From: Christensen H, Garner L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A077 List:
References
50-261-90-30, NUDOCS 9102130112
Download: ML14178A079 (16)


See also: IR 05000261/1990030

Text

t~kREGU'

UNITED STATES

NUCLEAR REGULATORY COMMISSION

0.,

REGION 11

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/90-30

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted: December 11, 1990 - January 10, 1991

Lead Inspector:

/

/

L.

. Ga

r, Senior

sid

Inspector

Ddte Sioned

Other Inspector:

K. R. Jury

Approved by:

.-

H. 0. Christensen, Section Chief

Date Signed

Reactor Projects Branch 1

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation,

refueling activities and action on previous inspection findings.

Results:

A violation was identified involving an inadequately established preventive

maintenance procedure for inspection of the residual heat removal system pump

discharge check valves (paragraph 4).

The ultrasonic surface reflectors on the A steam generator upper girth weld

were determined (by visual and fluorescent magnetic particle inspections) not

to be similar to those associated with rapid crack propagation occurring in

other utilities' steam generators (paragraph 6).

The actual 1990 radiological exposure of 437 Person-Roentgen Equivalent Man

(REM) was less than the 450 Person-REM goal established at the beginning of

1990 (paragraph 2).

9102130112 910201

PDR

ADOCK 05000261

G

PDR

2

The component cooling water piping to the residual heat removal pump seal

coolers ruptured during a hydrostatic test. The probable root cause was

attributed to rain or other external water intrusion between the piping and

thermal insulation, resulting in extensive external corrosion of the carbon

steel pipe (paragraph 2).

Extensive service water system inspection, repairs, and component

refurbishment/replacement were performed during the refueling outage

(paragraph 2).

Strong communications and interfacing was evident between Technical Support

and Nuclear Engineering Department on both the service water system efforts

and the A steam generator indications resolution (paragraphs 2 and 6).

Fourteen spent fuel assemblies have been shipped from the site to the Harris

Nuclear Facility in North Carolina (paragraph 6).

All control rod guide tube support pins have been replaced with a redesigned

pin which is less susceptible to intergranular stress corrosion cracking

(paragraph 6).

REPORT DETAILS

1. Persons Contacted

  • R. Barnett, Manager, Outages and Modifications

C. Baucom, Shift Outage Manager, Outages and Modifications

J. Benjamin, Shift Outage Manager, Outages and Modifications

C. Bethea, Manager, Training

  • W. Biggs, Manager, Nuclear Engineering Department Site Unit

S. Billings, Technical Aide, Regulatory Compliance

R. Chambers, Manager, Operations

  • D. Crook, Senior Specialist, Regulatory Compliance
  • J. Curley, Manager, Environmental and Radiation Control
  • C. Dietz, Manager, Robinson Nuclear Project

D. Dixon, Manager, Control and Administration

J. Eaddy, Supervisor, Environmental and Radiation Support

S. Farmer, Supervisor -

Programs, Technical Support

R. Femal, Shift Foreman, Operations

  • W. Gainey, Plant Support

E. Harris, Manager, Onsite Nuclear Safety

  • J. Kloosterman, Director, Regulatory Compliance

D. Knight, Shift Foreman, Operations

E. Lee, Shift Outage Manager, Outages and Modifications

A. McCauley, Supervisor -

Electrical Systems, Technical Support

R. Moore, Shift Foreman, Operations

D. Nelson, Shift Outage Manager, Outages and Modifications

  • M. Page, Manager, Technical Support

D. Seagle, Shift Foreman, Operations

  • J. Sheppard, Plant General Manager
  • R. Smith, Manager, Maintenance

R. Steele, Shift Foreman, Operations

D. Winters, Shift Foreman, Operations

  • H. Young, Director, Quality Assurance/Quality Control

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and office personnel.

  • Attended exit interview on January 15, 1991.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the facility

was being operated safely and in conformance with regulatory

requirements. These activities were confirmed by direct observation,

facility tours, interviews and discussions with licensee personnel and

2

management, verification of safety system status, and review of facility

records.

