ML092680208

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IR 05000282-09-009, 05000306-09-009, on 07/20/2009 - 08/13/2009, Prairie Island Nuclear Plant, Routine Biennial Problem Identification and Resolution Inspection
ML092680208
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 09/25/2009
From: Jack Giessner
Reactor Projects Region 3 Branch 4
To: Schimmel M
Northern States Power Co
References
EA-06-178 IR-09-009
Download: ML092680208 (37)


See also: IR 05000282/2009009

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

September 25, 2009

EA-06-178

Mr. Mark A. Schimmel

Site Vice President

Prairie Island Nuclear Generating Plant

Northern States Power Company, Minnesota

1717 Wakonade Drive East

Welch, MN 55089

SUBJECT:

PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2, NRC

BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION

REPORT 05000282/2009009; 05000306/2009009

Dear Mr. Schimmel:

On August 13, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed a biennial

team inspection of problem identification and resolution at your Prairie Island Nuclear

Generating Plant, Units 1 and 2. The inspection team also reviewed a sample of corrective

actions taken for Prairie Island in response to requirements of a confirmatory order issued to

Nuclear Management Company, LLC on January 3, 2007. The enclosed inspection report

documents the inspection findings which were discussed on August 7, 2009, with Mr. M. Wadley

and members of your staff; an exit was held on August 13, 2009, with Mr. D. Koehl and other

staff members.

This inspection was an examination of activities conducted under your license as they

relate to the identification and resolution of problems, compliance with the Commission=s

rules and regulations, and with the conditions of your operating license. Within these areas,

the inspection involved selected examination of procedures and representative records,

observations of activities, and interviews with personnel.

The inspection team concluded that on the basis of the sample selected for review, in general,

problems were properly identified, evaluated, and corrected.

Based on the results of this inspection, three NRC-identified findings of very low safety

significance were identified. These findings involved violations of NRC requirements. However,

because of their very low safety significance, and because the issues were entered into your

corrective action program, the NRC is treating the issues as Non-Cited Violations (NCVs) in

accordance with Section VI.A.1 of the NRC Enforcement Policy.

M. Schimmel

-2-

If you contest the subject or severity of these NCVs, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the

U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,

DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory

Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC

20555-0001; and the Resident Inspector Office at the Prairie Island Nuclear Generating Plant.

In addition, if you disagree with the characterization of any finding in this report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the

Prairie Island Nuclear Generating Plant. The information that you provide will be considered in

accordance with Inspection Manual Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA/

John B. Giessner, Chief

Branch 4

Division of Reactor Projects

Docket Nos. 50-282; 50-306;72-010

License Nos. DPR-42; DPR-60; SNM-2506

Enclosure:

Inspection Report 05000282/2009009; 05000306/2009009

w/Attachment: Supplemental Information

cc w/encl:

D. Koehl, Chief Nuclear Officer

G. Salamon, Regulatory Affairs Manager

P. Glass, Assistant General Counsel

Nuclear Asset Manager

J. Stine, State Liaison Officer, Minnesota Department of Health

Tribal Council, Prairie Island Indian Community

Administrator, Goodhue County Courthouse

Commissioner, Minnesota Department

of Commerce

Manager, Environmental Protection Division

Office of the Attorney General of Minnesota

Emergency Preparedness Coordinator, Dakota

County Law Enforcement Center

M. Schimmel

-2-

If you contest the subject or severity of these NCVs, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the

U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,

DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory

Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC

20555-0001; and the Resident Inspector Office at the Prairie Island Nuclear Generating Plant.

In addition, if you disagree with the characterization of any finding in this report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the

Prairie Island Nuclear Generating Plant. The information that you provide will be considered in

accordance with Inspection Manual Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA/

John B. Giessner, Chief

Branch 4

Division of Reactor Projects

Docket Nos. 50-282; 50-306;72-010

License Nos. DPR-42; DPR-60; SNM-2506

Enclosure:

Inspection Report 05000282/2009009; 05000306/2009009

w/Attachment: Supplemental Information

cc w/encl:

D. Koehl, Chief Nuclear Officer

G. Salamon, Regulatory Affairs Manager

P. Glass, Assistant General Counsel

Nuclear Asset Manager

J. Stine, State Liaison Officer, Minnesota Department of Health

Tribal Council, Prairie Island Indian Community

Administrator, Goodhue County Courthouse

Commissioner, Minnesota Department

of Commerce

Manager, Environmental Protection Division

Office of the Attorney General of Minnesota

Emergency Preparedness Coordinator, Dakota

County Law Enforcement Center

DOCUMENT NAME: G:\\Prai\\Prai Is 2009 009 PI&R.doc

Publicly Available

Non-Publicly Available

Sensitive

Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE

RIII

RIII

NAME

RLerch:dtp

JGiessnerRL

for

DATE

09/24/09

09/25/09

OFFICIAL RECORD COPY

Letter to M. Schimmel from J. Giessner dated September 25, 2009

SUBJECT:

PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2, NRC

BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION

REPORT 05000282/2009009; 05000306/2009009

DISTRIBUTION:

Susan Bagley

RidsNrrPMPrairieIsland

RidsNrrDorlLpl3-1 Resource

RidsNrrDirsIrib Resource

Cynthia Pederson

Steven Orth

Jared Heck

Allan Barker

Carole Ariano

Jeannie Choe

Linda Linn

DRPIII

DRSIII

Patricia Buckley

Tammy Tomczak

ROPreports Resource

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-282; 50-306;72-010

License Nos:

DPR-42; DPR-60; SNM-2506

Report No:

05000282/2009009; 05000306/2009009

Licensee:

Northern States Power Company, Minnesota

Facility:

Prairie Island Nuclear Generating Plant, Units 1 and 2

Location:

Welch, MN

Dates:

July 20 through August 13, 2009

Inspectors:

R. Lerch, Project Engineer, Team Leader

K. Stoedter, Senior Resident Inspector, Prairie Island

S. Thomas, Senior Resident Inspector, Monticello

D. Betancourt, Reactor Engineer

R. Winter, Engineering Inspector

M. Phalen, Senior Radiation Protection Inspector

Approved by:

J. Giessner, Chief

Branch 4

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

Summary of Findings .................................................................................................................. 1

Report Details ............................................................................................................................. 4

4.

OTHER ACTIVITIES .................................................................................. 4

4OA2

Biennial Problem Identification and Resolution (71152B) ........................... 4

4OA6

Management Meetings ............................................................................ 18

SUPPLEMENTAL INFORMATION ............................................................................................. 1

KEY POINTS OF CONTACT .................................................................................................. 1

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ........................................................ 2

LIST OF DOCUMENTS REVIEWED ....................................................................................... 3

LIST OF ACRONYMS USED ................................................................................................ 13

1

Enclosure

SUMMARY OF FINDINGS

IR 05000282;05000306/2009-009; 07/20/2009 - 08/13/2009; Prairie Island Nuclear Plant,

Routine Biennial Problem Identification and Resolution Inspection.

This inspection was performed by four NRC regional inspectors and the Prairie Island senior

resident inspector with a 1 week assist by the Monticello senior resident inspector. Three Green

findings were identified by the inspectors. The findings were considered Non-Cited Violations of

NRC regulations. The significance of most findings is indicated by their color (Green, White,

Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination

Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a

severity level after NRC management review. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 4, dated December 2006.

Problem Identification and Resolution

On the basis of the information reviewed, the team concluded that the corrective action (CA)

program at Prairie Island was functional, but implementation was lacking in rigor resulting in

inconsistent and undesirable results. In general, the licensee had a low threshold for identifying

problems (issue reports called CAPs) and entering them in the CA program; however, some

significant issues went unrecognized and therefore CAPs were not issued for these. Most items

entered into the CA program were screened and prioritized in a timely manner using established

criteria; however, inspectors observed inconsistency and lack of rigor in the screening process.

Most issues, including operating experience, were properly evaluated commensurate with their

safety significance; and corrective actions were generally implemented in a timely manner,

commensurate with the safety significance. However, the inspectors identified significant

examples of issues with evaluation and corrective action shortcomings that resulted in

inspection findings. The backlog of corrective actions was large and growing. Audits and self-

assessments were determined to be performed at an appropriate level to identify deficiencies,

but the station was not taking full advantage of the processes and results. On the basis of

interviews conducted during the inspection, and a review of the employee concerns program,

workers at the site were willing to enter safety concerns into the CA program.

Inspectors continued to have concerns with the performance of the corrective action program.

The last biennial problem identification and resolution inspection in 2007 was critical of program

implementation and weaknesses were recognized by the licensee. An improvement effort was

initiated. At the time of this inspection, inspectors concluded that performance had declined and

another improvement plan was in progress. The current improvement program was not yet fully

implemented and effective.

A.

NRC-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

Green. The inspectors identified a finding of very low significance and non-cited

violation (NCV) of Technical Specification 5.4.1.a for the licensee failing to obtain a

temporary or permanent procedure change, as required by their Procedure Use and

Adherence procedure, prior to implementing a procedure when it was determined that

they could not complete a required swap of two heater drain pumps using the applicable

2

Enclosure

section of the appropriate operating procedure. Once identified, the licensee took

actions to correct the issue and entered the issue into their corrective action program.

