05000331/LER-2005-004

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LER-2005-004,
Docket Number
Event date: 09-29-2005
Report date: 11-28-2005
Reporting criterion: 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
3312005004R00 - NRC Website

FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Duane Arnold Energy Center 05000331 YEAR NUMBER� NUMBER

I. Description of Event:

On September 29, 2005, the High. Pressure Coolant Injection (HPCI) system at the Duane Arnold Energy Center was declared inoperable following unsatisfactory venting results of the HPCI system injection piping. This venting was being performed to ensure the discharge piping was filled with water. Specifically, the venting operation was intended to satisfy Technical Specifications (TS) Surveillance Requirement (SR) that the system is full of water (SR 3.5.1.1) and to quantify any air accumulation in the system piping. During HPCI discharge line venting on September 29, 2005, a steady stream of water was not obtained for approximately 30 minutes and therefore, HPCI was declared inoperable for not being able to meet SR3.5.1.1.

II. Assessment of Safety Consequences:

This report is being submitted pursuant to 10CFR50.73(a)(2)(v)(D).

This event did not affect the availability of other systems needed to maintain safe shutdown conditions, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident.

The HPCI system was declared unavailable on three separate occasions between September 29 and October 12. The total unavailability time for HPCI was 102 hours0.00118 days <br />0.0283 hours <br />1.686508e-4 weeks <br />3.8811e-5 months <br />. When HPCI is out of service, core damage frequency (CDF) increases from the base value of 9.148E-06/yr to 1.728E-05/yr. Therefore, the incremental core damage probability (ICDP) was:

(1.728E-05/yr — 9.148E-06/yr) x (102 hrs) x (1 day / 24 hrs) x (1 yr / 365 days) = 9.47E-8 Section 11 of NUMARC 93-01 provides guidance for assessing risk resulting from performance of maintenance activities. Activities for which incremental core damage probability is less than 1.0E-06 are considered to be of minor consequence with regard to plant risk and do not warrant use of specific compensatory measures to reduce risk. The calculated value of ICDP for HPCI being unavailable for 102 hours0.00118 days <br />0.0283 hours <br />1.686508e-4 weeks <br />3.8811e-5 months <br /> is less than this threshold, and the activity is therefore considered to have an inconsequential impact on plant risk.

The value of 9.47E-8 for ICDP is conservative because it is assumed that HPCI was not capable of performing its intended function during the 102 hours0.00118 days <br />0.0283 hours <br />1.686508e-4 weeks <br />3.8811e-5 months <br /> for which it was declared to be unavailable. In fact, it was only incapable of starting automatically. If a valid HPCI initiation signal had occurred during the time it was said to be unavailable, the system could have been initiated manually simply by returning the HPCI Turbine Aux Oil Pump control from its Pull-to-Lock setting to Auto.

FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6 PAGE (3) Duane Arnold Energy Center 05000331 SEQUENTIAL� REVISIONYEAR� NUMBER� NUMBER Therefore, there were no actual safety consequences associated with this event. There was no effect on public health and safety as a result of this event.

This event did result in a Safety System Functional Failure.

III. Cause of Event:

Prior to this event, DAEC had designed a vent rig to vent the HPCI discharge piping with the ability to quantify the amount of non-condensable gases vented. Utilizing a Yi" ball valve, the rig was designed to quantify the volume of non-condensable gases. This configuration allowed for an accurate timing of the vent duration but created a high pressure drop across the ball valve. This vent rig had been successfully used on August 29, 2005. During the next performance of venting on September 29, 2005, a continuous stream of steam was vented from the discharge line for greater than 30 minutes. The only plant change from the August and September venting was the fact that the Condensate Storage Tank (CST), which is the preferred 'suction source for HPCI, was at a lower level in September than in August due to the need to adjust CST chemistry.

Investigation into this event revealed the existence of HPCI discharge piping temperatures higher than the original design. These elevated temperatures result in a steam void at the pipe elbow next to the HPCI discharge valve, MO 2312. As discussed above, the vent rig was designed for venting non-condensable gases, not to remove any existing steam void that may have been present and therefore, a continues stream of water was not achievable due to the fact that steam was being produced at the same rate that it was being vented.

