ML13333A696
| ML13333A696 | |
| Person / Time | |
|---|---|
| Site: | San Onofre |
| Issue date: | 08/31/1988 |
| From: | Morgan H, Siacor E SOUTHERN CALIFORNIA EDISON CO. |
| To: | NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM) |
| References | |
| NUDOCS 8809200146 | |
| Download: ML13333A696 (8) | |
Text
NRC MONTHLY OPERATING REPORT DOCKET NO. 50-206 UNIT SONGS - 1 DATE September 15, 1988 COMPLETED BY E. R. Siacor TELEPHONE (714) 368-6223 OPERATING STATUS
- 1. Unit Name:
San Onofre Nuclear Generating Station, Unit 1
- 2. Reporting Period:
August 1988
- 3. Licensed Thermal Power (MWt):
1347
- 4. Nameplate Rating (Gross MWe):
456
- 5. Design Electrical Rating (Net MWe):
436
- 6. Maximum Dependable Capacity (Gross MWe):
456
- 7. Maximum Dependable Capacity (Net MWe):
436
- 8. If Changes Occur In Capacity Ratings (Items Number 3 Through 7)
Since Last Report, Give Reasons:
NA
- 9. Power Level To Which Restricted, If Any (Net MWe):
390
- 10. Reasons For Restrictions, If Any:
Self-imposed power level limit to control steam generator tube corrosion.
This Month Yr.-to-Date Cumulative
- 11. Hours In Reporting Period 744.00 5,855.00 185,959.00
- 12. Number Of Hours Reactor Was Critical 634.17 1,702.84 108,164.36
- 13. Reactor Reserve Shutdown Hours 0.00 0.00 0.00
- 14. Hours Generator On-Line 626.00 1,689.08 104,115.77
- 15. Unit Reserve Shutdown Hours 0.00 0.00 0.00
- 16. Gross Thermal Energy Generated (MWH) 663,680.16 1,968,672.86 131,097,640.91
- 17. Gross Electrical Energy Generated (MWH) 217,800.00 648,000.00 44,325,728.42
- 18. Net Electrical Energy Generated (MWH) 202,046.00 597,777.00 41,820,440.00
- 19. Unit Service Factor 84.14%
28.85%
55.99%
- 20. Unit Availability Factor 84.14%
28.85%
55.99%
- 21. Unit Capacity Factor (Using MDC Net) 62.29%
23.42%
51.58%
- 22. Unit Capacity Factor (Using DER Net) 62.29%
23.42%
51.58%
- 23. Unit Forced Outage Rate 0.00%
0.00%
19.83%
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
Cycle 10 refueling outage scheduled for November 27, 1988
- 25. If Shutdown At End Of Report Period, Estimated Date of Startup: NA
- 26. Units In Test Status (Prior To Commercial Operation):
Forecast Achieved INITIAL CRITICALITY NA NA INITIAL ELECTRICITY NA NA COMMERCIAL OPERATION NA NA 7596u.rpt/3 SS8O9200146. 8031 PDR ADOCK 05000206 R
0 AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-206 UNIT SONGS - 1 DATE September 15, 1988 COMPLETED BY E. R. Siacor TELEPHONE (714) 368-6223 MONTH:
August 1988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 0.00 17 379.63 2
0.00 18 377.92 3
0.00 19 376.50 4
0.00 20 268.50 5
0.00 21 378.50 6
38.13 22 379.33 7
230.00 23 380.42 8
366.63 24 382.54 9
372.92 25 381.08 10 302.08 26 377.13 11 178.08 27 237.58 12 201.33 28 367.29 13 223.38 29 379.21 14 363.88 30 376.83 15 378.04 31 374.71 16 380.00 7596u.rpt/4
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-206 UNIT NAME SONGS - 1 REPORT MONTH AUGUST 1988 DATE September 15, 1988 COMPLETED BY E. R. Siacor TELEPHONE (714) 368-6223 Method of Shutting Cause & Corrective Duration Down LER Syste Compongnt Action to No.
Date Typel (Hours)
Reason2 Reactor3 No.
Code" Code" Prevent Recurrence 117 880214 S
118.00 H
4 88-001 BA ISV Mid-cycle maintenance out BQ PDSV extended to upgrade certain BP FT components in order to meet IP FSV,FCV 10CFR 50.49 requirements.
118 880810 S
0.00 B
5 NA KE COND Power reduction of 20% or greater to perform condenser water box cleaning.
119 880820 S
0.00 B
5 NA KE COND Power reduction of 20% or greater to perform condenser water box cleaning.
120 880826 S
0.00 B
5 NA KE COND Power reduction of 20% or greater to perform condenser water box cleaning.
1F-Forced 2Reason:
3Method:
41EEE Std 805-1984 S-Scheduled A-Equipment Failure (Explain) 1-Manual B-Maintenance or Test 2-Manual Scram.
C-Refueling 3-Automatic Scram.
D-Regulatory Restriction 4-Continuation from E-Operator Training & License Examination Previous Month F-Administrative 5-Reduction of 20%
G-Operational Error (Explain) or greater in the H-Other (Explain) past 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> 6-Other (Explain) 7596u/5
SUMMARY
OF OPERATING EXPERIENCE FOR THE MONTH DOCKET NO.
50-206 UNIT SONGS - 1 DATE September 15, 1988 COMPLETED BY E. R. Siacor TELEPHONE (714) 368-6223 Date Time Event August 1 0001 Unit is in Mode 4, day 171 of the current mid-cycle outage.