The inspectors determined the finding to be more than minor because if left uncorrected,

this finding had the potential to lead to a more significant safety concern. The inspectors

evaluated the finding using Inspection Manual Chapter (IMC) 0609, Appendix A,

Attachment 1, Significance Determination of Reactor Inspection Findings for At-Power

Situations, using the Phase 1 Worksheet for the Initiating Events Cornerstone. Since

the finding did not contribute to both the likelihood of a reactor trip and the likelihood that

mitigation equipment or functions will not be available, the inspectors concluded that the

finding was of very low safety significance. The inspectors determined that the

performance deficiency affected the cross-cutting area of Human Performance, having

work practices components, and involving aspects associated with personnel following

procedures. (H.4(b)). (Section 40A2.a(1))

Cornerstone: Mitigating Systems

Green. The inspectors identified a Non-Cited Violation (NCV) of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Actions, for the failure to promptly correct a

condition adverse to quality regarding the expired qualification of safety-related molded

case circuit breakers. Specifically, the licensee failed to evaluate extending the service

life of safety-related molded case circuit breakers beyond the 20 year life expectancy, a

condition adverse to quality. The licensee entered this issue into its corrective action

program.

The finding was more than minor in accordance with IMC 0612, Appendix B, Issue

Screening, dated December 4, 2008, because the finding was associated with the

Mitigating Systems Cornerstone attribute of equipment performance and affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences (i.e., core damage).

Specifically, an unqualified safety-related molded case circuit breaker could lead to

higher trip times and potential unavailability of safety-related components associated

with the bus when a circuit fault is present. The finding screened as of very low safety

significance because the finding was a qualification deficiency confirmed not to have

resulted in loss of operability or functionality in service. This finding had a cross-cutting

aspect in the area of Problem Identification and Resolution, operating experience,

because the licensee failed to implement maintenance information through changes to

station processes and procedures to address the qualification of the breakers from

Vendor Technical Bulletin 06-2 (P.2(b)). (Section 40A2.b.4))

Cornerstone: Emergency Preparedness

Green. The inspectors identified a finding of very low safety significance and a

Non-Cited Violation of 10 CFR 50.54(q), associated with 10 CFR 50.47(b)(8), for

failing to maintain the portion of the emergency plan in effect regarding the adequate

maintenance of the Technical Support Center (TSC) emergency facility. Specifically, the

implementation of procedure steps in Surveillance Procedure (SP) 1689, TSC

Ventilation System Operability Check, on January 25, 2009, resulted in the licensees

failure to test the TSC ventilation system in its as-found condition. As a result, the TSC

ventilation system and an emergency preparedness planning standard were

unknowingly degraded between July 26, 2008, and January 25, 2009. Corrective

3

Enclosure

actions for this issue included ensuring that the TSC ventilation system was

appropriately tested in July 2009 and revising SP 1689 to ensure that the TSC

ventilation system was appropriately tested in the future.

This finding was more than minor because it was associated with the attribute of

meeting the planning standards of 10 CFR 50.47(b). In addition, the finding affected

the cornerstone objective of ensuring that the licensee was capable of implementing

adequate measures to protect the health and safety of the public in the event of a

radiological emergency. The inspectors used Section 4.8 of the Emergency

Preparedness Significance Determination Process and concluded that this finding

was of very low safety significance, because the associated emergency preparedness

planning standard was not lost. The finding was determined to be cross-cutting in the

area of Human Performance, Resources because procedure SP 1689 was not complete

and accurate (H.2(c)). (Section 40A2.a(2))

B.

Licensee-Identified Violations

No violations of significance were identified.

4

Enclosure

REPORT DETAILS

4.

OTHER ACTIVITIES

4OA2 Biennial Problem Identification and Resolution (71152B)

The activities documented in Sections a. through d. constituted one biennial sample of

problem identification and resolution as defined in IP 71152.

a.

Assessment of the Corrective Action Program Effectiveness

Inspection Scope

The inspectors reviewed the licensees Corrective Action (CA) program implementing

procedures, interviewed personnel and attended CA program meetings to assess the

implementation of the CA program by site personnel.

The inspectors reviewed risk and safety significant issues in the licensees CA

program since the last NRC Problem Identification and Resolution (PI&R) inspection

in October 2007. The selection of issues ensured an adequate review of issues across

NRC cornerstones. The inspectors used issues identified through NRC generic

communications, department self assessments, licensee audits, operating experience

reports, and NRC documented findings as sources to select issues. Additionally, the

inspectors reviewed issue reports called CAPs, generated as a result of facility

personnels performance in daily plant activities. In addition, the inspectors reviewed

CAPs and a selection of completed investigations from the licensees various

investigation methods, which included root causes, apparent causes, equipment

apparent causes, and common cause investigations.

A 5 year review of emergency diesel generator (EDG) crankcase pressure issues

was also undertaken to assess the licensee staffs efforts in monitoring for system

degradation due to aging aspects. The inspectors also performed a partial system

walkdowns of the EDGs.

During the reviews, the inspectors evaluated the licensee staffs actions to comply with

the facilitys corrective action program and 10 CFR Part 50, Appendix B requirements.

Specifically, the inspectors evaluated if licensee personnel were identifying plant issues

at the proper threshold, entering the plant issues into the stations CA program in a

timely manner, and assigning the appropriate prioritization for resolution of the issues.

The inspectors also evaluated whether the licensee staff assigned the appropriate

investigation method to ensure the proper determination of root, apparent, and

contributing causes. The inspectors also evaluated the timeliness and effectiveness of

corrective actions for selected issue reports, completed investigations, and NRC

findings, including Non-Cited Violations.

5

Enclosure

Assessment

(1) Effectiveness of Problem Identification

In general, problem identification was adequate and at the right threshold. The sample

of issues reviewed by inspectors that were entered into the CA program indicated a low

threshold, with a steady generation of CAPs on a monthly basis. CAP generation

numbers appeared representative of a good problem identification ethic. Other safety

conscious work environment (SCWE) indications such as surveys and interviews

indicated willingness to identify issues and capture them in the CAP. However, there

were several previous NRC findings that demonstrated elements of failure to identify an

issue through generating a CAP. Examples included not recognizing wooden tables

used in an area of safety-related equipment as a fire load; operators proceeding with use

of non-aligned procedures which resulted in an unplanned automatic start of a diesel fire

pump; and use of inadequate procedures for feedwater heater drain pump swaps (see

the finding below). Other examples included performance indicator data for several

NRC performance indicators which were not accurately reported. This was also a repeat

issue. Inspectors at the CAP screening meeting observed problem descriptions that

were inadequate for screening and evaluating the issues, but went unchallenged by the

committee. Other issues were raised, but were not addressed by members. Specific

examples included ownership of equipment specifications for security equipment, and a

request for an operability evaluation for some uncontrolled acetone used in the plant.

The inspectors concluded that improved standards and expectations, and increased

accountability, were required for effective performance of the screening committee.

Findings

Failure to Follow Procedures for Heater Drain Pump Swaps

Introduction: The inspectors identified a finding of very low significance and a Non-Cited

Violation (NCV) of Technical Specification 5.4.1.a for failure to obtaining a temporary or

permanent procedure change, as required by the Procedure Use and Adherence

procedure, prior to implementing a procedure when it was determined that a swap of two

heater drain pumps could not be completed using the applicable section of the operating

procedure.

Description: On June 2, 2009, the operating crew was tasked with changing the heater

drain pump line-up utilizing operating procedure 2C28.4, Unit 2 Heater Drains. The

normal heater drain pump configuration for full power operations consists of two of the

three heater drain pumps operating, with one heater drain pump secured. The actual

evolution to be performed consisted of changing the heater drain tank pump

configuration of the operating heater drain pumps from pumps 22 and 23 to pumps 21

and 23. The evolution was to be conducted per section 5.3 (swapping heater drain

pumps) of operating procedure 2C28.4.

Shortly after commencing section 5.3, due to a pre-existing equipment deficiency

associated with the 23 heater drain pump speed control, the operating crew

discovered that they could not place the pump speed selector switch in Auto (as

required by step 5.3.5). Licensee procedure FP-G-DOC-03, revision 5, Procedure

Use and Adherence, step 3.3.6 required the following:

6

Enclosure

Stop work activity if a procedure deficiency is identified and activities cannot

proceed per the procedure. The procedure deficiency SHALL be corrected by

initiation of a temporary or permanent procedure change in accordance with

FP-G-DOC-04, Procedure Processing, prior to proceeding.

Instead of stopping when confronted with a procedural deficiency, the operating crew

decided to use multiple individual sections in the 2C28.4 procedure to accomplish the

heater drain tank pump swap. This decision resulted in several additional pump starts

and stops in a system which has the potential to directly impact reactivity. After

completing the evolution, the operating crew entered the issue into the corrective action

program and a condition evaluation was performed. The condition evaluation

determined that the procedure deficiency was a human performance error trap and that

the additional pump manipulations that were required to perform the heater drain pump

swap was an operator challenge. Even after it was determined to be a human

performance error trap and an operator challenge, nothing was done to address the

procedure deficiency, until after inspectors questioned the licensee, approximately

2 months later.