The cause of the elevated temperatures was the fact that thermal energy was being conducted through the inject valve disc to the water on the pump side of the discharge line. This condition resulted in steam being produced on the low-pressure side of MO 2312's valve disc. The thermal energy was bping delivered to MO 2312 via the phenomenon of "turbulent penetration." Therefore, the cause of this event was the fact that the HPCI system was designed with a lack of awareness to the "turbulent penetration" phenomenon and its effect on HPCI discharge piping.

Turbulent penetration (Corkscrew ConveCtion) occurs if a high energy fluid in a large pipe passes across the opening of a smaller brObh pipe to which it is connected. This results in fluid vibrations being induced resulting in eddy currents and thermal transport for a certain distance into the connected branch pipe. Thus, thermal penetration into a vertical line can induce circulation in a connected horizontal line which has stagnant and stratified fluid.

FACILITY NAME (1)� DOCKET NUMBER (2) LER NUMBER (6� PAGE (3) Duane Arnold Energy Center 05000331 YEAR I SEQUENTIAL REVISION NUMBER�NUMBER The thermal energy delivered in this manner can also induce a circulation loop in an isolated volume between two valves. The effect is to deliver thermal energy to a valve which is separated from the high-temperature and high-flow line by an intervening valve.

This is what has been observed at DAEC. Turbulent penetration delivers thermal energy into the vertical section of the HPCI injection line which is connected to the feedwater line. This induces a circulation current that delivers thermal energy to the inject check valve, V23-0049. This in turn induces a circulation current in the space between V23­ 0049 and MO 2312. This has the effect of delivering thermal energy to MO 2312.

Further discussions regarding this phenomenon can be found in IAEA-TECDOC-1361, dated July 2003 and EPRI MRP-32, Thermal Fatigue Monitoring Guidance, dated April 2001.

IV. Corrective Actions:

An operability recommendation (OPR) was completed on October 12, 2005. This OPR concluded that HPCI was operable but degraded and non-conforming based on the following:

The HPCI System is fully capable of performing its safety functions and TS SR 3.5.1.1 is satisfied, as summarized below:

1. The steam volume near the M02312 disk during standby readiness conditions has not cause a detrimental water hammer.

2. The steam volume near the M02312 disk during standby readiness conditions does not delay HPCI injection because it is collapsed when M02312 starts to open.

3. The HPCI quarterly surveillance test (STP 3.5.1-05) was performed on October 11, 2005 while monitoring pipe temperature and movement, in addition to the data from the transient recorder, and no evidence of water hammer was observed.

4. The non-conformance with design specifications for HPCI discharge pipe temperature has been evaluated, with the conclusion that the elevated temperatures have no affect on HPCI operability.

U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

SEQUENTI REVISION

Duane Arnold Energy Center 05000331 YEAR NUMB RAL NUMBER To provide additional assurance that the HPCI discharge piping is filled, the following compensatory measures were implemented and proceduralized:

1. HPCI suction will be lined up to the CST with level of 15 feet (minimum), or the HPCI Keep Fill System will be in service.

2. Periodic venting of the HPCI discharge piping, starting at an increased frequency and then extended out to the TS SR frequency based on experience.

3. Shiftly monitoring of HPCI discharge pipe temperature to assure that the existing void size is not changing.

Additionally, DAEC will perform an analysis of the effects on HPCI discharge piping caused by "turbulent penetration". This action will validate assumptions made in the operability recommendation regarding acceptable void size, minimum CST water level to assure operability, effects of pipe movement with determined void size and collapse under normal and automatic start scenarios, and a past operability determination. This action is due March 17, 2006.

After completion of the analysis, existing Technical Specification SR basis will be reviewed and revised based on the results of the analysis. This action is due April 28, 2006.

EIIS System and Component Codes:

N/A — There were no component failures.

V. Additional Information:

Previous Similar Occurrences:

A review of LERs at the DAEC over the last 3 years identified no LERs with similar events.