ML081930568

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IR 05000445-08-009 and 05000446-08-009 on 06/06/08 for Comanche Peak, Units 1 & 2, Supplemental Inspection
ML081930568
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 07/11/2008
From: Clay Johnson
NRC/RGN-IV/DRP/RPB-A
To: Blevins M
Luminant Generation Co
References
IR-08-009
Download: ML081930568 (14)


See also: IR 05000445/2008009

Text

July 11, 2008

Mike Blevins, Executive Vice President

and Chief Nuclear Officer

Luminant Generation Company LLC

ATTN: Regulatory Affairs

Comanche Peak Steam Electric Station

P.O. Box 1002

Glen Rose, TX 76043

SUBJECT:

COMANCHE PEAK STEAM ELECTRIC STATION - NRC SUPPLEMENTAL

INSPECTION REPORT 05000445/2008009 AND 05000446/2008009

Dear Mr. Blevins:

On June 6, 2008, the U.S. Nuclear Regulatory Commission completed an inspection at your

Comanche Peak Steam Electric Station, Units 1 and 2, facility. The enclosed supplemental

inspection report documents the inspection findings which were discussed at the exit meeting

on June 5, 2008, with Mr. R. Flores and other members of your staff.

The NRC performed this supplemental inspection to assess your evaluation associated with a

White finding in the first quarter of 2008 (failure of Unit 1 Train B Emergency Diesel

Generator 1-02). Detailed observations, assessments, and conclusions of the inspection are

presented in the enclosed inspection report.

The inspection concluded that the root causes of the finding were adequately defined and

understood, and the corrective actions resulting from the evaluations appropriately addressed

the identified causes.

Based on the results of this inspection, no findings of significance were identified.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter

and its enclosure will be made available electronically for public inspection in the NRC

Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS), accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (The Public Electronic Reading Room).

Sincerely,

/RA/

Claude E. Johnson, Chief

Project Branch A

Division of Reactor Projects

UNITED STATES

NUCLEAR REGULATORY COMMISSION

R E GI ON I V

612 EAST LAMAR BLVD, SUITE 400

ARLINGTON, TEXAS 76011-4125

Luminant Generation Company LLC

- 2 -

Dockets: 50-445; 50-446

Licenses: NPF-87; NPF-89

Enclosure:

NRC Inspection Report 05000445/2008009 and 05000446/2008009

cc w/enclosure:

Mr. Fred W. Madden, Director

Regulatory Affairs

Luminant Generation Company LLC

P.O. Box 1002

Glen Rose, TX 76043

Timothy P. Matthews, Esq.

Morgan Lewis

1111 Pennsylvania Avenue, NW

Washington, DC 20004

County Judge

P.O. Box 851

Glen Rose, TX 76043

Mr. Richard A. Ratliff, Chief

Bureau of Radiation Control

Texas Department of Health

1100 West 49th Street

Austin, TX 78756-3189

Environmental and Natural

Resources Policy Director

Office of the Governor

P.O. Box 12428

Austin, TX 78711-3189

Mr. Brian Almon

Public Utility Commission

William B. Travis Building

P.O. Box 13326

1701 North Congress Avenue

Austin, TX 78701-3326

Ms. Susan M. Jablonski

Office of Permitting, Remediation

and Registration

Texas Commission on

Environmental Quality

MC-122

P.O. Box 13087

Austin, TX 78711-3087

Luminant Generation Company LLC

- 3 -

Anthony Jones

Chief Boiler Inspector

Texas Department of Licensing

And Regulation

Boiler Division

E.O. Thompson State Office Building

P.O. Box 12157

Austin, TX 78711

Luminant Generation Company LLC

- 4 -

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

DRP Director (Dwight.Chamberlain@nrc.gov)

DRP Deputy Director (Anton.Vegel@nrc.gov)

DRS Director (Roy.Caniano@nrc.gov)

DRS Deputy Director (Troy.Pruett@nrc.gov)