Analysis: The inspectors determined that the failure of the licensee to implement their

Procedure Use and Adherence procedure when confronted with an operating procedure

that could not be performed, as written, constituted a performance deficiency warranting

significance evaluation in accordance with Inspection Manual Chapter (IMC) 0612,

Appendix B, Issue Disposition Screening. The inspectors determined the performance

deficiency to be more than minor, because if left uncorrected, the issue had the potential

to lead to a more significant safety concern. The inspectors evaluated the finding using

IMC 0609, Appendix A, Attachment 1, Significance Determination of Reactor Inspection

Findings for At-Power Situations, using the Phase 1 Worksheet for the Initiating Events

Cornerstone. Since the finding did not contribute to both the likelihood of a reactor trip

and the likelihood that mitigation equipment or functions will not be available, the

inspectors concluded that the finding was of very low safety significance (GREEN). The

inspectors determined that the performance deficiency affected the cross-cutting area of

Human Performance, having work practices components, and involving aspects

associated with personnel following procedures. (H.4(b))

Enforcement: Technical Specification 5.4.1.a requires that written procedures shall

be established, implemented, and maintained covering applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

The Administrative Procedures section of Regulatory Guide 1.33 specifically mentions

procedures for Procedure Adherence and Temporary Change Method." FP-G-DOC-03,

revision 5, Procedure Use and Adherence, step 3.3.6 requires, in part that the licensee

stops the work activity if a procedure deficiency is identified and activities cannot

proceed per the procedure and that the procedure deficiency SHALL be corrected

by initiation of a temporary or permanent procedure change in accordance with

FP-G-DOC-04, Procedure Processing, prior to proceeding. Contrary to this

requirement, on June 2, 2009, the licensee did not obtain a temporary or permanent

procedure change prior to proceeding when it was determined that they could not

complete a required swap of two heater drain pumps on Unit 2 using the applicable

section of the appropriate operating procedure. Because this violation was of very low

safety significance and it was entered into the licensees corrective action program

(CAP 1192435), it is being treated as an NCV, consistent with Section VI.A.1 of the

NRC Enforcement Policy. (NCV 05000306/2009009-01)

7

Enclosure

(2) Effectiveness of Prioritization and Evaluation of Issues

Assessment

The inspectors determined that the overall performance in prioritization and evaluation of

issues was acceptable, but marginal. Some corrective actions are years old and

completion priority is not linked to potential safety significance. For example, a final

White finding for the inadequate design of the component cooling water system (second

quarter 2009) was initially discovered by the licensee in completing a corrective action

which was over 3 years old. The issues in the CA program were being prioritized by

significance (root cause, apparent cause, common cause, fix) and by due dates. This

made it difficult to prioritize most routine issues assigned only due dates. The licensee

was applying a safety related (condition adverse to quality (CAQ)) versus non-safety

related (not a condition adverse to quality (NCAQ)) screening criteria to assist with

prioritization. Inspectors noted that this approach did not address the risk to plant

operations and was not always accurately applied, although all issues were addressed.

In addition, several issues in the inspection period occurred which had been identified

earlier, but were not corrected in time to prevent recurrence. These issues included:

Technical Support Center (TSC) dampers, underground cable failures (for which

corrective actions had been identified but not completed), and insulation on auxiliary

feedwater piping which was an issue in a previous outage.

While most evaluations were good, some evaluation weaknesses observed by

inspectors could be characterized as addressing the symptoms rather than the causes.

Several other issues had been identified in the inspection period where questioning by

inspectors resulted in significant changes to the evaluations and ultimately NRC findings.

Specifically, inspectors questioned evaluations on employee respirator qualifications, a

control room chill water pump mission time, and an event concerning a release of

hydrazine and others. Most weaknesses identified by inspectors could be generally

attributed to a lack of rigor in the analysis.

Observations

Operator Burdens

Corrective actions for operator burdens have not been adequately prioritized or effective

in maintaining operator burdens at a minimized level. The inspectors evaluated how the

licensee was handling selected long-term equipment issues and operator burdens and

the licensees efforts to reduce the numbers of each. A general assessment of key

areas is as follows:

5 of the top 10 equipment issues have been on the list for between 3 and

6 years;

there are currently in excess of 70 work request stickers in the control room;

5 of the 7 Operator Workarounds are in excess of 2 years old;

There are currently approximately 81 Operator Burdens. These burdens consist of

7 operator workarounds; 22 operator challenges; 38 control room deficiencies; and

14 long term installed clearances. The overall number of Operator Burdens also could

include temporary modifications which impact operations, but the inspector did not

evaluate this component and their number is not reflected in the 81 Operator Burdens.

8

Enclosure

The licensee has significantly exceeded their Operator Burden performance indicator

goal (<37) for at least the past 8 months.

Based on an increasing trend in the numbers of Operator Burdens over the past

2 months, the licensee has not successfully implemented corrective actions to reduce

and manage the number of existing Operator Burdens. Some observations associated

with specific Operator Burdens are as follows:

There is an operator workaround associated with each of the main turbine turning

gears failing to engage in automatic [schedule dates for repair are 12/7/2009 for

11, and 5/10/2010 for 21]. Since the failure of the 11 turning gear to engage

following the July 2008 reactor trip forced the licensee to break condenser

vacuum and significantly impacted the trip response and recovery, the inspectors

questioned the priority placed on remedying these deficiencies.

There is an Operator Challenge associated with each of the Instrument Air (IA)

Compressors (121/122/123) aftercooler cooling water control valve having to be

manually bypassed, due to the control valves being obsolete and non-functional.

For each compressor, the operators are tasked with maintaining the cooling

water pressure in a band higher than 60 psig, but less than the system relief

pressure of 75 psig. Exacerbating this condition is the fact that some of the

piping is experiencing periodic silting, which also impacts the ability to maintain

the appropriate pressure band to the IA compressors. The inspectors were

informed that the aftercooler cooling water control valves would not be repaired

since a major instrument air modification was being planned. Since the IA

system has some risk significance, the inspectors questioned the decision to live

with this operator challenge until the IA modification was completed (currently

scheduled for July 2010).

There was an Operator Challenge associated with the operation of heater drain

pumps. A finding associated with this issue in Section 40A2.a(1).

Foxboro H-Line Modules

Another long term equipment issue evaluated by the inspectors was associated with the

Foxboro H-Line modules which are used in reactor protection, reactor control, and

balance of plant applications. These components were first identified in 1985 for

replacement to be completed by 1995. Instead of replacement, they were reclassified as

run to failure. Since that time, the licensee has considered several options to address

the obsolescence of these modules. During July 2008, a plant trip occurred as a result

of the failure of one of these modules, coincident with reactor protection system (RPS)

testing. In summary, the licensee continues to be at risk for a plant trip during their

monthly RPS testing. No long term corrective action to address the obsolete Foxboro

modules has been implemented. The licensee currently has funded a project designed

to replace the obsolete modules.

9

Enclosure

Findings

Inadequate Technical Support Center Ventilation System Testing

Introduction: The inspectors identified a Non-Cited Violation (NCV) of

10 CFR 50.47(b)(8) having a very low safety significance (Green) for failing to maintain

the portion of the emergency plan in effect regarding the adequate maintenance of the

TSC emergency facility. Specifically, the implementation of procedure steps in

Surveillance Procedure (SP) 1689, TSC Ventilation System Operability Check, on

January 25, 2009, resulted in the licensees failure to test the TSC ventilation system in

its as-found condition. As a result, the TSC ventilation system and an emergency

preparedness planning standard were unknowingly degraded between July 26, 2008

and January 25, 2009.

Description: The Prairie Island TSC is a two story structure within the turbine building.

The upper floor is the TSC proper and the lower floor is an overflow area that is used as

the work control center during normal operation. The TSC ventilation system consists of

separate upper and lower trains that, in the normal mode, draws in outside air through

two large dampers, blows the air through an air handler for heating or cooling, and then

recirculates the air through the structure and back to the air handlers through return

ducts. When switched to the emergency mode, which is required during TSC activation,

the normal outside air dampers would close, and a smaller outside air damper would

modulate open to supply air through particulate and charcoal filters to the air handlers.

In addition, some of the air in the return ducts would also be directed through the filters.

The air handler fans remain on to recirculate the air.

As part of this inspection, the inspectors reviewed the corrective actions associated with

Non-Cited Violation 05000282/2008002-01; 05000306/2008002-01. During this review,

the inspectors identified that operations personnel were verifying the position of four

manual TSC ventilation system dampers as discussed in SP 1689, TSC Ventilation

System Operability Check. If any of the dampers were found in an unexpected position,

SP 1689 allowed the dampers to be repositioned prior to performing the system

operability test. Based upon the information discussed above, the inspectors were

concerned that the licensee was potentially pre-conditioning the TSC ventilation system.

This pre-conditioning could result in the failure to demonstrate the continued functionality

of the TSC ventilation system due to the failure to test the system in the as-found

configuration.

The inspectors reviewed the results of TP/SP 1689 performed between March 5, 2008,

and July 31, 2009. The inspectors identified that two of the manual dampers were

re-positioned prior to performing SP 1689 on January 25, 2009. As a result, the

inspectors were concerned that the TSC may have been non-functional for

approximately 6 months during the timeframe mentioned above. The inspectors

determined that the TSC was currently functional due to the successful completion of

SP 1689 (without any damper adjustments) on July 31, 2009.