To verify equipment operability and compliance with TS, the inspectors

reviewed shift logs, Operations' records, data sheets, instrument traces,

and records of equipment malfunctions. Through work observations and

discussions with Operations staff members, the inspectors verified the

staff was knowledgeable of plant conditions, responded properly to

alarms, adhered to procedures and applicable administrative controls,

cognizant of in-process surveillance and maintenance activities, and

aware of inoperable equipment status. The inspectors performed channel

verifications and reviewed component status and safety-related parameters

to verify conformance with TS. Shift changes were observed, verifying

that system status continuity was maintained and that proper control room

staffing existed. Access to the control room was controlled and

operations personnel carried out their assigned duties in an effective

manner. Control room demeanor and communications continued to be

informal, yet effective.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment, and to

verify that radiological controls, fire protection controls, and physical

protection controls were properly implemented.

Source Range Monitors

In preparation for fuel reloading, I & C determined on December 4, 1990,

that both source range monitors (NI-31 and NI-32) were not operable and

could not be repaired. Moisture apparently had intruded into the cables

and/or connectors, and short circuited the detectors. A PNSC review of

potential alternatives to monitor the core during fuel reloading resulted

in a decision to replace both the NI-31 and NI-32 detectors. Replacement

detectors were installed, tested, and placed in service on December 15,

1990. At the end of the report period, the licensee was in the process

of replacing the source range and intermediate range monitor cables.

CCW Line Degradation

On December 13, 1990, during hydrostatic testing for modification M-1017,

Eliminate RHR Pump Common Mode Failure, the CCW return line from the A

RHR pump seal cooler ruptured. Subsequently, based upon a visual

inspection, engineering concluded that portions of the supply and return

lines into the RHR pit were so extensively damaged by external corrosion

that successful hydrostatic test completion appeared improbable.

Engineering recommended replacement of supply and return piping sections

from both A and B RHR pump seal coolers. The pipe replacement was

accomplished in accordance with WR/JO 90-ARIT1, 90-ARIW1, and 90-ARJK1.

The piping was subsequently successfully hydrostatically tested on

December 19, 1990, per SP-369, System Hydrostatic Pressure Testing of

Component Cooling Water System, and returned to service.

3

The affected piping consisted of approximately 20 feet of 1 and 2-inch,

schedule 40 carbon steel piping. Preliminary root cause analysis

indicated that water, most likely rain, had over a period of years

penetrated between the pipe and its thermal insulation, thereby wetting

the pipe OD and causing the external corrosion. The piping degradation

went undetected apparently due to the piping being insulated. The

replacement piping was painted with an epoxy type paint to reduce the

potential for external corrosion. The licensee has not determined what

monitoring or inspections, if any, are necessary to detect future or

additional external piping corrosion. This is an IFI:

Review Steps To

Detect And/Or Preclude Extensive External Corrosion Of Carbon Steel

Piping, 90-30-01.

Inspection Report 89-09 discussed a RHR system common mode failure in

which a leak in the RHR pit would not be isolable during the

recirculation phase of an accident due to high radiation fields. This

postulated scenario would eventually result in both RHR pump motors

shorting out (i.e., loss of all ECCS capability). The report describes

compensatory measures to isolate certain potential leak paths into the

RHR pit by closing certain valves before entering the recirculation phase

of an accident. The compensatory actions did not include isolation of

the CCW lines to the RHR pump seal coolers. The pump vendor indicated

that the RHR pump seals could operate indefinitely at the temperatures

anticipated during the recirculation phase of an accident; however, it

was considered prudent to have the seal coolers remain in service during

an accident. This decision was based in part on the determination that

leakage from these lines was a relatively small contributor to the

estimated core melt frequency for the assumed event. If an external

inspection had been performed of these lines at that time, it appears

that the low probability of failure would not have been assumed. The

inspectors discussed with management that -future JCO evaluations should

consider what measures, if any, need to be taken to establish confidence

that equipment relied upon for acceptable continued operation is not

degraded.

1990 Radiological Goals Status

The E & RC Manager provided the inspectors with the following actual

end-of-year status of selected radiological goals:

Actual

Goal

Exposure (Person-REM)

437

<450

Contamination Events

235

<300

Contaminated Area (sq. ft.)

5795

<2000

Radwaste Volume (cu. ft.)