Senior Resident Inspector (John. Kramer@nrc.gov)

Branch Chief, DRP/A (Claude.Johnson@nrc.gov

Senior Project Engineer, DRP/A (Thomas.Farnholtz@nrc.gov)

Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Only inspection reports to the following:

DRS STA (Dale.Powers@nrc.gov)

J. Adams, OEDO RIV Coordinator (John.Adams@nrc.gov)

P. Lougheed, OEDO RIV Coordinator (Patricia.Lougheed@nrc.gov)

ROPreports

CP Site Secretary (Sue.Sanner@nrc.gov)

SUNSI Review Completed: CEJ ADAMS: Yes

No Initials: CEJ

Publicly Available Non-Publicly Available Sensitive Non-Sensitive

R:\\_REACTORS\\_CPSES\\2008\\CP2008-009 RBC.doc ML 081930568

RIV:RI:DRP/A

C:DRP/A

RBCohen

CEJohnson

/RA electronic/

/RA/

07/09/08

07/11/08

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

- 1 -

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets:

50-445, 50-446

Licenses:

NPF-87, NPF-89

Report :

05000445/2008009 and 05000446/2008009

Licensee:

Luminant Generation Company LLC

Facility:

Comanche Peak Steam Electric Station, Units 1 and 2

Location:

FM-56, Glen Rose, Texas

Dates:

June 2-6, 2008

Inspector:

R. Cohen, Resident Inspector

Approved by:

C. Johnson, Chief, Project Branch A

Division of Reactor Projects

- 2 -

Enclosure

SUMMARY OF FINDINGS

IR 05000445/2008009, 05000446/2008009; 06/02/2008 - 06/06/2008; Comanche Peak Steam

Electric Station, Units 1 and 2, Procedure 95001 Supplemental Inspection.

This report covers a one week period of inspection by a Comanche Peak Steam Electric Station

based resident inspector. No violations were identified. The significance of most findings is

indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609,

Significance Determination Process." Findings for which the significance determination

process does not apply may be Green or be assigned a severity level after NRC managements

review. The NRCs program for overseeing the safe operation of commercial nuclear power

reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated

December 2006.

Cornerstone: Mitigating Systems

The U.S. Nuclear Regulatory Commission performed this supplemental inspection to

assess the licensees evaluation associated with a White finding (failure of Unit 1 Train B

Emergency Diesel Generator 1-02) in the first quarter of 2008. The primary reason for

this finding being characterized as White was based on the results of a Phase 3 analysis

performed by a region-based senior reactor analyst. The failure of Emergency Diesel

Generator 1-02 was attributed to paint being deposited in a location that caused the EDG

to fail to start on demand. During this supplemental inspection, performed in accordance

with Inspection Procedure 95001, the inspector determined that the licensee identified

the most probable cause of the diesel failure to start, adequately determined the

apparent root cause and significant contributing causes, and established appropriate

corrective actions to prevent recurrence. The licensees evaluation identified that the

most probable cause was a drop of paint that adhered to the fuel pump control rack so as

to keep it from operating as designed. The paint came from a maintenance activity

where the Train B emergency diesel generators in both units were being painted to

improve material condition. The root cause analysis determined that, although there was

no documented evidence that a drop of paint was on the fuel rack at the time of the test,

there was evidence that a drop of paint was there at one time.

- 3 -

Enclosure

REPORT DETAILS

01

INSPECTION SCOPE

The U.S. Nuclear Regulatory Commission (NRC) performed this supplemental

inspection to assess the licensees evaluation associated with a White finding (Train B

Emergency Diesel Generator [EDG]) in the first quarter 2008.

Unit 1 Train B EDG 1-02 failed to start on demand. The primary reason for this finding

being characterized as White was based on the results of a Phase 3 analysis performed

by a region-based senior reactor analyst. The failure of EDG 1-02 was attributed to a

drop of paint being deposited in a location that caused the EDG to fail to start on

demand during a monthly surveillance test on November 21, 2007. Following 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />

of troubleshooting, EDG 1-02 was restored to operable status.