The inspectors discussed this issue with operations and engineering personnel. The

licensee conducted a functionality review and determined that the TSC ventilation

system was functional but degraded from July 26, 2008 through January 25, 2009 due to

the failure to test the TSC ventilation system in its as-found configuration. The licensee

10

Enclosure

also implemented a procedure change request to remove the procedure steps that

allowed the dampers to be repositioned prior to performing SP 1689.

Analysis: The inspectors concluded that the failure to test the TSC ventilation system in

a manner that supported emergency response activities was a performance deficiency

because it could result in the failure to maintain TSC habitability, and a failure to ensure

adequate protection of emergency response personnel from airborne contamination

during an actual emergency.

The inspectors concluded that the finding did not have actual safety consequences

because there were no events that resulted in a radioactive release between July 2008

and January 2009. The finding did not affect the NRCs ability to perform its regulatory

function and was not willful. The inspectors applied the Significance Determination

Process (SDP) to the finding and determined it was associated with a failure to meet a

regulatory requirement in the emergency preparedness cornerstone. The finding was

more than minor because it was associated with the attribute of meeting the planning

standards of 10 CFR 50.47(b) and affected the cornerstone objective of ensuring that

the licensee was capable of implementing adequate measures to protect the health and

safety of the public in the event of a radiological emergency.

In accordance with the SDP Phase 1 Screening Worksheet of Inspection Manual

Chapter (IMC) 0609, the inspectors applied Appendix B, Emergency Preparedness

Significance Determination Process, and determined that Section 4.8 applied. The TSC

function was degraded for a period of longer than 7 days from the time of discovery as

defined in the emergency preparedness SDP. Although not specifically discussed in

Section 4.8 of the SDP, a finding involving a degraded planning standard was one color

lower in significance than a finding involving a loss of the planning standard. Since a

loss of the TSC for more than 7 days from the time of discovery would have been a

White finding under Section 4.8, a degraded TSC was determined to be a Green finding.

This was supported by the flow chart on Sheet 1 of Section 4.8 by answering yes to the

planning standard problem decision point, no to the risk significant planning standard

problem decision point, no to the planning standard functional failure decision point,

and thus arriving at the Green result box. This finding was also related to the

cross-cutting area of Human Performance, Resources because procedure SP 1689

was not complete and accurate (H.2(c)).

Enforcement: Part 50.54(q) of 10 CFR required that licensees follow and maintain in

effect emergency plans which meet the standards in 10 CFR 50.47(b). Part 50.47(b)(8)

of 10 CFR required that adequate emergency facilities and equipment to support the

emergency response be provided and maintained. Prairie Island Nuclear Generating

Plant Emergency Plan, Revision 40, Section 7.1.1, required that the TSC have a

shielding and ventilation cleanup system to provide habitability under accident

conditions. Contrary to the above, the licensee failed to maintain the portion of their

emergency plan in effect regarding the adequate maintenance of the TSC emergency

facility. Specifically, the implementation of procedure steps in SP 1689 on January 25,

2009, resulted in the licensees failure to test the TSC ventilation system in its as-found

condition. As a result, the TSC ventilation system and an emergency preparedness

planning standard were unknowingly degraded between July 26, 2008 and January 25,

2009. The licensee entered this issue into their corrective action system as

CAP 1192415. The licensee also initiated a procedure change request to ensure that

the TSC ventilation system was tested in its as-found configuration in the future.

11

Enclosure

Because this violation was of very low safety significance and was entered into

the licensees corrective action program, this violation is being treated as a

Non-Cited Violation consistent with Section VI.A of the NRC Enforcement Policy

(NCV 05000282/2009009-02; 05000306/2009009-02). Corrective actions for this

issue consisted of ensuring that the TSC ventilation system was appropriately tested

in July 2009 and revising SP 1689 to ensure that the TSC ventilation system was

appropriately tested in the future.

(3) Effectiveness of Corrective Actions

While the majority of issues were effectively resolved, a significant number of repetitive

issues were reviewed by inspectors during the inspection period. A lack of consistent

effectiveness was evident in repeated issues with very high radiation area keys, security

weapons controls, check valve SI-9 5, and roll-up door compensatory actions.

Additionally, many long term issues lingered. Issues considered by inspectors to be

lacking resolution included the turbine turning gears on both units, operator burdens,

Foxboro controller issues, TSC dampers, and air compressor aftercooler cooling water

control valves.

Work load appeared to be a factor in corrective action effectiveness by impacting the

timeliness of the implementation of actions. The station had backlogs in corrective

actions as well as work requests, engineering requests and other work items. Backlogs

existed at the time of the last PI&R and have not improved. Some backlogs have

increased.

Observations

Five Year Historical Review - D5/D6 Emergency Diesel Generator Crankcase Pressure

Issues

In the late 1990s the licensee began experiencing high crankcase pressure conditions

on the D5 and D6 emergency diesel generators during routine surveillance testing.

This condition has resulted in the entry into numerous unplanned limiting conditions

for operation and a Unit 2 shutdown. During this inspection, the inspectors reviewed

a sampling of corrective action program documents regarding this issue that were

generated between the years 2004 and 2009. The inspectors also discussed this issue

with operations, engineering, and management personnel. The corrective action

documents indicated that the elevated crankcase pressure condition was caused by the

reduction in diesel fuel oil sulfur content. Based upon this information, the licensee had

pursued two courses of action to resolve the crankcase pressure condition. The first

course of action involved modifying the engine crankcase breather system. The second

course of action involved increasing the sulfur content of the diesel fuel oil. In 2009, the

licensee began introducing an additive to the diesel fuel oil to increase the sulfur content.

The licensee referred to this action as fuel oil doping. Although the fuel oil doping had

resulted in a reduction in engine crankcase pressure for the D5 and D6 emergency

diesel generators, the licensee was continuing to monitor engine performance. The

licensee planned to make a decision regarding the need for the breather system

modification after obtaining additional engine performance data.

12

Enclosure

Findings

No findings of significance were identified.

b.

Assessment of the Use of Operating Experience

1) Inspection Scope

The inspectors reviewed the licensees implementation of the facilitys Operating

Experience (OE) program. Specifically, the inspectors reviewed implementing operating

experience program procedures, attended CA program meetings to observe the use of

OE information, reviewed completed evaluations of OE issues and events, and reviewed

selected monthly assessments of the OE composite performance indicators. The

inspectors review was to determine whether the licensee was effectively integrating OE

experience into the performance of daily activities, whether evaluations of issues were

proper and conducted by qualified personnel, whether the licensees program was

sufficient to prevent future occurrences of previous industry events, and whether the

licensee effectively used the information in developing departmental assessments and

facility audits. The inspectors also assessed if corrective actions, as a result of OE

experience, were identified and effectively implemented.

2) Assessment

The inspectors determined that the overall performance of the operating experience

program was acceptable, but that a negative trend in the use of Operating Experience

needs to be promptly addressed. The licensee utilized a program that was structured

and established reasonable objectives. The licensee used its screening meetings to

select relevant OE and direct them to the appropriate department. The inspectors did

identify, by reviewing the Operating Experience procedure, that the licensee had

committed to assess its program every 2 years, but the licensee had not performed a

self-assessment since 2005. This information was provided to the licensee and is being

addressed by the licensees corrective action program. Two key observations and a

finding, discussed below, indicate the licensee is not being proactive in its use of OE.

Nuclear Oversight (NOS) performed independent assessments of the site. They

appeared to identify some negative trends. Additionally, the evaluations of external OE

and NRC generic communications the inspectors reviewed seemed to appropriately

address some issues identified in the OE. However, the NRC, not the site, identified the

trend that OE was not being effectively used at the site.

3) Observations

Tracking of Vendor Manual Changes

It was noted during this inspection that vendor manual changes were difficult to track

through the corrective action program. The inspector reviewed the Vendor Manual

Procedure to evaluate the process by which the vendor manual changes are

incorporated into the appropriate procedures, and also interviewed the Vendor

Information Coordinator (VIC) to further understand the process. The procedure guided

the VIC to use the corrective action program to process changes to procedures, but the

inspector was not able to find any open vendor manual changes. The VIC noted that the

person assigned the action would know it, but the inspector noted that for every one else

13

Enclosure

it is difficult to find. The inspector concluded there was a vulnerability in the tracking

system since there is a potential to not complete the changes by the due date. In

addition, the staff may not know what changes are being processed through the

corrective action program. One NRC identified and several licensee identified instances

were found in which vendor manual changes had not being incorporated into

procedures. The VIC noted that an action had been recently implemented to add a

method to track the vendor manual changes, and it was entered into the licensees

corrective action program.

Untimely Implementation of Operating Experience

During the inspection period the inspectors reviewed a previously identified

trend regarding the untimely implementation of OE (see NRC inspection report

05000282/2009003; 05000306/2009003). The trend had five new examples of untimely

operating experience that led to operational challenges and equipment failures. For

example, actions from the lessons learned on long standing issues for Unit 1 cavity

leakage were still open and had not been implemented. In addition, several OE sources

for flooding and high energy line breaks were not effective in identifying potential issues

at the site until brought to the attention by the NRC. Through the review of various OE

evaluations, the inspectors agreed with the identified trend that there is a weakness

related to the implementation of OE that could lead to additional equipment failures or

failure to identify an adverse condition. A condition report was initiated to address the

trend of untimely implementation of corrective actions, but it was too soon to see if the

actions taken have been effective.

