ML14178A054

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Insp Rept 50-261/90-22 on 900911-1010.Violations Noted.Major Areas Inspected:Operational Safety Verification,Surveillance Observation,Maint Observation,Onsite Followup of Events, Written Repts of Nonroutine Events
ML14178A054
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 11/07/1990
From: Carroll R, Garner L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A052 List:
References
50-261-90-22, NUDOCS 9011160172
Download: ML14178A054 (16)


See also: IR 05000261/1990022

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/90-22

Licensee: Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.:

DPR-23

Facility Name: H. B. Robinson

Inspection Conducted:

September 11 - October 10, 1990

Lead Inspector:

fLAe.I'

/ /

L.'W. Garner, Senior Resident Inspector

D te S gne

Other Inspector: K. R. Jury

Approved by:____

. E. Carroll, Acting Section

ief

atE Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation, onsite

followup of events, written reports of nonroutine events,

and action on

previous inspection findings.

Results:

Release of Freon R-22 gas into a vital area resulted in an Alert declaration.

Incorrect determination that the affected area was a protected area resulted in

improper initial event classification as an Unusual Event. Based upon previous

inspection.findings, the improper classification was a violation for failing to

correct an exercise weakness as required by 10 CFR 50, Appendix E (paragraph 5).

Two examples of a violation for failure to properly implement procedures were

identified.

One example involved valve mispositioning which resulted in

draining 8,000 gallons of spent fuel pool water to the containment sump. The

.other

example was the discovery that the primary air and back-up nitrogen

supplies to the cavity seal were isolated after vessel defueling with the

cavity still flooded (paragraph 2).

9011160172 901107

PDR ADOCK 05000261

G

PNU

2

A non-cited violation was identified for failure to implement a procedure, in

that, the state and county emergency operation centers were not contacted when

a Unusual Event notification was made to the warning points (paragraph 5).

A temporary waiver of compliance was granted October 5, 1990, for a one-time

change to Technical Specification 3.5.3.3.

The waiver allowed reactor

containment vessel purging without operable effluent radiation monitors when

containment integrity is not required and there is no fuel in-containment

(paragraph 2).

All 106 guide tube support pins will be replaced this outage as a result of

ultrasonic inspections which identified 38 pins with intergranular stress

corrosion crack indications (paragraph 3).

At least thirteen flexureless guide tube inserts will be installed in locations

which have less than two intact flexures (paragraph 3).

A safety injection pump test into three cold legs resulted in flow rates for

which net positive suction head requirements were not specified (paragraph 7).

Frequent management tours and emphasis on housekeeping have generally resulted

in maintaining housekeeping at an acceptable or above level during the outage.

.

An exception was the reactor cavity area cleanliness during control rod

unlatching commencement(paragraph 2).

Periodic Onsite Nuclear Safety Section distribution of relevant operating

experience feedback reminders prior to significant evolutions was noteworthy

(paragraph 2).

REPORT DETAILS

1. Persons Contacted

  • R. Barnett, Manager, Outages and Modifications

C. Baucom, Shift Outage Manager, Outages and Modifications

J. Benjamin, Shift Outage Manager, Outages and Modifications

C. Bethea, Manager, Training

  • S. Billings, Technical Aide, Regulatory Compliance
  • R. Chambers, Manager, Operations

D. Crook, Senior Specialist, Regulatory Compliance

  • J. Curley, Manager, Environmental and Radiation Control

C. Dietz, Manager, Robinson Nuclear Project

D. Dixon, Manager, Control and Administration

J. Eaddy, Supervisor, Environmental and Radiation Support

S. Farmer, Supervisor - Programs, Technical Support

R. Femal, Shift Foreman, Operations

  • E. Harris, Manager, Onsite Nuclear Safety

J. Kloosterman, Director, Regulatory Compliance

D. Knight, Shift Foreman, Operations

E. Lee, Shift Outage Manager, Outages and Modifications

A. McCauley, Supervisor -

Electrical Systems, Technical Support

R. Moore, Shift Foreman, Operations

R. Morgan, Assistant to the Manager, Robinson Nuclear Project

D. Nelson, Shift Outage Manager, Outages and Modifications

  • M. Page, Manager, Technical Support

D. Quick, Manager, Plant Support

D. Seagle, Shift Foreman, Operations

  • J. Sheppard, Plant General Manager
  • R. Smith, Manager, Maintenance

R. Steele, Shift Foreman, Operations

D. Winters, Shift Foreman, Operations

  • H. Young, Director, Quality Ass-urance/Quality Control

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and office personnel.