The supplemental inspection was focused on the event occurring since the last

successful surveillance test on EDG 1-02 on October 24, 2007, and when the diesel was

returned to operable status, November 22, 2007, whether root causes and contributing

causes were understood, whether extent of conditions and extent of causes were

identified, and whether sufficient corrective actions were taken to prevent recurrence.

02

EVALUATION OF INSPECTION REQUIREMENTS

02.01 Problem Identification

a.

Determination of who (i.e., licensee, self-revealing, or NRC) identified the issue and

under what conditions

Paint that was deposited and adhered to a fuel rack in a location that prevented Unit 1

Train B EDG 1-02 to start on demand during a monthly surveillance test was

self-revealing. EDG 1-02 was declared inoperable on November 21, 2007.

b.

Determination of how long the issue existed and prior opportunities for identification

The issue existed some time between the last successful test on October 24, 2007, and

the monthly surveillance test failure that occurred on November 21, 2007. EDG 1-02

successfully started and loaded during a surveillance performed on October 24, 2007.

The diesel failed to start during a monthly surveillance test on November 21, 2007,

because the fuel rack on at least one fuel injection pump was bound to the extent that

the entire fuel rack assembly was unable to leave the no fuel position. This was

caused by painting activities on and around the diesel. Painting activities to improve the

appearance of EDG 1-02 started on October 15, 2007, and ended on November 21,

2007. The licensee determined that no root cause was identified; however, it is believed

that the most probable cause of EDG 1-02 failure to start was a paint drop that was not

cleaned off of the 6L fuel pump control rack. This paint drop prevented the operation of

the control rack from moving into the fuel pump and at the same time restricted

operation of all other 15 fuel racks on the EDG 1-02. The failure of this component to

respond to the diesel start prevented the engine from receiving sufficient fuel to run.

- 4 -

Enclosure

The licensee had prior opportunities to identify this condition. The licensee determined

that although there were daily inspections of the engine performed by painters, paint

supervisors and an operations field support supervisor or operations nuclear equipment

operators, paint could still be found on sensitive components. Not only did these

inspections fail to cause this paint to be removed from the sensitive components, but

they also failed to identify the existence of the paint drop on the 6L fuel pump control

rack. This is supported by photographs taken immediately after the event that showed

that some components had paint on them but should have been free of paint according

to a pre-job briefing notebook that was used by painters. This notebook identified

sensitive components that were not to be painted or have paint on them.

The inspector reviewed the records describing the as-found condition of the diesel,

reviewed the tests and analysis performed on EDG 1-02, and discussed the issue with

the dispositioning manager and the diesel system engineer. As a result of these

activities, the inspector agreed that EDG 1-02 failed to start due to paint being deposited

on the diesel fuel rack linkage during painting activities on and around EDG 1-02

between October 24 and November 21, 2007.

c.

Determination of the plant-specific risk consequences (as applicable) and compliance

concerns associated with the issue

The licensee determined that EDG 1-02 was inoperable for a period of time since the

last successful surveillance on October 24, 2007, and November 21, 2008 when EDG 1-

02 was successfully started. On November 7, 2007, the redundant train EDG 1-01 was

being barred over in preparation for its monthly surveillance test. During this 65 minute

period, two trains of emergency power may not have been operable. To account for the

increased risk of the EDG 1-01 being taken out of service for 65 minutes, EDG 1-02 was

assumed to be unavailable (due to the failure on November 21, 2007). Although the

EDG 1-01 was removed from service for a surveillance test, the EDG 1-01 was

considered to be recoverable during a water roll and available during the run portion of

the surveillance. The configuration risk for the period of unsure operability was found to

be risk significant (total of 9.47E-06). It was noted that even if an exposure time 14 days

(T/2) is used, since the actual time that the EDG 1-02 became unavailable is not known,

the configuration risk value would still be risk significant (4.90E-06). A Phase 3 analysis

performed by a Region IV senior reactor analyst determined that the total change in core

damage frequency was 8.93E-6 which is considered comparable to the licensees

results. The analyst used the SPAR model for CPSES (Comanche Peak Steam Electric

Station) to estimate the change in risk associated with internal initiators that was caused

by the finding.