2467

<4000

Prior to the outage (i.e., end of August 1990), the contaminated area YTD

value was 1220 sq. ft..

During the outage, the contaminated area has

typically varied between 5,000 and 6,000 sq. ft..

The licensee is

decontaminating areas such that the amount of contaminated space will be

4

reduced to levels similar to that existing prior to the outage. The

radwaste volume shipped is the lowest amount since 1973, the year in

which radwaste volume trending was initiated.

System Cleanliness

On January 3, 1991, the inspectors observed that CC-702A, the A CCW pump

discharge check valve, had been left open without anyone in the area. The

inspectors reported this condition to an operator so that appropriate

measures could be taken to preclude foreign materials from entering the

system. The inspectors visually verified that no foreign materials had

entered into the valve body at that time.

SW System Outage Activities

During RO-13, extensive inspections, repairs, refurbishment/replacements,

and modifications were performed on the SW system and its components.

These activities were performed as a result of various requirements (i.e.,

GLs 89-13 and 90-05), commitments, and licensee initiatives. The

inspection portion of the SW system efforts included visual and camera

inspections of the 30", 24", 20", 18", and 16" diameter, cement-lined

piping.

This inspection included both the buried north and south SW

supply headers which are discussed later in detail.

Key SW check valves

inspected include:

the A,B,C, and D SW pump discharge check valves,

SW-374, -376, -375, and -377, respectively; the north and south header

check valves, SW-541 and -545, respectively; and the A and B SWBP

discharge check valves, SW-561 and -560, respectively. These valves were

not disassembled due to replacement part unavailability; however, each

valve was inspected, cleaned, and mechanically stroked with the exception

of SW-561, which was replaced on November 8, 1989.

With the exception of the buried SW supply headers, most of the cement-lined

SW lines and joints inspected were relatively sound, with only localized

cement liner spalling evident. These localized areas, as well as the

header joints, were repaired with Speed Crete Blue Line, which is a

commercially prepared portland cement mortar. The acceptability of this

material was justified and approved by EE 90-100, Revision 0, Evaluation

of a Commercial Prepared Portland Cement Mortar for Repair of Cement

Lining of the RNP's Service Water Pipes. The repairs were performed

under SP-968, Cement Lining Repairs Using "Speed Crete Blue Line".

Additionally, a black "slime" was identified as covering the inside of

the large majority of the SW piping inspected. This foreign substance is

discussed in the following paragraph. In regard to the buried north and

south SW supply headers, the following paragraphs give a brief description

of the inspection/repairs that were performed on the subject piping.

The buried SW supply piping is a 31.375" OD by 0.188" nominal wall,

cement-lined pipe divided into two headers approximately 900 feet long

each. The piping was purchased and installed in 1968 under the AWWA

specifications.

Camera, visual, and UT inspections were performed inside

5

the pipe. The initial camera inspections, as well as visual walkdowns,

indicated the piping to be coated with a black "slime" with localized

areas of concrete lining missing. The inspections also identified that

the non-coated cross-sectional areas had experienced corrosion-induced

pipe thinning. Degradation was observed primarily in the bell and spigot

(mechanical slip-fit) joints with additional joints also exhibiting

corrosion. The black "slime" was determined to be manganese dioxide

hydroxide and iron dioxide hydroxide. Agitation and aeration of Lake

Robinson water which contains high levels of tanic acid caused these

chemicals to precipitate out of solution.

After the initial inspections revealed corrosion in the locations which

were not cement-lined, the licensee attempted to quantify the degree of

corrosion through interior UT examinations of selected north and south

header joints. This UT indicated that there were not any areas with a

minimum wall thickness less than the calculated required thickness.

Based upon both the interior UT and the visual examinations, the bell and

spigot joints in the north header were cleaned and covered with Speed

Crete. Subsequently, it was determined that the interior UT data was

invalid due to the UT probe being larger than the effective size of the

corroded areas being measured (i.e., some pit depth was measured as wall

thickness). Additional and more accurate UT was then performed on

selected joints from the piping's exterior. Based on the initial visual

determination that the south header was in worse shape and more

susceptible to corrosion (i.e., piping not as well fit-up with larger

joint gaps and contained more elbows), the additional examinations

focused on the joints determined to be the 12 worst south header joints.