  • Attended exit interview on October 18, 1990.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the facility

was being operated safely and in conformance with regulatory requirements.

These activities were confirmed by direct observation, facility tours,

interviews and discussions with licensee personnel and management,

verification of safety system status, and review of facility records.

2

To verify equipment operability and compliance with TS,

the inspectors

reviewed shift logs, Operation's records, data sheets, instrument traces,

and records of equipment malfunctions.

Through work observations and

discussions with Operations staff members,

the inspectors verified the

staff was knowledgeable of plant conditions, responded properly to alarms,

adhered to procedures and applicable administrative controls, cognizant of

in-process surveillance

and maintenance activities,

and aware

of

inoperable equipment status.

The inspectors performed channel

verifications and reviewed component status and safety-related parameters

to verify conformance with TS.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment,

and to

verify that radiological controls, fire protection controls, physical

protection controls,

and equipment tagging procedures were properly

implemented.

Temporary Waiver of Compliance

On October 5, 1990, the licensee .requested an emergency TS amendment and

Temporary Waiver of Compliance from the requirements of TS 3.5.3.3, Table

3.5-7, items 3.a and 3.b required action b.

The waiver request was

verbally granted the same day and subsequently confirmed by letter dated

October 9, 1990.

The waiver was to remain into effect until emergency TS

amendment processing was completed.

The emergency TS amendment was

subsequently issued on October 16, 1990, as amendment no. 130. The waiver

and the amendment authorized purging of the CV without effluent radiation

monitors RMS-11, RMS-12, RM-14 and RMS-34 operable. This was a one time

change for refueling outage 13, applicable only when fuel is not in the CV

and

CV integrity is not required.

Additionally,

CV atmosphere grab

samples are to be taken once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and analyzed for radionoble

gases within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Containment purging during outages is desirable to maintain safe personnel

working conditions.

The need for the waiver and emergency TS change

resulted from the simultaneous installation of two modifications: M-1005,

Upgrade Plant Vent Radiation Monitoring and Stack Flow Monitor,

and

M-1049, Radiation Monitoring System Upgrade. The latter modification was

initiated in the third quarter of 1989 by a system team to improve the

overall system reliability.

In either March or April 1990, engineering

identified that CV purging would not be allowed by TS 3.5.3.3, Table

3.5-7, item 3.a and 3.b required action b, if

RMS-11,

12,

14, and 34 were

simultaneously removed from service.

As

a result of an interdepartmental

miscommunication,

engineering

proceeded with development of M-1049 in conjunction with M-1005 such that

these monitors would be simultaneously inoperable without initiating

actions to obtain relief. On July 31, 1990, this oversight was discovered

and discussed by the PNSC. Alternate installation options to maintain at

least one of the monitors in service were reviewed; however, they were not

considered feasible due to the relatively short time available to perform

3

necessary major changes in the modification packages.

If an appropriate

TS change request had been promptly submitted subsequent to initial issue

identification, a waiver and emergency TS amendment would not have been

required.

Prior to October 5, 1990,

NRR recognized that the replacement high range

noble gas effluent monitor had a maximum detection range one decade less

than the existing monitor. The existing monitor met the maximum detection

range (100,000 microcuries per cubic centimeter) required by the March 14,

1983 order confirming licensee commitments on post-TMI related issues.

The required maximum range was specified in NUREG-0737,

item II.F.1-1.

Subsequently,

the licensee revised the modification to increase the

maximum detection range for the replacement monitor to be in compliance

with the above order.

Based upon commitments to RG-1.97, Instrumentation

For Light-Water-Cooled Nuclear Power Plants To Assess Plant And Environs

Conditions During and Following An Accident, revision 3, the licensee had

improperly determined that item I.F.1-1 was no longer applicable. At the

end of the report period, the licensee was reviewing if similar problems

exist with other modifications.

This is an URI:

Review If TMI Item

Commitments

Have Been Improperly Superseded by RG-1.97 Commitments,

90-22-01.

Inadvertent Draining Of SFP Water

On September 22, 1990, during performance of GP-009, Filling,

Purification,

and Draining of the Refueling Cavity, revision 9, an

operator inadvertently opened valve WD-1757C,

which is the lower cavity

drain to the CV sump.

As a result, approximately 8,000 gallons of SFP

water was subsequently discharged into the CV sump.

This procedure was

being performed in preparation for performance of EST-030,

Fuel Handling

Equipment Interlock and Operation Test, and prior to initial cavity fill.