Additionally, during this inspection the inspector identified another example of

untimely implementation of OE in that a number of safety-related breakers were

past their qualified life, as mentioned in the OE Evaluation of a Technical Bulletin

from Westinghouse. The condition had not been addressed or corrected. This

issue is discussed in the findings section.

4) Findings

Failure to Qualify Safety-Related Molded Case Circuit Breakers

Introduction: The inspectors identified a Non-Cited Violation (NCV) of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Actions, for the failure to promptly correct a

condition adverse to quality regarding the expired qualification of safety-related molded

case circuit breakers.

Description: On August 3, 2009, the inspectors identified that the licensee had deferred

the preventive maintenance for five safety-related HFB Molded Case Circuit Breakers

(MCCBs) beyond 125 percent of the required 5 year frequency. The inspectors

questioned the reason for the deferral, and also requested that the licensee provide the

life expectancy of the MCCBs, as well as the duration that these breakers had been in

service. The licensee stated that the deferral was due to unanticipated complications

encountered in the engineering change process associated with the selection of an

acceptable replacement model, as well as parts availability. It was also stated that there

was no indication of any age-related degradation in the operation of the breakers. The

licensee also stated that, per Westinghouse Technical Bulletin-06-02 (TB-06-02), dated

March 10, 2006, the life expectancy for these breakers was 20 years due to the type of

14

Enclosure

grease and oil used in them, which were found to be limiting factors for continued

operability within published specifications. At the time the bulletin was received, the

breakers in question had been in service for 23 years. At the time of this inspection,

those breakers had been in service for 26 years.

The licensee had entered the 2006 bulletin into their corrective action program as

AR 01019169. The licensees evaluation of the bulletin determined that a total of

89 MCCBs of the affected style (both safety and non-safety related) were in use at

Prairie Island at the time. As a result, the licensee developed a corrective action to

replace the safety-related MCCBs every 15 years going forward; however, they failed

to evaluate the acceptability of operation of the currently installed MCCBs that were

beyond their 20 year life expectancy. The licensee also failed to extend the qualified life

by meeting the requirements of TB-06-2 by using a combination of preventive

maintenance and aging management.

As of August 06, 2009, the licensee had 13 safety-related MCCBs that were older than

20 years for which the licensee had not performed an evaluation to provide reasonable

assurance that these circuit breakers could perform their safety function until

replacement. Some examples of the affected breakers include: BKR-112G-1 to the

Shield Building Gas Radiation Monitor, BKRG-12 121 to the Control Room Chilled Water

Pump and BKRG-122G-15 to the Control Room Air Handler and Fan.

On August 9, 2009 the licensee performed an operability determination and

determined that the HFB breakers were operable, but non-conforming, based on

acceptable performance history of the breakers during past preventive maintenance

and no in-service failures. Based on discussion with Westinghouse, the licensee tested

three MCCBs (10 percent of the population) to support that the breakers had not been

affected by binding or sluggish operation. The three MCCBs were selected based on

the length of time since their last test. The results showed trip times in the appropriate

range. The licensee stated that they plan to test the rest of the breakers before the next

refueling outage in October 2009.

Analysis: The inspectors determined that the failure to promptly correct a condition

adverse to quality regarding the expired qualification of safety-related molded case

circuit breakers was a performance deficiency. Specifically, the licensee failed to

evaluate extending the service for safety-related molded case circuit breakers beyond

the 20 year life expectancy, a condition adverse to quality. The finding was determined

to be more than minor in accordance with IMC 0612, Appendix B, Issue Screening,

dated December 4, 2008, because the finding was associated with the Mitigating

Systems Cornerstone attribute of equipment performance and affected the cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences (i.e., core damage). Specifically,

an unqualified safety-related molded case circuit breaker could lead to higher trip times

and potential unavailability of safety-related components associated with the bus when a

circuit fault is present.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of Findings, Table 3b for the Mitigating System

Cornerstone. Although the molded case circuit breakers associated with this

performance deficiency affected systems and components in the Mitigating System,

15

Enclosure

Occupational Radiation Safety and the Containment Barrier Cornerstones, the number

of mitigating systems affected was significantly higher than the systems associated with

the Containment Barrier and Occupational Radiation Safety Cornerstones and was used

to evaluate the significance of the finding. The finding screened as of very low safety

significance (Green) because the finding was a qualification deficiency confirmed not to

result in loss of operability or functionality.

This finding had a cross-cutting aspect in the area of Problem Identification and

Resolution, operating experience, because the licensee failed to implement maintenance

information through changes to station processes and procedures to address the

qualification of the breakers from Vendor Technical Bulletin 06-2 (P.2(b)).

Enforcement: 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires,

in part, that measures be established to assure that conditions adverse to quality, such

as failures, malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformance are promptly identified and corrected. Contrary to the above, from

March 10, 2006 to August 9, 2009, the licensee failed to promptly correct a condition

adverse to quality regarding the expired qualification of safety-related molded case

circuit breakers. Specifically, although the bulletin was in their corrective action program

as AR0119169, the licensee failed to evaluate extending the service for safety-related

molded case circuit breakers beyond the 20 year life expectancy. Because this violation

was of very low safety significance and was entered into the licensees corrective action

program as AR 1192430, this violation is being treated as an NCV, consistent with

Section VI.A.1of the NRC Enforcement Policy (NCV 05000282/2009009-03; 05000306/2009009-03). Corrective actions included conducting an operability

determination and setting a program in place to test the remaining breakers.

c.

Assessment of Self-Assessments and Audits

1)

Inspection Scope

The inspectors assessed the licensee=s ability to identify and enter issues into the station

CAP, prioritize and evaluate issues, and implement effective corrective actions, through

efforts from departmental and nuclear oversight (NOS) assessments. The inspectors

assessed the licensee=s ability to properly capture the documented deficiencies from

assessments into CAP items. The inspectors reviewed the focused self-assessment

performed on the corrective action program early in 2009.

2) Assessment

While the licensee has programs and processes in place to conduct meaningful

assessments and audits, full benefits of these programs were not realized due to their

limited application and ineffective corrective actions. Organizational self assessments

were limited to assessments conducted prior to audits by external organizations. While

problem identification was reasonable and many issues were resolved, the program was

driven by external schedules that may not address station weaknesses. Backlogs of

other work products were a limiting factor in assigning resources to perform self

assessments. Also, the station was not responding rigorously to issues identified by

NOS (see the observations below) such that some NOS identified issues were not

corrected before NRC inspectors identified and evaluated them.

16

Enclosure

The site performed a 2009 PI&R self-assessment of the CA program and determined,

although several areas needed improvement, the station was adequately implementing

the CA program. The assessment documented issues in the major areas of cause

analysis, safety culture, effectiveness of performance indicators, management oversight,

timely and effective execution of corrective actions and completion dates based on the

significance of issues. The CAP overall effort was hindered by having no simple

mechanism to identify ineffective corrective actions. Although the causes were generally

found, most apparent cause evaluations tended to be short and did not always examine

the issue in sufficient depth to resolve the issue fully. Backlog in the work products

including the CA program work products remained high. The site did not consistently set

due dates for corrective actions that are commensurate with the significance of issues,

leading to having repeat issues.

Generally, the assessment identified issues that were consistent with the conclusions of

the inspectors. The inspectors held discussions with the NOS Manager regarding NOS

activities with respect to the station=s performance in CA program. The inspectors

concluded that although the station has had improvement programs and effort toward

CA program improvement since the last PI&R, recognizable improvement in most areas

was lacking.

3) Observations

Nuclear Oversight Assessments

The inspectors considered the quality of the NOS assessments to be adequate.

However, the inspectors were concerned that several NOS identified issues have

remained open and unresolved for an extended period of time. Specifically, the first

quarter 2009 NOS Assessment Report identified that the stations radiation protection

program had been assessed as below expectations since the fourth quarter of 2006.

The stations corrective actions program had been assessed by NOS as performing

below expectations for over 3 1/2 years. The site has one White finding in the public

radiation cornerstone from the first quarter 2009. In discussions with the NOS staff, it

was identified that although there were processes in place to escalate specific and

discrete issues, a similar process for programmatic issues was just recently

implemented. This change in the NOS program was designed to increase the focus

on resolving long-standing programmatic issues through accountability of the line

organization. Requiring the line organizations that are assessed as below expectations

for two consecutive quarters to develop recovery plans that are reviewed and approved

by the line managers, the site vice president, and the NOS manager, should drive

correction of the actual performance deficiency and facilitate the timely resolution of

issues.

Additionally, further review by NRC inspectors identified that some of the issues

chronically identified by NOS lacked consistent performance deficiency specificity.

For example, while the NOS reports state that the radiation protection program was

performing below expectations, the actual deficiencies described in each report varied.