Two "typical" (bell and spigot) joints in the south header, S-10 and

S-42, were determined to require repair. All other "typical" joints were

evaluated per calculations and formulas (calculation no. RNP-C/STRS-1114)

per ASME Code Case N-480 and were determined to be acceptable.

The four atypical (non-bell and spigot) joints in the north header were

repaired/replaced based on the corrosion severity on those joints. In

addition to south header joints S-10 and S-42, weld areas on joints S-6,

5-31, and a factory butt welded joint required repair. Joints S-10 and

S-42 utilized a butt strap repair/replacement technique, where S-6, S-31,

and the factory joint required weld repair. All repair/replacements were

performed in accordance with the original pipe design, ASA B31.1-1955

Edition, Code for Pressure Piping, and AWWA Standard, ANSI/AWWA C206-88,

Field Welding of Steel Water Pipe. Subsequent weld joint inspection was

performed per AWWA C206-88, Section 5.8. All repaired/replaced joints

were subsequently covered with Speed Crete.

Upon repair/replacement

completion, the system was hydrotested per ASME Section XI, IWA-5000,

1977 Edition, Summer 1978 Addenda. At the end of the report period, the

inspectors had not reviewed the calculations, inspections, and hydrotest

results; however, they were deemed acceptable by the licensee.

Also inspected during the outage were the smaller diameter SW lines, as

well as the SW intake structure and traveling screens.

The intake

structure and screen inspections did not identify significant structural

6

damage nor sediment/fouling buildup that could affect SW pump

performance. Smaller diameter SW piping lines (i.e., MDAFW and SDAFW Lube

Oil Coolers, ECCS Pump Room Coolers) were determined to have varying

degrees of fouling. The normal manual cleaning and flushing method was

supplemented by utilization of a foam plug or "pig".

The procedure

involved the forcing of the "pig" through the lines, thus swabbing the

pipe walls and loosening the fouling material.

The lines were

subsequently flushed. Some small diameter SW lines were only manually

cleaned and flushed.

During the outage, extensive refurbishment was performed on three SW

pumps and three motors, as well as the SWBPs and motors. The

refurbishment included, but was not limited to: shaft, impeller, and

bearing replacement; tolerance and clearance checks; shop testing; and

generation of pump specific head curves. The motor refurbishment (also

vendor performed) included cleaning, tolerance checks, electrical

testing, etc., as well as any necessary component repair/replacement.

At the end of the report period, A, B, and D SW pumps and motors had

been refurbished and installed with the original C pump and motor

installed as well.

The refurbished C motor (originally a spare) was

expected to arrive on site by January 18, 1991. An additional

refurbished (spare) pump was already on site. Upon delivery and outage

schedule permitting, the refurbished pump and motor will be installed.

Subsequent to this installation, the original C pump and motor will be

refurbished, with the pump's internals being upgraded. The refurbished

SWBP and motors have been reinstalled.

Prior to the outage, twenty-nine SW valves were scheduled to be replaced.

The valves were scheduled for replacement due to design changes, lack of

replacement parts, and in some cases due to degradation. Component

availability resulted in twenty-two of these valves being replaced, as

well as three others which were originally scheduled for repair. The

following is a list of the replaced valves:

Valve

Description

SW-20

CCW Hx A Cooling Water Supply

SW-21

CCW Hx B Cooling Water Supply

SW-23

SW Return from Auxiliary Building

SW-142

TCV-1650 Inlet

SW-143

TCV-1650 Outlet

V6-33 A,B,C,D,E,F

SWBP Supply to HVH Units

V6-34 A,B,C,D

HVH Cooling Water Return

Isolation

SW-24

South Header Supply to SWBP

SW-26

SWBP Suction Cross Connect

SW-27

SWBP Suction Cross Connect

SW-28

SWBP A Suction Valve

SW-29

SWBP B Suction Valve

SW-32

SW Pump A Discharge Valve

SW-33

SW Pump B Discharge Valve

7

SW-739

CCW Hx A Cooling Water Return

SW-740

CCW Hx B Cooling Water Return

SW-741

CCW Hx B and Auxiliary Building

Return Isolation

The seven SW valves which were not replaced included: V6-12A and D, the

South and North SW Supply Header Isolation valves, respectively; V6-12B,

and C, the SW Pump Discharge Cross Connect valves; V6-16 A and B, the

North and South SW Supply to Turbine Building, respectively; and V6-16C,

the Turbine Building Cooling Water Isolation valve. The V6-12 valves were

inspected and found to be in good condition (i.e., no repair or replace

ment was necessary). The V6-16 valves were inspected, cleaned, Belzona

covered, and received new seats. Valves SW-739, -740, and -741 which were

not originally scheduled for replacement were replaced due to significant

degradation. Additionally, significant pipe erosion downstream of these

latter valves was detected. The eroded pipe was replaced. Some erosion

had been anticipated; however, the amount of degradation found was

unexpected. The system engineer plans on initiating a PM Route to inspect

this piping on a regular interval.

This is an IFI: Establishment of PM

Route To Inspect SW Piping, 90-30-02.

While the SW buried piping corrosion issue/resolution was very complex

and time consuming, the communications and interfaces between Technical

Support and NED were effective, with the Technical Support system

engineer's coordination and oversight being particularly noteworthy.

Spent Fuel Shipments

On December 4, 1990, fourteen spent fuel assemblies were transported from

the HBR site to the spent fuel storage facility at SHNPP in North

'

Carolina. Future shipments are scheduled for 1991. The shipments will

allow sufficient room in the spent fuel pool for a full core off-load.

No violations or deviations were identified.

3. Monthly Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities on

systems and components to ascertain that these activities were conducted

in accordance with license requirements. For the surveillance test-

procedures listed below, the inspectors determined that precautions and

LCOs were adhered to, the required administrative approvals and tagouts

were obtained prior to test initiation, testing was accomplished by

qualified personnel in accordance with an approved test procedure, test

instrumentation was properly calibrated, and that the tests conformed to

TS requirements. Upon test completion, the inspectors verified the

recorded test data was complete, accurate, and met TS requirements; test

8

discrepancies were properly documented and rectified; and that the

systems were properly returned to service. Specifically, the inspectors

witnessed/reviewed portions of the following test activities:

OST-401 (revision 25)

Emergency Diesels (Slow Speed Starts)

SP-1002

RHR Pump Flow Test

RHR Flow Test

On January 4, 1991, the inspectors observed performance of SP-1002, RHR

Pump Flow Test. While attempting to take flow and pressure data with the

A RHR pump operating in shutdown cooling, the flow rate appeared unstable

or oscillatory in nature. The procedure was discontinued after two sets

of data was taken. At the end of the report period the flow instability

cause(s) had not been determined and a revised test procedure was being

prepared utilizing another system configuration. The licensee plans to

perform this test and resolve the issue prior to startup. The inspectors

will review and document the resolution in IR 91-01.

No violations or deviations were identified.

4.

Monthly Maintenance Observation (62703)

)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

accordance with TS and approved procedures.

The inspectors determined

that these activities did not violate LCOs and that required redundant

components were operable. The inspectors verified that required

administrative, testing, radiological, and fire prevention controls were

adhered to. In particular, the inspectors observed/reviewed the

following maintenance activities:

90-ALYE1

Snubber 30 Bracket Repair

91-ARRSI

Adjustment of A EDG Turbocharge Exhaust Nozzle

90-AKGE1

Votes Testing of FW-V2-6A

90-AKGF1

Votes Testing of FW-V2-6B

91-AAQH1

MCC Contractor Contacts Inspection

B RHR Pump Impeller

On November 26, 1990, the inspectors witnessed the technical support

inspection of the B RHR pump impeller. The impeller was considered to be

in good condition; however there was an eroded area, less than 1 sq. cm.,

observed on one discharge vane. Repair of this area was deemed not to be

currently necessary. At the end of this reporting period, the licensee

had not determined if periodic inspections of the eroded area need to be

conducted. This an IFI:

Review Periodic Inspection Frequency

Determination For B RHR Pump Impeller, 90-30-03.

9

A EDG Operating Temperatures

The A EDG, Fairbanks Morse model 38TD81/8, has historically operated

fully loaded with the exhaust temperature approximately 100 degrees

centigrade higher than that measured on the B EDG.