Valve WD-1757C is located in the excess letdown heat exchanger room which

is a locked high radiation area, and is covered with lead blanketing for

shielding purposes.

Valve operation is by means of a reach rod through

the room's door and the valve is reverse acting (i.e., clockwise to open),

which is a different operation than almost all valves at HBR.

Valve

WD-1757C is a ball valve with movement limited by mechanical stops.

This valve mispositioning was discovered on September 23,

1990, when an

increase in CV sump level was noticed on the RTGB after the SFP gate valve

was opened; operations then verified the sump level increase in the CV.

The SFP gate valve was subsequently closed and WD-1757C was discovered

open.

Valve WD-1757C was then closed and CV sump level stabilized.

SCR 90-071 was initiated to document this event and determine root cause,

including performance of an HPES evaluation. Failure to correctly operate

valve WD-1757C as required by GP-009 was

identified as a violation:

Failure To Adequately Implement Procedures As Required By TS, 90-22-02.

4

Pneumaseal Supply Air Isolation

On October 8, 1990, during routine CV inspections, operations personnel

discovered both the primary air and back-up nitrogen gas supplies isolated

to the pneumaseal while the cavity was flooded. The pneumaseal provides

the inflatable seal between the reactor vessel flange and the reactor

cavity.

The seal, which prevents leakage of refueling water from the

cavity, was installed per WR/JO 90-AEJI1 on September 22,

1990,

in

preparation for flooding the cavity for refueling operations. Based on a

review of Combustion Engineering's Field Activities Log,

adequate air

supply to the seal was verified as late as October 2, 1990 (i.e.,

subsequent to the vessel being defueled).

The licensee initiated SCR 90-077 to document the incident and determine

root cause.

Maintenance Refueling Procedure MRP-001, Pneumaseal

Installation and Removal,

revision 3, Step 7.2.9, required that the

instrument air and nitrogen supply valves be wired open and a warning sign

be provided so that air and the nitrogen supplies would not be interrupted

while the pneumasel was in service.

Evidently, at some time between

October 2 and 8, 1990, the supply valves were closed, resulting in the

isolation of supply air and nitrogen.

Per MRP-001, prior to pneumaseal

installation, the seal is to be inflated and leak checked with

verification that the seal maintains pressure for fifteen minutes with the

supply air and nitrogen isolated.

There are check valves installed

downstream of the manual

supply valves to prevent back-leakage.

Additionally, in 1984 and 1985,

pnemaseal tests were conducted to ensure

the seal could not be physically maneuvered through an opening equivalent

to the size of the opening between the vessel flange and cavity with the

cavity flooded. This testing was conducted in response to IEB 84-03 which

was generated as a result of the pneumaseal failure at Haddam Neck.

The

testing demonstrated that the seal would not fail even if it was deflated.

As such, even with seal air and nitrogen supplies isolated, seal failure

was not expected and did not occur.

However, failure to maintain the

instrument and nitrogen supply valves open as required is considered

another example of violation 90-22-02.

During review of MRP-001,

the inspectors noted that there are no

procedural sign-offs nor were acceptance criteria provided within the

procedure to document acceptable pneumaseal pre-installation testing and

installation. Procedure MRP-001 was revised in August 1990 as part of the

Maintenance Procedure Upgrade Program. Based on the fact that neither the

procedure nor the WR contained sign-offs verifying certain steps within

the procedure were adequately performed,

it

was difficult to ascertain

that seal testing and installation was completely performed as specified.

This lack of acceptance criteria and verification sign-offs was considered

a procedural weakness.

Vital Power Availability During Refueling

The inspectors verified that from the time the reactor was shut down on

September 8, 1990, until all fuel was removed from the reactor vessel,

both.RHR pumps and associated heat exchangers were operable with the vital

busses energized from the SAT. During this period, at least one EDG was

5

maintained available.

During the majority of this period, both EDGs and

the dedicated shutdown DG were available.

In addition,

two SI pumps,

though de-energized per TS, were available for service. It was noted that

the licensee has conservatively elected to schedule fuel loading with both

emergency busses operable, even though it is allowable to load fuel with

only one emergency bus available.

Midloop/Reduced Inventory

All work activities which would require reduced inventory operations was

scheduled to be performed with the reactor vessel defueled (i.e., reduced

inventory operation was not scheduled during refueling outage 13).