0548 Entered Mode 3.
August 5 1307 Entered Mode 2.
1350 Reactor made critical.
2045 Entered Mode 1.
2200 Unit synchronized to the grid. Continue reactor power increase.
August 8 0929 Reactor at 92% power. Turbine load at 397 MWe gross.
August 10 1100 Commenced reduction to 50% reactor power to allow bumping circulating water pumps for condenser water box cleaning.
1755 Reactor at 50% power.
August 13 2230 Commenced reactor power increase following completion of water box cleaning.
August 14 0535 Reactor at 92% power. Turbine Load at 403 MWe gross.
August 20 001 Commenced reduction to 50% reactor power to allow cleaning of condenser water boxes.
0708 Reactor at 50% power.
1630 Commenced reactor power increase following completion of condenser water box cleaning.
2313 Reactor at 92% power. Turbine load at 401 MWe gross.
7596u.rpt/6
SUMMARY
OF OPERATING EXPERIENCE FOR THE MONTH DOCKET NO.
50-206 UNIT SONGS - 1 DATE September 15, 1988 COMPLETED BY E. R. Siacor TELEPHONE (714) 368-6223 Date Time Event August 26 2300 Commenced reduction to 50% reactor power to allow cleaning of condenser water boxes, the forebay and circulating water tunnels.
August 27 2200 Commenced reactor power increase following completion of condenser water box, forebay and circulating water tunnel cleaning operations.
August 28 0450 Reactor at 91% power. Turbine load at 400 MWe gross.
August 31 2400 Unit is in Mode 1 at 92% reactor power. Turbine load at 396 MWe gross.
7596u.rpt/7
REFUELING INFORMATION DOCKET NO.
50-206 UNIT SONGS - 1 DATE September 15, 1988 COMPLETED BY E. R. Siacor TELEPHONE (714) 368-6223 MONTH:
August 1988
- 1. Scheduled date for next refueling shutdown.
November 27, 1988
- 2. Scheduled date for restart following refueling.
Under Evaluation
- 3. Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?
Yes.
What will these be?
Proposed Technical Specification Changes are as follows:
Proposed Change Number (PCN) 169 revises Technical Specification (TS) 3.5.2, "Control Group Insertion Limits" to delete Control Group 1 allowable insertion and to incorporate Standard Technical Specification (STS) format and Action Statements.
Proposed Change Number (PCN) 182 revises TS 4.16, "Inservice Inspection of Steam Generator Tubing" to include an alternate tube plugging criteria.
Proposed Change Number (PCN) 184 revises the demonstration of Control Element Assembly trippability to 7 days prior to reducing shutdown margin below the limits.
Proposed Change Number (PCN) 185 revises Appendix A TS 2.1 and 3.5.1 to include the revised steam/feedwater flow mismatch trip setpoints and associated Limiting Conditions for Operations.
Proposed Change Number (PCN) 186 revises TS 4.2, "Safety Injection and Containment Spray System" periodic testing to include surveillance of a planned modification to add Safety Injection/Feedwater Pump trip on low-low Refueling Water Storage Tank (RWST) level.
Proposed Change Number (PCN) 194 modifies the positive isolation barrier requirements in TS 3.3.2 due to modifications to include MOV-358 onto the Uninterruptible Power Supply (UPS) for MOV-850C.
7596u.rpt/8
REFUELING INFORMATION DOCKET NO.
50-206 UNIT SONGS - 1 DATE September 15, 1988 COMPLETED BY E. R. Siacor TELEPHONE (714) 368-6223 MONTH:
August 1988 Proposed Change Number (PCN) 197 increases the load limit to 6000 KW for each of the two Emergency Diesel Generators.
- 4.
Scheduled date for submitting proposed licensing action and supporting information.
PCN 169 - submitted to the NRC on 05/26/88 PCN 182 - submitted to the NRC on 03/10/88 PCN 184 - scheduled for submittal to the NRC by mid-October 1988 PCN 185 - scheduled for submittal to the NRC by mid-October 1988 PCN 186 - scheduled for submittal to the NRC by mid-October 1988 PCN 194 - scheduled for submittal to the NRC by mid-October 1988 PCN 197 - scheduled for submittal to the NRC by mid-October 1988
- 5.
Important Licensing considerations associated with refueling, e.g. new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.
None
- 6. The number of fuel assemblies.
a) In the core.
157 b) In the spent fuel storage pool.
146
- 7.
Licensed spent fuel storage capacity. 216 Intended change in spent fuel storage capacity. Under review
- 8.
Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.
Under Evaluation 7596u.rpt/9
Southem California Edison Company SAN ONOFRE NUCLEAR GENERATING STATION P.O. BOX 128 SAN CLEMENTE, CALIFORNIA 92672 H. E. MORGAN TELEPHONE STATION MANAGER (714) 368-6241 September 15, 1988 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555
Subject:
Docket No. 50-206 Monthly Operating Report for August 1988 San Onofre Nuclear Generating Station, Unit 1 Enclosed is the Monthly Operating Report as required by Section 6.9.1.10 of Appendix A, Technical Specifications to Provisional Operating License DPR-13 for San Onofre Nuclear Generating Station, Unit 1.
Please contact us if we can be of further assistance.
S's erely, Enclosures cc:
J. B. Martin (Regional Administrator, USNRC Region V)
F. R. Huey (USNRC Senior Resident Inspector, Units 1, 2 and 3)
Institute of Nuclear Power Operations (INPO) 2, L