02.02 Root Cause and Extent of Condition Evaluation

a.

Evaluation of methods(s) used to identify root cause(s) and contributing cause(s)

To evaluate this issue, the licensee used a combination of structured root cause analysis

techniques including barrier analysis, confirm refute matrix, and event and casual factor

chart. The inspector determined that the licensee followed its procedural guidance for

performing root cause analysis. The procedural guidance is contained in

Procedure CPSES Cause Analysis Handbook, Revision 10.

- 5 -

Enclosure

b.

Level of detail of the root cause evaluation

The licensees root cause evaluation was thorough and identified the most probable

cause of the Unit 1 Train B EDG 1-02 failure to start on demand during a monthly

surveillance test. This cause was due to a paint drop being deposited on the diesel fuel

rack linkage during painting activities on and around EDG 1-02. This paint drop was not

cleaned off of the 6L fuel injector control rack after painting activities. This paint drop

prevented the operation of the control rack from moving into the 6L fuel pump and at the

same time restricted operation of the other 15 fuel racks on EDG 1-02. The failure of

this component to respond to the diesel start prevented the engine from receiving

sufficient fuel to run. Painting Procedure MSM-G0-0220, General Plant Painting,

Revision 2, allowed a visual inspection for paint or a manual manipulation of the fuel

rack.

In addition, significant contributing causes were identified which included: (1) work

practices of painters and other groups who performed daily paint clean up inspections

failed to identify paint spatter and drops that needed to be cleaned off sensitive engine

components, (2) painters tools and techniques were not completely effective in

preventing paint spatter and drips, (3) the directions in Control Room Alarm

Procedure ALM-1302A, Revision 5, were not specific and due to differences in

interpretation, the time to discover the problem was extended for approximately

8.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, (4) the fuel control shaft break away force was last performed in 1999 and,

due to aging, the licensee believes that this force may have increased because of wear.

This increased force may have contributed to the force it would have taken to overcome

the adhesion of the paint drop.

c.

Consideration of prior occurrences of the problem and knowledge of prior operating

experience

The licensees evaluation included a review to determine if similar problems had

previously been reported with painting activities resulting in inoperability of an EDG. The

review included both internal (Comanche Peak) and external operating experience. An

internal operating experience review determined that no prior experiences were found

associated with mechanical binding of EDG control linkage as a result of painting

activities causing a failure to start of any EDGs. The external operating experience

search returned records where paint was determined to cause the failure to start of

EDGs as a result of gross painting errors (e.g., painting activities causing binding of

control linkages). In several cases, paint was found on fuel metering rods. The licensee

reported that these events differed from the CPSES event because paint was

purposefully applied directly to the control linkages, where at CPSES, the paint was

accidentally splattered or dripped onto the fuel rack. The inspector did not possess any

information to the contrary.

d.

Consideration of potential common cause(s) and extent of condition of the problem

The licensees evaluation considered the potential for common causes and extent of

condition associated with painting activities resulting in inoperability of EDG1-02. The

licensee reported that the extent of condition applied to three other EDGs, but in

particular, the EDG 2-02 which was being painted in a parallel activity at the same time.

The licensees extent of cause evaluation stated that paint can block vent holes, air

pathways, and bind mechanical equipment when it dries. No other vulnerabilities were

- 6 -

Enclosure

identified. The inspector considered the extent of condition and the extent of cause

evaluations to be adequate to address this concern.

02.03 Corrective Actions

a.