As a

result, the licensee had no need to review their controls or administra

tive procedures governing reduced inventory operation. However, in case

reduced inventory operation becomes necessary during the outage, the

inspectors verified that procedures were available which adequately

address items 3.a through 3.f listed in TI 2515/101, Loss of Decay Heat

Removal (Generic Letter No.88-17). 10 CFR 50.54(F).

Specifically, the

inspectors verified that the current revisions of GP-008, Draining the

Reactor Coolant.System, revision 20, and OMM-030, Control of CV Penetra

tions During Mid-Loop Operation,

revision 1, contained the proper

precautions and instructions. A similar inspection was documented in IR

89-08.

The inspectors discussed with the licensee that contingency plans

had not been established to repower vital busses from an alternate source

if the primary source were lost during reduced inventory operations. If

reduced inventory operation becomes necessary, the inspectors will review

the proposed plant configuration and discuss with the licensee the need,

if any, for power restoration contingency plans.

Outage Status

At the end of the inspection period, the outage was on schedule with

modification M-994, Control Room Habitability, the critical path activity,

as was anticipated. Obtaining sufficient Q-list fasteners and refrigerant

tubing for M-994 continued to be a challenge.

Reactor defueling was

completed on October 1, 1990.

Fuel reload is scheduled to begin on

November 8, 1990 (i.e., subsequent to the scheduled completion of S/G eddy

current testing and restoration of both E-1 and E-2 emergency busses to

service).

Organizational Changes

On September 24, 1990, Mr. J. J. Sheppard, Manager - Operations, replaced

Mr.

R. E. Morgan as the Plant General Manager.

Mr. R. H. Chambers,

Technical Support Supervisor - Plant Performance, was promoted to

Manager - Operations. Mr. R. E. Morgan has accepted a position as Manager

-

Nuclear Assessment, Harris Nuclear Project.

6

OEF Activities

Inspection Report 90-11 documented that prior to the May 1990 transformer

upgrade outage, ONS conducted a pre-outage, Focus on Safety meeting. The

meeting centered on review of the defined work scope and potential safety

concerns based upon OEF reports.

Prior to refueling outage 13,

ONS

sponsored a similar meeting,

and has periodically issued OEF reminders

prior to significant evolutions.

For example, on October 10, 1990, OEF

reminder #4 was issued prior to SW system, turbine, S/G sludge lancing,

and S/G eddy current test work. This reminder included descriptions of:

foreign objects in S/Gs (IEN 88-06); main turbine blade damage caused by

foreign objects left in turbines (SER 86-07); loss of reactor coolant

inventory while in a shutdown condition (IEN 90-55); release of slightly

contaminated material offsite (POER 87-17); and a HPES report involving

consequences of using unclear procedures.

This effort is considered

noteworthy, in that it emphasized management's commitment to learning from

industry experiences such that similar problems are avoided.

Management Tours

Plant management, including unit managers and shift outage managers, have

made frequent tours of the facility, including the CV,

since refueling

outage initiation. This effort has resulted in high management visibility

at job sites and housekeeping has been generally maintained at or above

acceptable levels.

One exception was the reactor cavity area cleanliness

at the start of control rod unlatching. The inspector noted rubber gloves

and a partially torn step-off pad with duct tape within the roped off area

around the cavity. Cloth towels and a roll of duct tape were observed on

the refueling bridge without being secured. The inspector also observed

that items such as tools were being passed in and out of the area without

any apparent accountability.

At the time the inspector made these

observations, a unit manager also observed similar poor conditions and

directed that these conditions be corrected prior to resuming work.

Subsequently, work in the refueling cavity was again discontinued until

the exclusion area was more clearly delineated and additional work and

tool controls were established.

This item was discussed with the

Operations Manager.

One violation, with two examples, was identified.

3. Monthly Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities on

systems and components to ascertain that these activities were conducted

in accordance with license requirements.

For the surveillance test

procedures listed below, the inspectors determined that precautions and

LCOs were adhered to, the required administrative approvals and tagouts

were obtained prior to test initiation, testing was accomplished by

qualified personnel in accordance with an approved test procedure, test

instrumentation was properly calibrated, and the tests were completed at

the required frequency. Upon test completion, the inspectors verified the

recorded test data was complete, accurate, and test discrepancies were

7

properly

documented

and rectified.

Specifically, the inspectors

witnessed/reviewed portions of the following test activities:

SP-386

Safety Injection Hydrostatic Test

SP-938

Safety Injection Pumps Cold Leg Runout Test

Upper Internals Inspection

As a result of the reactor vessel internals inspection, issues have been

identified concerning IGSCC in control rod guide tube flexures and support

pins (i.e., split pins).