The first quarter 2009 report identified the radiation protection areas of concern as

human performance events and the key control program. In the third quarter 2008

report, the areas of concern were identified as ALARA planning, personal contamination

events, and the trip ticket program. The escalation process described above is designed

to focus the line organization around solving specific issues, while more clearly defining

17

Enclosure

the systemic concerns that NOS may have with any particular program. Additionally,

there is evidence that the line organization is slow to respond and resolve issues

identified by the NOS organization. Specifically, NOS recognized issues associated with

respirator qualifications, the load sequencer and compensatory measures with the roll up

door, prior to these issues being identified and issued as violations by the NRC.

4) Findings

No findings of significance were identified.

d.

Assessment of Safety Conscious Work Environment (SCWE)

1) Inspection Scope

The inspectors assessed the licensees safety conscious work environment through the

reviews of the facilitys employee concerns program (ECP) implementing procedures,

postings for maintaining employee awareness of the ECP program, literature,

discussions with the ECP coordinator, interviews with personnel from various

departments, and reviews of issue reports. The inspectors reviewed the results from an

August 2008 Safety Culture Survey, and reviewed corrective actions taken in response

to an order issued to Nuclear Management Company LLC dated January 3, 2007.

2) Assessment

The licensee maintains an accessible, functioning ECP program, promotes a safety

conscious work environment to employees, and periodically assesses employee

attitudes though email surveys and a safety culture assessment by an outside team from

the Utilities Service Alliance. Based on the CAPs generated at the plant, discussions

with employees, and survey results, the SCWE at the plant appeared adequate and no

concerns were identified by the inspectors.

3) Observations

Safety Conscious Work Environment

The ECP procedure does not reference 10 CFR 50 Appendix B. Employees raising

concerns through the ECP program may identify a condition adverse to quality, a

condition that must be corrected. The ECP coordinator was aware that conditions

adverse to quality were to be entered into the CA program for correction, and records

indicated that no conditions adverse to quality were identified that had not had a CAP

written.

Confirmatory Order EA-06-178

(Discussed) Corrective Actions for Confirmatory Order for NMC Re: 10 CFR 50.7

Violation (EA 2006-178) Inspectors reviewed the CAPs initiated to address the Order.

The biennial PI&R inspection of 2007 (inspection report 2007006) reviewed SCWE

training material, which had been developed in response to NRC Confirmatory Order

Enforcement Action (EA-06-178). Actions were completed in 2008 addressing a safety

conscious work environment in all organizations of the plant, including the appropriate

headquarters personnel. Corrective actions included periodic training requirements so

18

Enclosure

new employees would be trained and existing employees retrained on a programmed

schedule. Effectiveness reviews were also performed. The inspectors concluded that

the actions appeared thorough and complete such that the issues of the order were

adequately addressed for Prairie Island Nuclear Generating Plant.

4) Findings

No findings of significance were identified.

4OA6 Management Meetings

Exit Meetings Summaries

On August 7, 2009, the inspectors presented some of the inspection results to

M. Wadley (then Vice President), and other members of the licensee staff. The

licensee acknowledged the issues presented. The inspectors confirmed that none

of the potential report input discussed was considered proprietary.

On August 13, inspectors conducted an exit by telephone with licensee

staff and presented the final determination of NCV 05000282/2009009-03; 05000306/2009009-03, Molded Case Circuit Breaker Qualification. In the previous

week, the licensee tested a sample of breakers, confirming the proper functional

capability (see Section 4OA2.b.4, Assessment of the Use of Operating Experience).

ATTACHMENT: SUPPLEMENTAL INFORMATION

1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

D. Koehl, Chief Nuclear Officer, Excel Energy *

M. Wadley, Site Vice President +

B. Sawatzke, Director Site Operations +

K. Ryan, Plant Manager +

D. Albarado, Organizational Effectiveness

J. Anderson, Regulatory Affairs Manager +

T. Bacon, Ops Support Manager

B. Boyer, RP Supervisor

M. Brassart. Engineering Supervisor +

H. Butterworth, Operations Support Fleet Director Operations Standards

L. Clewett, Business Support Manager +

M. Davis, Regulatory Compliance Analyst +

C. England, RP/Chemistry Manager Acting

B. Flynn, Safety and Human Performance Manager

S. Ford, Design Engineering Supervisor

D. Hartinger, System Engineering Supervisor

R. Hite, Radiation Protection and Chemistry Manager

M. Hopman, Engineering Supervisor

S. Ingalls, Operations Shift Manager +

B. Kappes, Nuclear Oversight Assessor

D. Kettering, Site Engineering Director +

J. Kivi, Employee Concerns Program Manager

L. Koehl, Communications *

S. Lappegaard, On-line Manager

J. Lash, Operations Manager

G. Lenertz, Maintenance Engineer

L. Lisson, IT

R. Madjerich, Production Planning Manager +

S. Martin, Nuclear Oversight

S. McCall, Engineering Manager, plant and System Engineering

K. Mews, Regulatory Affairs Engineer +

J. Muth, Nuclear Oversight Manager

S. Myers, Design Engineering Manager +

C. Nash, Chemistry General Supervisor

S. Northard, Performance Improvement Manager

S. Oswald, Regulatory Analyst

K. Petersen, Performance Assessment

A. Pullam, Training Supervisor

B. Rogers, Training Supervisor +

M. Schmidt, Maintenance Manager

S. Skoyen, Engineering programs Manager

J. Sternisha, Training Manager

J. Verbout, IT

J. Windschill, Fleet Performance Assessment Manager

2

Attachment

+ August 7 and 13, exits

  • August 13, 2009 teleconference exit

Nuclear Regulatory Commission

J. Giessner, Branch Chief, Branch 4 Division of Reactor Projects, Region III

P. Zurawski, Resident Inspector, Prairie Island

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened 05000306/2009009-01

NCV

Failure to Follow Procedures for Heater Drain

Pump Swaps05000282/2009009-02; 05000306/2009009-02

NCV

Inadequate Technical Support Center (TSC)

Ventilation System Testing 05000282/2009009-03; 05000306/2009009-03

NCV

Failure to Qualify Safety-Related Molded Case

Circuit Breakers

Closed 05000306/2009009-01

NCV

Failure to Follow Procedures for Heater Drain

Pump Swaps05000282/2009009-02; 05000306/2009009-02

NCV

Inadequate Technical Support Center (TSC)

Ventilation System Testing 05000282/2009009-03; 05000306/2009009-03

NCV

Failure to Qualify Safety-Related Molded Case

Circuit Breakers

Discussed

EA 2006-178

ORD

Confirmatory Order for NMC 10 CFR 50.7

Violation (EA 2006-178)

3

Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspectors reviewed the documents in their entirety, but

rather, that selected sections of portions of the documents were evaluated as part of the

overall inspection effort. Inclusion of a document on this list does not imply NRC

acceptance of the document or any part of it, unless this is stated in the body of the

inspection report.

OPERATING EXPERIENCE

Number

Description or Title

Date or Revision

N/A

OEs discussed during 7/23/09 OE

Screening Meeting

07/23/2009

01019169

Westinghouse TB-06-2 Aging Issues and

Subsequent Operating issues for Breakers

that are at their 20 Year Design/Qualified

Lives

05/14/2006

01114450

OE25538- Emergency Diesel Generator

Starting Air Check Valve Failure

01/07/2008

01114820

NRC in 2007-28: Potential Common

12/11/2007

01125130

SOER 2007-01 Initial Review

06/14/2008

01125290

Potential Trend in SOER implementation

quality

03/15/2008

01129444

Conduct FSA - SOER 99-01 and 01-03

review

07/02/2009

01133930

SOER 96-1 Implementation and

Effectiveness Review

02/20/2009

01133939

SOER 03-1 Implementation and

Effectiveness Review

04/06/2009

01133941

SOER 93-1 Implementation and

Effectiveness Review

02/28/2009

01133942

SOER 96-2 Implementation and

Effectiveness Review

04/06/2009

01133947

SOER 97-1 Implementation and

Effectiveness Review

04/09/2008

01133949

SOER 98-1 Implementation and

Effectiveness Review

02/28/2009

01133954

SOER 87-1 Implementation and

Effectiveness Review

11/22/2008

01133958

SOER 02-4 Implementation and

Effectiveness Review

05/06/2009

01133963

SOER 95-1 Implementation and

Effectiveness Review

12/22/2008

01137327

SOER 07-02, Intake Cooling Blockage

05/15/2008

01141208

Actions not fully implemented for SOER

03-02

02/03/2009

01143220

SOER FSA: Analysis of a Single point

vulnerability

07/03/2008

4

Attachment

OPERATING EXPERIENCE

Number

Description or Title

Date or Revision

01143430

SOER FSA: Sustainability of SOER

actions

09/24/2008

01156119

Part 21 issue with Gaskets

10/19/2008

01169744

SOER 90-2 Implementation and

Effectiveness Review

04/06/2009

01169746

SOER 91-1 Implementation and

Effectiveness Review

04/30/2009

01175087

FBM: Lifting and Rigging and evaluate

SOER 06-01 Actions

03/26/2009

PLANT PROCEDURES

Number

Description or Title

Date or Revision

2C28.4

Unit 2 Heater Drains

Rev. 26

5AWI 3.10.8

Equipment Problem Resolution Process

Rev. 13

5AWI 3.15.5

Operability determinations

Rev. 14

DP-NO-IA-01

Internal Assessments

Rev. 04

DP-NO-IA-01

Internal Assessments

Rev. 01

DP-NO-IA-03

Internal Assessment Issue

Characterization and Tracking

Rev. 05

DP-NO-IA-06

Stop Work Order

Rev. 01

DP-NO-IA-07

Internal Assessment: Topic Selection,

Scheduling, and Quarterly Reporting

Rev. 04

FG-PA-CAE-01

Corrective Action Effectiveness Review

Manual

Rev. 06

FG-PA-DRUM-01

Department Roll Up Meeting (DRUM)