Appropriateness of corrective action(s)

After it was identified that EDG 1-02 failed to start on November 21, 2007, the licensee

declared EDG 1-02 inoperable and entered the applicable Technical Specification (TS)

action statement. Troubleshooting and investigating activities were initiated. It was

determined that a paint drop was deposited and remained on at least one fuel rack in a

location that prevented motion required to support the operation of EDG 1-02. The

licensee satisfied the Technical Specification required actions by restoring the EDG to

an operable status on November 22, 2007.

The licensee established corrective actions to prevent recurrence including: (1) develop

and implement procedures to ensure that a maintenance pull test of the fuel rack

mechanisms ensures they are free to operate after painting activities, (2) develop an as

you go inspection and clean up when painting around sensitive components, (3) use

this issue as operational experience in prejob briefing for painters to heighten their

sensitivity to the problems paint drops and spatter can cause for mechanical linkages,

(4) develop a checklist to be used by the painters to perform an inspection of equipment

in applicable areas of the plant, (5) procure paint brushes which can better hold paint

without drips, (6) investigate alternate techniques of painting which would minimize paint

drips and spatter on sensitive engine components, (7) revised diesel failure to start

alarm response procedure that components are free to move by including an action to

manually manipulate the fuel racks, (8) perform a break away force test on a periodic

basis to ensure that the fuel rack operating resistance has not increased to the extent

that could degrade engine response and control, and (9) assess the effectiveness of the

corrective actions to prevent recurrence. The inspector determined that the proposed

corrective actions were appropriate.

b.

Prioritization of corrective actions

The licensees immediate corrective actions restored the EDG 1-02 to operable status

within the Technical Specification allowed outage time. After the EDG was returned to

operable status, the licensee inspected other potentially affected EDGs to assess the

extent of condition. The inspector verified that these inspections did not reveal similar

condition on other diesel generators due to painting activities. The inspector considered

the prioritization of corrective actions to be appropriate.

c.

Establishment of schedule for implementing and completing the corrective actions

The licensee established adequate schedules for completion of the specified corrective

actions. The troubleshooting, investigation, and the return of the EDG 1-02 to operable

status was completed at the earliest opportunity and within the Technical Specification

allowable outage time. The procedure improvements had been completed at the time of

the inspection and incorporated into Procedures MSM-G0-0220, General Plant Painting

Procedure, Revision 2, and ALM-1302A, Alarm Procedure Diesel Generator 1-02

Panel, Revision 5.

- 7 -

Enclosure

d.

Establishment of quantitative or qualitative measures of success for determining the

effectiveness of the corrective actions to prevent recurrence

Smart Form SMF-2008-0000418-00 specified an action to perform an effectiveness

review to determine if corrective actions have corrected the cause of the identified

condition or has created barriers to reduce the frequency and consequences of the

cause of the identified condition to acceptable levels. This action involves performing a

self-assessment to measure the effectiveness of the process changes to ensure future

painting activities around safety-related EDGs do not effect the safety function of the

EDGs. Success criteria are specified in the corrective action plan. This action has a

due date of November 11, 2008. The inspector considered this to be adequate to

determine the effectiveness of the corrective actions to prevent recurrence.

03

MANAGEMENT MEETINGS

Exit Meeting Summary

On June 5, 2008, the inspector presented the inspection results to Mr. R. Flores, Site

Vice President, and members of his staff who acknowledged the findings. The inspector

confirmed that proprietary information was provided or examined during the inspection

and the inspector destroyed this information at the conclusion of the inspection.