The split pins are utilized to provide attachment

of and lateral support for the guide tubes at the upper core plate.

Each

of the 53 guide tubes contains two split pins for a total of 106 pins.

Split pins have experienced IGSCC and resultant failures in the shank to

collar and/or leaf area. This issue was identified by Westinghouse in the

early 1980's as a domestic industry concern for split pins with certai.n

heat treatments.

In March 1989,

the licensee experienced a split pin

failure (failure location other than those described above, see IR 89-08)

and subsequently shut the plant down to retrieve the loose part from S/G

C. During September 1990, as a result of this failure and recommendations

from Westinghouse, the licensee performed UT on all 106 split pins.

The

results revealed 38 split pins with crack indications; 37 pins had only

shank crack indications, one pin had a leaf crack indication only, and one

of the 37 pins with a shank crack indication also had a leaf crack

indication.

Subsequent to the report period, the licensee conservatively

decided to replace all 106 split pins during the present refueling outage.

This adequately addresses IFI 89-08-02, Review Long Term Resolution Of

Split Pin Cracking Issue. Hence, item 89-08-02 is considered closed.

The control rod guide tube flexure issue, also a previously identified

generic industry problem,

involved cracking and resultant flexure

failures. There are four flexures on each guide tube which contain the

removable inserts on the top end of the upper guide tubes.

The removable

insert provides a flow restriction to minimize bypass flow from the outlet

plenum to the upper head plenum and simultaneously provides guidance for

the drive rod.

As a result of the flexure inspection, the licensee

determined that there were 13 guide tubes which currently require a

flexureless insert (i.e., had one or no sound flexures remaining).

The

flexureless insert was developed by Westinghouse to replace the inserts

previously contained by flexures.

There were 19 guide tubes with two

remaining flexures, the minimum number of flexures needed for insert

restraint. The licensee plans to have a minimum of 34 flexureless inserts

available for installation; however, the licensee is evaluating if,

and

how many, additional flexureless inserts will be installed other than the

required 13.

The results of this evaluation will be documented in

IR 90-23.

No violations or deviations were identified.

8

4. Monthly Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

accordance with TS,

approved procedures, and appropriate industry codes

and standards.

The inspectors determined that these activities did not

violate LCOs and that required redundant components were operable.

In

particular, the inspectors observed/reviewed portions of the following

maintenance activity:

WR/JO 90BCC435

Perform Annual PMs on A EDG

EDG PM

During

PM activities on the A EDG,

the following conditions were

identified: two piston heads had locations where the chromium clading was

burned through; one of the above pistons had the lower oil scraper ring

cracked; and both turbocharger nozzle rings were cracked.

The two lower

pistons had been selected-for inspection based upon their cylinder exhaust

temperatures being at the high end of the acceptance range.

Based upon

the inspection results, two additional lower pistons were removed for

inspections.

These cylinders had also tended to operate at

slightly

higher than average temperatures.

No damage was observed on these piston

heads.

The later two pistons were re-installed and the two damaged

pistons were replaced. The upper pistons in the above mentioned cylinders

were also examined for burn locations; none were observed.

This was

expected,

as the upper pistons operate at lower temperatures than the

lower pistons due to the way fuel is injected into the cylinders.

Both turbochargers were replaced.

The inspectors examined the cracked

nozzle rings.

Each nozzle ring had one crack at approximately the same

location.

The Colt Industries'

technical representative indicated that

this has been a problem on Fairbanks Morse Model 38 TD 8 1/8 engines.

Such cracks are not anticipated to affect the performance of the

turbocharger unless:

(1) another crack would occur and a piece of the

nozzle ring were to break off, or (2) the crack would propagate into the

turbocharger housing.

Neither failure mechanism appeared likely since

there was no evidence of additional cracks and crack propagation into the

housing was not considered feasible as the nozzle ring was bolted to the

housing.

No violations or deviations were identified.

5. Onsite Followup of Events (93702)

On September 11, 1990, at 8:50 a.m., the control room was notified of a

Freon leak/tube rupture in the control room HVAC equipment room which is

located immediately below the main control room.

The shift foreman

directed that the area be evacuated and that control room ventilation be

secured. All personnel who had been in the area were verified to have

exited the area and no injuries occurred.

The freon release lasted for

9

approximately one minute (i.e., the time it

took the HVA unit to

discharge). The area was then secured and preparations for temporary HVAC

equipment room ventilation were initiated. At 9:10 a.m., after review of

the EAL flow chart, the shift foreman declared an unusual event due to a

toxic gas release into the protected area.