Manual - Department Performance

Trending

Rev. 08

FP-EC-ECP-01

Employee Concerns Program

Rev. 03

FP-E-VEN-01

Vendor Manual Control

Rev. 02

FP-G-DOC-03

Procedure Use and Adherence

Rev. 05

FP-OP-OB-01

Operator Burden Program

Rev. 00

FP-PA-ARP-01

Cap Action Request Process

Rev. 22

FP-PA-OE-01

Operating Experience

Rev. 12

FP-PA-SA-01

Focused Self-Assessment Planning,

Conduct and Reporting

Rev. 09

FP-PA-SA-02

Focused Self-Assessment and Formal

Benchmarking Scheduling

Rev. 05

5

Attachment

CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED

CR Number

Description or Title

Date or Revision

0831627

D5 Slow Start Surveillance Terminated Due To

High Crankcase Pressure

04/11/2005

0833665

Unexpected Signs of Wear on D5 Engine 1

Cylinder

04/15/2005

0864735

Opportunities are Being Missed to Improve

Equipment Performance via the Corrective

Action Program

07/07/2005

01013473

D6 Experienced High Crankcase Pressure

02/04/2006

01035981

Speed Control Problems with 23 Charging

Pumps Resulted in Flow Variations to Reactor

Coolant System and Charging Line High

Pressure Alarms

06/18/2006

01040613

Inadequate Implementation of Welding

Program

07/20/2006

01055847

Evaluate NRC IN- 2006-22; New Ultra-Low-

Sulfur Fuel Could Adversely Impact Diesel

Engine Performance

10/16/2006

01059041

Manage D5/D6 Enhancements Identified by

Root Cause

11/01/2006

01074017

Vendor Manual XH 52-32 is not up to date

01/26/2007

01082591

Xcel Energy Truck Struck a Tower in Prairie

Island Switchyard

03/16/2007

01088616

Operations Adverse Trend in Human

Performance

07/22/2009

01094238

D5 Engine 2 Elevated Crankcase Pressure

During Post Maintenance Testing

05/28/2007

01095381

D6 Crankcase Breather Imbalance

06/05/2007

01099211

2007 System Trending and Monitoring

Focused Self Assessment

12/16/2007

01106329

SOER 07-1 Reactivity Management

07/23/2009

01109480

EA (SBO) Components with incorrect quality

level

08/31/2007

01111011

MRE 01100534-02 incomplete

09/12/2007

01114156

Root Cause Evaluation; VHRA Key RCE

Inadequate

10/05/2007

01115585

Root Cause Report for D5 Inoperability

(Equipment Root Cause and Organizational

Root Cause)

10/22/2007

01118522

Significant OE Issues

03/12/2008

01070334

NRC Confirmatory Order EA-06-178

01/05/2007

01133384

Excel and NMC EE may not have SCWE

training

04/04/2008

01135591

Contractors not trained on policy on writing

CAPs

04/24/2008

01119052;

Shackle came apart and hit Crane; Work Not

Stopped

11/26/2007

6

Attachment

CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED

CR Number

Description or Title

Date or Revision

01121442

D5 Engine 1 Gen Bearing Vibration above

alarm set point

03/08/2008

01123680

D2 Diesel Generator Lube Oil Cooling Water

Side Leak

01/14/2008

01125087

Shortfalls in SOER 2007-01 Assessment

02/27/2008

01125903

TSC Normal Ventilation Performance

Challenged

02/01/2008

01126006

Vendor Info not included in Maintenance

Procedure

02/04/2008

01127120

MR Unavailability for 11 CL Pump 334.5 Hours

not documented in MR

02/13/2008

01127570

TSC Ventilation Temperature Control

Challenged

02/16/2008

01128432

Evaluate TSC Ventilation Function with

Damper Not Full Closed

02/23/2008

01128817

Adverse Trend in Outage Related Isolations

02/26/2008

01129236

During PM Motor Driven Aux Feedwater Pump

12 and 21 noted MSIP 1001 indicated oil is

Heavy Medium while D18 Lubrication specified

Mobil DTE Light

02/29/2008

01129421

TSC Lower Level HVAC Will Not Control

Temperature

03/01/2008

01129623

Control Room Alarm Diesel Room Vent System

Trouble coming in and out

03/03/2008

01129731

TSC Ventilation System Challenged

03/04/2008

01131494

Ineffective Corrective Actions for TSC

Ventilation

03/18/2008

01132293

Programmatic Issues Regarding TSC

Ventilation

03/25/2008

01132717

Root Cause Report for SI-9-5 Check Valve

Failure

06/30/2009

01132717

Apparent Cause Report for SI-9-5 Check Valve

Failure

05/09/2008

01135172

TSC Ventilation Roll Up CAP

04/21/2008

01135817

121 MD CLP has a declining pump performance

trend

04/28/2008

01137253

Engineering CAP Backlog Reduction Effort

Needs Goal

05/09/0208

01140557

TSC System Could Not Maintain Required

Vacuum

06/11/2008

01141755

Root Cause Evaluation; Cross-Cutting Aspects

06/23/2008

01142664

Flexible Electrical Conduit Accidently Pinched

resulting in a Small Amount of Oil into the

Transfer Canal

06/30/2008

01143721

Training to comply with Confirmatory Order not

timely

07/10/2008

7

Attachment

CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED

CR Number

Description or Title

Date or Revision

01144249

TSC Vent System Issues, Not Operating

Properly

07/15/2008

01146105

Deviation from EPRI guidelines

09/05/2008

01146374

Root Cause Evaluation; Hydrazine Event

Rev. 0

01147180

Secondary Chemistry does not meet EPRI

guidelines

09/16/2008

01147573

RPIP 3005 Procedure compliance issue

09/08/2008

01151789

10 CFR Part 21 Relays installed on D5 and D6

05/29/2009

01152814

Evaluate need for airborne hydrazine and

ammonia testing

10/07/2008

01157554

Hydrazine Concentration falls below spec in 21

SG

11/01/2008

01160372

Root Cause Evaluation; Refuel Cavity Leakage

11/24/2008

01165133

Root Cause Evaluation; Cross-Cutting Themes

01/12/2009

01165257

MREP moved SSC from a(1) - a(2) w/o

revised a(1) Action Plan

01/13/2009

01166375

Production Planning DRUM identified potential

trend in schedule development accuracy for

both online and outage schedules

01/22/2009

01166830

Root Cause Evaluation; Corrective Action

Program

01/26/2009

01167124

Effectiveness Review Determined Corrective

Actions to Prevent Recurrence Were

Ineffective

01/28/2009

01167466

Adverse Trend Identified with Engineering CAP

Self Identification Problem Ratio

01/30/2009

01167806

D6, Engine 1 Crankcase Pressure High

02/02/2009

01169214

Unit 2 Turbine Building Crane Cracking

03/22/2009

01169490

D5 - Response to Monitoring Requirement

from CAP 1115585-11

02/15/2009

01171115

D5 Crankcase Pressure Exceeded 20 mm

Water

02/27/2009

01171319

Unit 2, D6 Engine 1 Crankcase Pressure High

03/01/2009

01173309

ABB Part 21 Notification Deviation

03/17/2009

01175335

Work Order 332186 Strainer Backwash

Replacement had not been through Planning

even though on workweek schedule.