ATTACHMENT: SUPPLEMENTAL INFORMATION

- 1 -

Attachment

LIST OF DOCUMENTS REVIEWED

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

M. Blevins, Executive Vice President and Chief Nuclear Officer

M. Bozeman, Supervisor, Emergency Planning

G. Casperson, Interim Manager, Training

H. Davenport, System Engineer

R. Flores, Site Vice President

D. Goodwin, Director, Operations

A. Heap, System Engineer

T. Hope, Manager, Regulatory Performance

R. Kidwell, Licensing Analyst

D. Kross, Plant Manager

F. Madden, Director, Regulatory Affairs

M. McCutchen, System Engineer

E. Meaders, Manager, Outage

J. Mercer, Maintenance Rule Coordinator

G. Merka, Licensing Analyst

J. Meyer, Manager, Nuclear Technical Support

W. Morrison, Interim Director, Nuclear Maintenance

W. Reppa, Manager, System Engineering

J. Skelton, System Engineer

K. Strickland, Supervisor, Nuclear Maintenance

P. Torres, Supervisor, Nuclear Maintenance

C. Tran, Engineering Programs Manager

D. Wilder, Manager, Security, Emergency Planning, and Environmental

H. Winn, System Engineer

NRC

C. Johnson, Chief, Project Branch A, DRP

D. Allen, Senior Resident Inspector, CPSES

B. Tindell, Resident Inspector, CPSES

LIST OF ITEMS, OPENED, CLOSED, AND DISCUSSED

Opened and Closed

None

LIST OF DOCUMENTS REVIEWED

Smartforms/Evaluations

Eval-2007-003253-00

SMF-2004-001177-00

SMF-2004-001884-00

SMF-2006-003157-00

SMF-2007-002401-00

SMF-2007-003035-00

SMF-2008-001905-00

SMF-2008-001906-00

SMF-2008-001908-00

- 2 -

Attachment

SMF-2004-002972-00

SMF-2005-000395-00

SMF-2006-001656-00

SMF-2007-003302-00

SMF-2007-003426-00

SMF-2008-001898-00

SMF-2008-001910-00

SMF-2008-001980-00

Licensee Event Reports

LER 2007-01-00, EDG Failed Surveillance Test Due to Paint on Fuel Injector Control Linkage,

Comanche Peak Unit 1

Procedures

NUMBER

TITLE

REVISION

MSM-GO-0220

General Plant Painting

2

ALM-1302A

Diesel Generator 1-02 Panel

5

MSM-P0-3374

EDG Monthly Run Related Inspections

3

MSM-GO-0216

Protective Coatings

23

OPT-214A

Emergency Diesel Operability Test

19

OWI-104-28

Plant Equipment Operator Diesel Generator 1-02

Operating Log;

11

MSM-GO-0220

Diesel Generator Painting Pre-Job Work Aid

0

STA-202

Nuclear Generation Procedure Change Process

32

OPT 214A

EDG Operability Test

19

ES Cause Analysis Handbook

10

Work Orders

3439601

3439604

4-07-176543

4-07-176545

4-07-276544

5-07-502391

Drawings

Fuel Control Shaft Break Away Force Study dated October 8, 1999

Other

CPSES Operations Logs, dated November 21-22, 2007

Root Cause Analysis, Eval-2007-003253-02-02

TU Electric Office Memorandum; CPSES-9800371; Expectations For Procedure Compliance;

dated February 2, 1998

OE 26026, Unit 1 B-Train EDG Failed to Start at Comanche Peak

- 3 -

Attachment

Information Notices

IN 93-76, Inadequate Control of Paint and Cleaners for Safety-Related Equipment

IN 91-46, Degradation of EDG Fuel Oil Delivery Systems

NRC Inspection Documents

Manual Chapter 0612 Appendix C; Guidance For Supplemental Inspections; June 20, 2003

NRC Inspection Plan - Comanche Peak 95001; INSPECTION FOR ONE OR TWO WHITE

INPUTS IN A STRATEGIC PERFORMANCE AREA; dated May 29, 2008

Inspection Report Numbers 05000445/2008009 and 05000446/2008009

Inspection Procedure 95001, Inspection For One Or Two White Inputs In A Strategic

Performance Area, dated October 16, 2006

NRC Inspection Report

CPSES IR 05000445/2007008 (ML080600164)