Upon hearing the subsequent PA announcement, the inspector went to the

control room. At that time, approximately 9:20 a.m., preparations were in

progress to make the required emergency notifications. At 9:22 a.m., the

emergency communicator notified the State of South Carolina, Darlington

County, Lee County, and Chesterfield County warning points of the UE. At

9:36 a.m.,

the NRC was notified in accordance with 10 CFR 50.72.

At

approximately 9:40 a.m., while reviewing the EAL flow chart, the inspector

questioned the Operations Manager as to the affected area's proper

security classification.

The inspector was informed that based upon a

similar question from an SRO, security was verifying the area's security

classification.

At 9:46 a.m.,

a security supervisor indicated that the

area was not listed in the security plan as a vital area; however, it was

within security doors bounding the auxiliary building and should therefore

be considered a vital area.

Based upon this information,

the SEC

reclassified the event as an Alert (i.e., toxic gas release into a vital

area).

The emergency communicator then notified state and county EOCs of

the reclassification. The TSC was incorporated into the protected area at

10:08 a.m..

At 10:13 a.m., after approximately one-half hour of room

ventilation, initial remote Freon sampling detected 0.5 ppm Freon in the

HVAC equipment room.

At 10:14 a.m.,

the OSC was fully manned and

activated.

At 10:21 a.m.,

the control room was notified that local

sampling results indicated that oxygen levels were 20.8 -

21.0 percent and

Freon levels were 1.9 ppm.

The TLV for Freon is 1000 ppm. Based upon

this information, the SEC terminated the Alert at 10:21 a.m. The TSC had

been fully manned and was prepared to activate when the Alert was

cancelled.

The licensee's review of the event and associated response was documented

in SCR 90-069.

The event was initiated when a worker inadvertently cut a

Freon line to the operating control room heating and air conditioning unit

HVA-2.

The worker had been instructed to cut four empty Freon lines

associated with HVA-1 as part of M-994, Control Room Habitability.

The

worker had made several cuts on two of the lines, was transferred

temporarily to another task, then resumed the Freon line cutting. Prior

to work resumption, another employee pulled one of the cut lines through a

wall penetration. Upon resumption of work, the worker thought he had only

cut one line and continued to cut three more lines.

The fifth line (which

he thought was the fourth) was the HVA-2 charged Freon line that was

adjacent to the HVA-1 empty Freon lines.

The SCR also identified several concerns/weaknesses.

The shift foreman

had to determine whether the gas was toxic and if so, whether or not the

affected area was a protected or vital area. Without adequate procedural

guidance available to define what gases onsite are toxic, he conserva

tively assumed that Freon R-22 was toxic. Additionally, after consulting

10

the security plan, which did not provide a clear definition of the

affected area's status as a vital or protected area, as well as consulting

with other individuals who were also unsure of the area's classification,

he decided that the area was only in the protected area.

As discussed

above, this decision was later determined to be incorrect.

The shift

foreman stated that to his knowledge the equipment in the room was not

considered vital equipment and that much of the equipment in the room was

in the process of being dismantled per modification M-994. Hence, lacking

definitive guidance from the security plan, the shift foreman determined

that the area was not a vital area.

Though this specific event had

minimal safety significance as the total refrigerant quantity released was

small,

it

did highlight a fundamental

weakness in emergency plan

implementation (i.e., guidance and training on EAL flowchart specific

decision blocks have been inadequate).

Previous inspection findings

concerning emergency classification problems are contained in IRs 88-07,

88-16, and 89-27. Specifically, IR 89-27 identified the shift foreman's

failure to recognize the occurrence of an initiating condition for an UE

as an exercise weakness.

Though the drill's artificiality was a major

contributor to this weakness, as discussed in IR 89-27, the identification

of this item as an exercise weakness underscored the concern that

previously identified problems in this area were not completely corrected.

The September 11,

1990 event indicated that proper emergency classifica

tions, especially for non-FSAR Chapter 15 events, continue to be a

weakness.

The failure to correct an exercise weakness identified in IR

89-27 is a violation of 10 CFR 50 Appendix E Section IV.F.5: Failure To

Correct An Exercise Weakness Concerning Event Classification, 90-22-03.

The SCR also discussed the emergency communicator identifying that he did

not correctly dial the automatic ringdown circuit to simultaneously

contact both the state and county warning points and EOCs when the NOUE

was made. The failure to properly notify state and county EOCs of the UE

as required per PEP-171,

step 5.2.1.1 is a violation.