03/27/2009

01175917

Potential Inadequate Resolution of SOER 02-

04 issues

03/31/2009

01176383

MR Unavailability Data Collection for July 2009

04/02/2009

01176851

April 2009 Documentation of Engine Crank

Case Pressure During Monthly Run

04/05/2009

01180912

RHR procedures are not adequate in Modes 3

and 4

05/05/2009

01181122

Cant Procedurally Swap HDT Pumps

8

Attachment

CORRECTIVE ACTION PROGRAM DOCUMENTS REVIEWED

CR Number

Description or Title

Date or Revision

01181967

U2 Condensate oxygen above EPRI diagnostic

parameter

07/08/2009

01181983

U2 Unplanned Secondary Action Level 1

05/26/2009

01183067

Ineffective Resolution of OE 15095

05/24/2009

01183142

Trend in ineffective Resolution of OE items

05/26/2009

01184607

Self Assessment Programmatic Weaknesses

06/05/2009

01184643

U2 Entered AL 1 for FW Hydrazine Less than

8X Cond O2

07/20/2009

01187837

Adverse Trend in Governing and Oversight of

PARB

10/30/2009

01190271

Revise to use the CAP process to review and

disposition vendor information

07/21/2009

01191042

Post Maintenance Testing for TSC Ventilation

System Did Not Meet Acceptance Criteria

07/27/2009

01191165

SP 1689 TSC Vent System Operability Test

Failed Acceptance Criteria

07/28/2009

01192415

Functionality Review for TSC Ventilation

System

08/06/2009

AUDITS, ASSESSMENTS AND SELF-ASSESSMENTS

Number

Description or Title

Date or Revision

Nuclear Safety Culture Assessment

August 2009

NOS Observation

Report

Corrective Action Program

12/20/2007

NOS Observation

Report

Corrective Action Program

02/29/2008

NOS Observation

Report

Operating Experience and Self

Assessment

01/06/2009

NOS Observation

Report

CAP Assessment

02/29/2008

NOS Observation

Report

Security

09/02/2008

Nuclear Oversight

4th Quarter 2007 Assessment Report

02/08/2008

Nuclear Oversight

1st Quarter 2008 Assessment Report

05/23/2008

Nuclear Oversight

2nd Quarter 2008 Assessment Report

08/13/2008

Nuclear Oversight

3rd Quarter 2008 Assessment Report

11/14/2008

Nuclear Oversight

4th Quarter 2008 Assessment Report

02/20/2009

Nuclear Oversight

1st Quarter 2009 Assessment Report

06/03/2009

01088616

Snap Shot Report: Procedure Use and

Adherence

09/24/2008

01116150

Operations Training

10/26/2007

01121615

Radiation Program Annual Review

12/18/2007

01124352

Training DRUM

01/21/2008

01124941

HRA/LHRA/VHRA Controls

01/25/2008

9

Attachment

AUDITS, ASSESSMENTS AND SELF-ASSESSMENTS

Number

Description or Title

Date or Revision

01128817

Snapshot Report: Worker Protective

Tagging

06/15/2009

01129439

Emergency Preparedness

03/01/2008

01129444

SOER 99-01

03/01/2008

01129451

Focused Self-Assessment MOV - Motor

Operated Valve Program

08/22/2008

01129453

Focused Self-Assessment Fire

Protection Appendix R;

08/29/2008

01129453

Focused Self-Assessment TDAFW

95001 Inspection Preparation

06/05/2009

01129460

Outage Readiness

03/01/2008

01129463

Safety Culture

03/01/2008

01141307

Emergency Preparedness NEI Forum

06/18/2008

01143359

Training

07/07/2008

01146374

Hydrazine Issue

04/16/2009

01149046

High Radiation Area

08/29/2008

01118231

FTFSA-08-02

02/15/2008

01121596

Focused Self Assessment on 50.59

Program

12/18/2007

01129439

Emergency Preparedness Exercise

Inspection and Performance Indicator

Verification

09/22/2008

01141307

Informal Benchmarking of Emergency

Preparedness

01/19/2009

01155350

Snapshot Report: Security Training

10/07/2008

01158973

Emergency Preparedness

10/21/2008

01158973

Focused Self Assessment of Emergency

Preparedness

12/18/2008

01160507

Snapshot Report: Procedures and Work

Instructions

4/30/2009

01169735

Snapshot Report: Worker Protective

Tagging

07/02/2009

01174895

Training

03/25/2009

01174995

Radiation Protection / Chemistry

Organization

03/26/2009

01175030

Focused Self Assessment of Pre-NRC

Emergency Preparedness Routine

Inspection

06/08/2009

01175071

Focused Self Assessment on System

Trending and Monitoring

07/26/2007

01175930

Emergency Preparedness

03/31/2009

01185859

Snapshot Self Assessment on OE

06/17/2009

01189843

DRUM Security

07/17/2009

10

Attachment

MISCELLANEOUS

Number

Description or Title

Date or Revision

01192324

Procedure Change Request for SP 1689

08/04/2009

D86

Protection of Pre, Absolute, and Charcoal

Ventilation Filters from Contamination

Rev. 07

EC11098

Equivalency Evaluation

Rev. 00

Equipment

Performance

Period Report U2C24

03/30/2009

Health and Status

Report

AF Auxiliary Feedwater

07/02/2009

Health and Status

Report

CT External Circulating Water

07/02/2009

Health and Status

Report

D5 Diesel Generator

07/02/2009

Health and Status

Report

4.16 kV Electrical

07/02/2009

Health and Status

Report

FW Feedwater

07/02/2009

Health and Status

Report

Reactor Protection

07/02/2009

Health and Status

Report

SA Station and Instrument Air

07/02/2009

Health and Status

Report

ZH Safeguards Chilled Water

07/02/2009

IN- 2006-22

New Ultra-Low-Sulfur Fuel Could

Adversely Impact Diesel Engine

Performance

10/12/2006

Maintenance Rule

a(1) Action Plan

Station Air

06/25/2009

Maintenance Rule

a(1) Action Plan

Auxiliary Feedwater

08/21/2008

Maintenance Rule

a(1) Action Plan

EA System 4,160 VAC

11/22/2007

Maintenance Rule

a(1) Action Plan

D5 Diesel Generator

04/21/2009

Maintenance Rule

a(1) Action Plan

RP System F delta Controller

02/10/2009

Maintenance Rule

a(1) Action Plan

Safeguards Chilled Water System 2H

04/16/2009

N/A

NOS Operating Experience Assessment

2008

SA037271

Operating Experience Program

2005

SWI GSE-27

Conduct of System Engineering

Rev. 08

TP 1689

TSC Ventilation System Operability Check

Rev. 17

WO 107758

PE MCC 1T2-A4/BKR 122G-21

WO 107786

PE MCC 1T2-A3/BKR 122G-20

WO 107787

PE MCC 1T2-B2/BKR 122G-13

WO 328804

PE MCC 1T2-B3/BKR 122G-5

11

Attachment

MISCELLANEOUS

Number

Description or Title

Date or Revision

WO 352844

PE MCC-W5 BKR 122G-12

WO 355100

Replace Variable Frequency

03/10/2008

WO 371819

Perform SP 1689 - TSC Ventilation

System Operability Check

01/28/2009

WO 378154

Perform SP 1689 - TSC Ventilation

System Operability Check

07/28/2009

WO 387170

Perform SP 1689 - TSC Ventilation

System Operability Check

07/8/2009

WO 388060

Perform SP 1689 - TSC Ventilation

System Operability Check

07/31/2009

WR 34472

Mark TSC Ventilation Damper Position

CAP Screen Team Meeting Package

08/04/2009

Leadership Alignment Meeting Package

08/04/2009

Management Review Meeting Package;

Rev.01

July 2009

Operator Burden List

08/04/2009

Prairie Island Top Ten Equipment Issue

List

Undated

Reactor Protection Health and Status

Report

07/02/2009

Station and Instrument Air Health and

Status Report

07/02/2009

Team Notes

03/10/2009

CAPs Written as a Result of the Inspection

Number

Description or Title

Date or Rev

1190255

Repeat Task Instruction Found in PMQR

07/21/2009

1190416

SAR 01141307 Did Not Contain Share

Point Attachment

07/22/2009

1190448

Initial NRC Submittal Incorrectly CT as MR

at (1)

07/22/2009

1190547

OE Program Requirements Not Followed

07/22/2009

1190598

B Level CAP 011882867 Has no ACE or

Deviation Listed

07/23/2009

1190625

NRC Feedback on AR Screening

Performance

07/23/2009

1191839

Updates to PMs Not Initiated for Vendor

Documents Change

07/31/2009

1192375

Perform PRA Review of Operator Work

Around

08/05/2009

1192387

Improper Place-keeping During SP 1689

TSC Vent Oper Check

08/05/2009

1192415

SP 1689 TSC Ventilation Operability Ck

Promotes Preconditioning

08/05/2009

12

Attachment

1192430

Safety Related Westinghouse HFB

Breakers Past 20 Year Life

08/05/2009

1192435

Need TCE for Swapping Heater Drain

Tank Pumps

08/05/2009

1192456

Breaker PMID on MCC 1T1/1T2

Improperly Set to Retire

08/06/2009

13

Attachment

LIST OF ACRONYMS USED

AC

Alternating Current

ADAMS

Agencywide Document Access Management System

ALARA

As-Low-As-Is-Reasonably-Achievable

CA

Corrective Action

CFR

Code of Federal Regulations

DC

Direct Current

DG

Diesel Generator

DRP

Division of Reactor Projects

EDG

Emergency Diesel Generator

EPRI

Electric Power Research Institute

FSAR

Final Safety Analysis Report

FW

Feedwater

IMC

Inspection Manual Chapter

IP

Inspection Procedure

kV

Kilovolt

LLC

Limited Liability Corporation

MOV

Motor-Operated Valve

NCV

Non-Cited Violation

NEI

Nuclear Energy Institute

NOS

Nuclear Oversight

NRC

U.S. Nuclear Regulatory Commission

PARS

Publicly Available Records

PI

Performance Indicator

PI&R

Problem Identification and Resolution

PM

Planned or Preventative Maintenance

RFP

Reactor Feed Pump

RP

Radiation Protection

RPS

Radiation Protection Specialist

RPS

Reactor Protection System

SBO

Station Blackout

SDP

Significance Determination Process

SSC

Systems, Structures, and Components

SW

Service Water