Individual cylinder

exhaust temperatures have been 50 to 75 degrees centigrade hotter on A

EDG than these experienced on the corresponding B EDG cylinders. The A

EDG turbocharger air inlet check valve has not operated in a manner

similar to the B EDG valve. Normal valve operation is as follows: At

less than 80 to 90 percent of full load (2500 KW) the valve is fully

closed. This allows the inlet air to be diverted through the scavenger

air blower prior to being routed under the valve and into the

turbochargers. As the load is increased, an increasing volume of air is

drawn into the engine and exhausted through the turbocharger exhaust

turbine blades. The increasing flow increases the turbocharger speed

(i.e., the inlet pressure decreases at the turbocharger suction and below

the air inlet check valve). The differential pressure across the valve

will result in the valve modulating open as load increases. Opening of

the air inlet check valve allows air to flow directly to the

turbocharger. The air flow, being increased above the scavenger air

blower's capacity, allows the cylinders to operate at a lower temperature

than that experienced with only the scavenger air blower air flow. The B

EDG valve works in this manner; however, the A EDG air inlet check valve

remains closed and/or open less than desired as load is increased to full

load. The ability to operate the A EDG at full load with operating

temperatures similar to B EDG has been demonstrated by manual valve

operation.

Actions taken to date have not corrected the A EDG's high temperature

condition. These actions included: replacement of both turbochargers,

adjustment of the turbocharger exhaust nozzles to increase turbocharger

rpm, and inlet check valve replacement. These actions have been

developed in conjunction with, and monitored by, a Colt Industries

technical representative, On January 8, 1990, air pressure data was

recorded with the A and B EDG engines operating at various loads.

This

information along with previously submitted data was being analyzed by

the vendor for other possible corrective actions. Correction of this

higher than normal temperature condition is considered to be desirable

(i.e., would improve reliability, but is not required for the A EDG to

perform its safety function).

The inspectors have discussed the above problems and corrective actions

with both the engineering staff and the vendor representative and

observed various associated corrective maintenance as it was performed.

RHR-753B Degradation

During the performance of OST-251, RHR Component Test, on December 24,

1990, valve RHR-753B, the B RHR pump discharge check valve, did not

close.

Inspection of the valve internals revealed that the clapper arm

10

was worn and the disc travel stop was deformed. The valve is a 10-inch

Aloyco swing disc check valve. Apparently, the disc stem had become

misaligned due to the worn arm and had stuck on the gouged stop.

According to the vendor, this is a known failure mode for this valve.

The stop was weld repaired in accordance with WR/JO 90-ARZT5, the valve

was reassembled, and proper operation was verified by the successful

completion of OST-251. The worn clapper arm will be replaced when a

replacement part is received in mid-January.

This valve had been inspected on November 24, 1990, per PM-300, Aloyco

Swing Check Valve Inspection, revision 0. Though PM-300, revisions 0 and

1, steps 7.2.1 and 7.3.10.1 required inspection and documentation of the

general condition of the valve body, no specific steps were provided to

address the travel stop. Though deformation of the travel stop was

observed on November 24, 1990, it was not documented on Attachment 8.4 of

PM-300. Failure to specifically require the condition of the stop to be

documented so that degradation can be detected is considered a VIO:

Procedure PM-300 Was Inadequate In That Condition of The Aloyco Check

Valve Travel Stop Was Not specifically Required To Be Evaluated and

Documented, 90-30-04.

The inspectors are concerned that the maintenance procedure upgrade

program failed to incorporate specific steps in the inspection procedure

to address a known failure mode.

One violation was identified.

5.

Refueling Activities (60710)

Movement of fuel into the reactor vessel was initiated on December 25 and

completed on December 29, 1990. The inspectors observed 12 fuel

assemblies being loaded on December 28. The inspectors verified that

activities were being conducted in accordance with FMP-019, Fuel and

Insert Shuffle and GP-010, Refueling. During refueling activities, the

inspectors verified that the requirements of TS 3.8.1 c, 3.8.1.d, 3.8.1.e,

3.8.1.g, 3.8.1.h, and 3.8.2.d were being met. On December 27 the

inspectors observed that refueling activities were suspended in accordance

with TS 3.8.2.d when the relative humidity of the air processed by the

refueling filter systems approached 70 percent. Fuel movement resumed

when the relative humidity decreased to less than 70 percent. Later that

night and the next day, fuel movement had to be suspended on two additional

occasions due to relative humidity restrictions. The condition was caused

by a combination of faulty duct heaters and rain and fog in the area.