This violation

meets the criteria specified in Section V.G.1 of the NRC Enforcement

Policy for not issuing a Notice of Violation and is not cited.

The

violation is identified as a NCV:

Failure To Implement Procedure PEP 171,

90-22-04.

Additionally, the SCR also identified that manning of the OSC and TSC

occurred without problems. This was significant in that augmentation has

been identified as a weakness in previous emergency exercises.

Specifi

cally, the new beeper notification method for ERO personnel worked well.

Although this cannot be considered a demonstration of the licensee's

augmentation ability during. nights and weekends,

ERO beeper tests

conducted on weekends and in the evening have indicated that both the OSC

and TSC could be activated within procedural guidelines during off-normal

hours.

Two violations, one being non-cited, were identified.

6. Onsite Followup of Written Reports of Nonroutine Events (92700)

(Closed)

LER 89-10,

Inadequate Auxiliary Feedwater Pump Net Positive

Suction Head.

This issue was discussed in IR 89-17, 89-18, 89-20, 89-23,

and 89-32.

Inspector Followup item 89-32-01 was established to review

acceptance test ST-2 for modification M-1018, Auxiliary Feedwater -

NPSH.

The inspectors reviewed the acceptance test performed on December 27,

1989.

The test successfully demonstrated that the modified AFW suction

piping was adequately sized with sufficient NPSH available to allow

simultaneous operation of all three AFW pumps.

(Closed)

LER 89-14,

Loading of Safety-Related Equipment Could Exceed

Assumptions Of Accident Analysis.

This issue was discussed in IR 89-25,

89-31, and 89-32.

The inspectors verified that Agastat digital timing

relays were installed as committed in the LER.

However, the hardware

installation did not completely resolve the concern involving potential

emergency bus overloading during accident load sequencing. Specifically,

under certain grid conditions, sequencing with offsite power available

could result in undesirable emergency buss undervoltages.

This concern

was addressed by the placement of: administrative controls on the VAR

sharing between the coal fired unit (unit-1) and the nuclear unit

(unit-2); restrictions on switchyard capacitor bank usage; and procedural

controls requiring certain loads be in service so they do not have to

sequence onto the their respective emergency buss.

Periodically during

the last cycle, the inspectors verified that these items were being

implemented.

Modification M-1043, Modification of Degraded Grid Voltage

Relay Logic, is scheduled for installation this outage to address this

concern.

(Closed)

LER

90-02,

Reactor Trip During

Performance of Nuclear

Instrumentation Surveillance Test And VIO 90-02-02, Failure To Follow

Procedure OST-007 Resulted In Reactor Trip. In the April 9, 1990 response

to the NOV,

the licensee committed to make changes to OST-007 to help

ensure procedure format will not contribute to personnel error.

Revision

5 to OST-007 was issued on May 7, 1990, with an improved format. A review

of other OSTs identified that similar procedure format weaknesses existed

in OST-001 through OST-006. The inspectors verified that these procedures

were reformatted as committed in a May 10,

1990 supplemental response to

the NOV. Subsequently, OST-009 was similarly formatted in September 1990,

to provide consistent formats among OST procedures.

(Closed) LER 90-05, Failure To Test RPS Logic Channels In Accordance With

Technical Specifications. On May 3, 1990, a telephone conference was held

between Region II

management

and the licensee concerning RPS logic

testing. By letter dated May 11, 1990, the licensee confirmed four verbal

commitments. The inspectors verified that these four items were completed

as committed.

Corrective actions to ensure similar logic testing

deficiencies do not exist will be inspected as part of violation 90-11-01.

No violations or deviations were identified.

12

7. Action on Previous Inspection Findings (92701)

(Open)

URI 89-09-02, Determine If One SI Pump Injection Into Three Cold

Legs Should Be Demonstrated.

On September 25,

1990, SP-938,

Safety

Injection Pumps Cold Leg Runout Test, was performed to measure pump

discharge pressures and flow rates of the A and B SI pumps when each pump

injected into the three cold legs.

The measured cold leg injection header

flow for both pumps was approximately 640 gpm at 360 psig.

Due to these

values being outside the stated acceptance criteria, each pump was secured

prior to the specified two-minute run time data point.

However, the

inspectors observed that both flows and discharge pressures

stabilized

before the pumps were secured.

In accordance with their established

procedure, a 72-hour operability determination period was entered.

The

established acceptance criteria, flow less than 600 gpm and pressure

greater than 500 psig,

had been chosen by engineering based upon

historical anticipated pump performance.

Thus,

failure to meet the

procedural

acceptance criteria did not demonstrate the pumps were

incapable of meeting their intended safety function nor that performance

was degraded.

Initial review indicated that the higher flow rates would

not adversely affect the pump motors; however,

the 1968 Worthington

Corporation estimated NPSH curves did not provide required NPSH values for

flow rates greater than 600 gpm.

Vendor curve extrapolation by the

inspectors indicated that the required NPSH at 640 gpm would be between 33

and 35 ft.

In comparison, a 1988 calculation, FRSS/SS-CPL-1131, showed

with a maximum flow rate of 596 gpm, one SI pump would have 29.8 ft. NPSH

available at the low-low RWST level.

As the NPSH adequacy concern could

not be resolved within 72-hours, the licensee conservatively declared the

SI pumps inoperable and reported the potential problem per 10 CFR 50.72.

At the end of the report period, another SP was being developed to obtain

more accurate flow and pressure data,

as well as additional data which

would characterize the pump and pump motor performance.

(Closed) IFI 89-08-02, Review Long Term Resolution of Split Pin Cracking

Issue.

(See paragraph 3, Upper Internals Inspection.)

No violations or deviations were identified.

8.

Exit Interview (30703)

The inspection scope and findings were summarized on October 18,

1990,

with those persons indicated in paragraph 1. The inspectors described the

areas inspected and discussed in detail the inspection findings listed

below and in the summary. Dissenting comments were not received from the

licensee. Proprietary information is not contained in this report.

Item Number

Description/Reference Paragraph

90-22-01

UNR - Review If TMI Item Commitments

Have

Been Improperly Superseded By

RG-1.97 Commitments (paragraph 2)

13

90-22-02

VIO- Failure To Adequately Implement

Procedures As Required By TS (paragraph

2)

90-22-03

VIO - Failure To Correct An Exercise

Weakness

Concerning

Event

Classification (paragraph 5)

90-22-04

NCV - Failure To Implement Procedure

PEP-171 (paragraph 5)

9. List of Acronyms and Initialisms

AFW

Auxiliary Feedwater

CFR

Code of Federal Regulations

CV

Containment Vessel

DG

Diesel Generator

EAL

Emergency Action Level

EDG

Emergency Diesel Generator

EOC

Emergency Operation Center

ERO

Emergency Response Organization

EST

Engineering Surveillance Test

ft

Feet

gpm

Gallons Per Minute

HBR

H. B. Robinson

HPES

Human Performance Evaluation System

HVAC

Heating Ventilation Air Conditioning

IEB

Inspection Enforcement Bulletin

IEN

Inspection Enforcement Notice

IGSCC

Intergranular Stress Corrosion Cracking

IR

Inspection Report

LCO

Limiting Condition for Operation

LER

Liscense Event Report

M

Modification

MRP

Maintenance Refueling Procedure

NOUE

Notification of Unusual Event

NOV

Notice of Violation

NPSH

Net Positive Suction Head

NRC

Nuclear Regulatory Commission

OEF

Operating Experience Feedback

OMM

Operations Management Manual

ONS

Onsite Nuclear Safety

OSC

Operations Support Center

OST

Operations Surveillance Test

PM

Preventive Maintenance

PPM

Parts Per Million

PNSC

Plant Nuclear Safety Committee

POER

Plant Operating Experience Report

psig

Pounds per square inch -

gage

RHR

Residual Heat Removal

14

RM

Radiation Monitor

RMS

Radiation Monitoring System,

RO

Reactor Operator

RPS

Reactor Protection System

RTGB

Reactor-Turbine Generator Board

RWST

Refueling Water Storage Tank

SAT

Station Auxiliary Transformer

SCR

Significant Condition Report

SEC

Site Emergency Coordinator

SER

Safety Evaluation Report

SFP

Spent Fuel Pool

S/G

Steam Generator

SI

Safety Injection

SP

Special Procedure

SRO

Senior Reactor Operator

TI

Training Instruction

TMM

Technical Support Management Manual

TLV

Threshold Limiting Value

TS

Technical Specification

TSC

Technical Support Center

UE

Unusual Event

URI

Unresolved Item

UT

Ultrasonic Testing

VAR

Volts-Amps Reactive

VIO

Violation

WD

Waste Disposal

WR

Work Request

WR/JO

Work Request/Job Order