Inspection Report 90-22 documented that cleanliness controls in the

reactor cavity area at the start of control rod unlatching was poor. The

inspectors observed that housekeeping was being maintained at an acceptable

level during fuel reloading.

6. Action on Previous Inspection Findings (92700, 92701, 92702, 71707)

Upper Internals Repair

During the September 1990 reactor vessel upper internals inspection, the

licensee observed crack indications in 38 control rod guide tube support

pins (split pins) and 13 guide tube removable inserts with less than the

necessary number of flexures.

See IR 90-22 and 90-24 for additional

description of these problems.

By December 12, 1990, the licensee had completed replacement of split

pins on all 53 guide tubes with a redesigned split pin. The replacement

split pins received a higher temperature heat treatment and have a larger

shank to collar radius than the original supplied split pins. The heat

treatment makes the material less susceptible to IGSCC and the radius

increase reduces the stresses at a location where IGSCC had occurred in

the previous designed type of split pins.

By December 12, 1990,

flexureless inserts had also been installed on the guide tubes such that

all 45 guide tubes which had removable inserts earlier now have flexureless

inserts. Eight guide tubes of the total 53 guide tubes did not have

flexures. These eight guides tubes were used previously with the no

longer installed partial length control rods. Based upon the

repair/replacement activities, the split pin and flexure failure issues

have been satisfactorily addressed.

S/G Girth Weld 5 ID Indications

Inspection Report 90-24 documented that preliminary in-process external UT

examination of A S/G weld 5 (upper girth weld) resulted in detection of

low amplitude ultrasonic reflectors at the vessel ID which ran circumfer

entially in the base metal adjacent to the wall edge. Subsequently,

indications have been found in the same general area of C S/G. Ultrasonic

examinations had previously recorded isolated indications on the B S/G

upper girth weld. The B S/G indications were not considered to be indica

tive of cracks. After reviewing available information, the licensee

decided to perform internal ID magnetic particle examination of the A S/G

weld 5. The A S/G was selected because its external UT examination had

been completed (i.e., C S/G was still being examined) and A S/G was more

readily accessible than C S/G due to outage activities in and around the

S/Gs.

Visual examination of the A S/G weld from the inside revealed no

indication of cracks. The visual inspection also revealed that the weld

on the inside was much wider, 3 to 4 inches in width, than shown on the

drawing. Thus, the UT indications were all in the weld area, not in the

base metal as originally thought. Ten linear feet of the weld,

encompassing the worst UT indications, was selected for fluorescent MT.

This confirmed that surface indications were present in the weld, and not

in the base metal.

Two indications were surface prepared before the MT.

These indications were found to be associated with weld porosity.

Preliminary analysis of the A and C S/G UT results by Structural Integrity

12

Associates indicates that it is acceptable to operate at least one cycle.

The UT and MT results were discussed with Region II and NRR personnel via

a conference call on December 14, 1990. The NRC has tentatively concurred

with the licensee's approach (i.e., it is acceptable to operate one cycle

without removing the indications). The licensee has agreed to submit to

NRR for further review the UT and MT examination results and the associated

engineering analysis prior to startup. In addition, the licensee indicated

a.willingness to perform external UT examinations of the affected S/G

areas should a forced outage of sufficient duration put the unit in cold

shutdown after mid-cycle. Such an examination would determine if the

character of the existing indications had changed. The licensee currently

plans to re-examine these indications during the next refueling outage,

scheduled for March 1992.

On December 18, 1990, the inspectors visually

inspected an accessible portion of the A S/G welds from the secondary

side. Comparison of the observed conditions with those depicted in

pictures from another site that had pitting which resulted in rapidly

propagating cracks, showed that such pitting did not exist in the area

viewed. These pictures were also viewed by the cognizant engineer who had

looked at the entire A S/G weld 5 area. The engineer also indicated that

pitting as shown in the other site's pictures did not occur in the A S/G.

On December 18, 1990, while removing work platforms from inside A S/G, an

internal ladder rung broke at its attachment weld and fell into the

annulus area. Subsequent underwater TV camera inspection located the

broken rung and the part was retrieved. Magnetic particle testing of the

other ladder rungs' attachment welds revealed no other defects.

The communications and interfaces among the groups (NED, HEEC and Technical

Support) involved in the resolution of the S/G indications were effective.

The support provided to the site by the offsite organizations was

especially noteworthy.

(Closed) VIO 89-18-01, 10 CFR 50 Appendix B Criterion XVI Failure To

Promptly Identify And Correct Conditions Associated With the AFW System

Potential Escalated.

Inspection Report 89-18 transmittal letter

identified that the subject item was under consideration for escalated

enforcement action and accordingly no NOV was being issued at that time.

On November 15, 1989, the NOV was issued with a proposed imposition of

civil penalty. Inspection of this item is being conducted under item

number 89-11-01. Thus, for administrative purposes, violation 89-18-01 is

considered closed.

No violations or deviations were identified.

13

7. Exit Interview (30703)

The inspection scope and findings were summarized on January 15, 1991,

with those persons indicated in paragraph 1. The inspectors described

the areas inspected and discussed in detail the inspection findings

listed below and in the summary. Dissenting comments were not received

from the licensee. Proprietary information is not contained in this

report.

Item Number

Description/Reference Paragraph

90-30-01

IFI - Review Steps To Detect And/Or

Preclude Extensive External Corrosion

Of Carbon Steel Piping, paragraph 2.

90-30-02

IFI - Establishment Of PM Route To

Inspect SW Piping, paragraph 2.

90-30-03

IFI - Review Periodic Inspection

Frequency Determination For B RHR Pump

Impeller, paragraph 4.

90-30-04

VIO - Procedure PM-300 Was Inadequate

In That Condition Of The Aloyco Check

Valve Travel Stop Was Not Specifically

Required To Be Evaluated And

Documented, paragraph 4.

8. List of Acronyms and Initialisms

AFW

Auxiliary Feedwater

ANSI

American National Standards Institute

ASME

American Society of Mechanical Engineers

AWWA

American Water Works Association

CC

Component Cooling

CCW

Component Cooling Water

CFR

Code of Federal Regulations

cu. ft.

Cubic Feet

e.g.

For Example

ECCS

Emergency Core Cooling System

E & RC

Environmental and Radiation Control

EDG

Emergency Diesel Generator

EE

Engineering Evaluation

EQ

Environmental Qualification

FMP

Fuel Management Procedure

GL

Generic Letter

GP

General Procedure

HEEC

Harris Energy and Environmental Center

HVH

Heating, Ventilation Handling

14

I&C

Instrumentation & Control

ID

Inside Diameter

IFI

Inspector Followup Item

IGSCC

Intergranular Stress Corrosion Cracking

IR

Inspection Report

JCO

Justification For Continued Operation

KW

Kilowatt

LCO

Limiting Condition for Operation

MCC

Motor Control Center

MDAFW

Motor Driven Auxiliary Feed Water

MT

Magnetic Particle Testing

NED

Nuclear Engineering Department

NI

Nuclear Instrumentation

NOV

Notice of Violation

NRR

Nuclear Reactor Regulation

OD

Outside Diameter

OST

Operations Surveillance Test

PM

Preventative Maintenance

PNSC

Plant Nuclear Safety Committee

REM

Roentgen Equivalent Man

RHR

Residual Heat Removal

RNP

Robinson Nuclear Project

rpm

Revolutions Per Minute

RO

Refueling Outage

RW

Radwaste

SDAFW

System Driven Auxiliary Feedwater

S/G .

Steam Generator

SHNPP

Shearon Harris Nuclear Power Plant

SP

Special Procedure

Sq. Ft.

Square Feet

Sq. Cm.

Square Centimeters

SWBP

Service Water Booster Pump

SW

Service Water

TS

Technical Specification

TSC

Technical Support Center

TV

Television

URI

Unresolved Item

UT

Ultrasonic Test

VIO

Violation

WR/JO

Work Request/Job Order

YTD

Year To Date