ML052280254
| ML052280254 | |
| Person / Time | |
|---|---|
| Site: | Beaver Valley |
| Issue date: | 08/05/2005 |
| From: | Pearce L FirstEnergy Nuclear Operating Co |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| GL-97-002, L-05-134 | |
| Download: ML052280254 (3) | |
Text
FENOC Beaver Valley Power Station P. 0. Box 4 Shippingport, PA 15077 L-05-134 August 5, 2005 Beaver Valley Power Station Unit 1 -Docket No. 50-334, License No. DPR-66 Unit 2-Docket No. 50-412. License No. NPF-73_ -
Monthly Operating Report U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
In accordance with NRC Generic Letter 97-02, "Revised Contents of the Monthly Operating Report", and Unit I and 2 Technical Specification 6.9.4, the "Monthly Operating Report" is submitted for Unit 1 and Unit 2 for the month of July, 2005. This information has also been inputted into the INPO Consolidated Data Entry (CDE) System.
No regulatory commitments are contained in this submittal.
Vice-President BVPS DTJ/cjg Enclosures cc:
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OPERATING DATA REPORT DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE REPORTING PERIC 50-334 Beaver Valley 1 August 01, 2005 David T. Jones 724-682-4962 July 2005
- 1.
Design Electrical Rating
- 2.
Maximum Dependable Capacity (MWe-Net) 835.00 821.00 This Month Yr-to-Date Cumulative
- 3.
Number of Hours the Reactor was Critical 744.00 5,087.00 181,250.14
- 4.
Number of Hours Generator On-line 744.00 5,087.00 178,704.14
- 5.
Reserve Shutdown Hours 0.00 0.00 0.00 6.-Net Electrical Energy Generated (MWHrs) g-o_--- 608,900.00 --
4,222,410.00 -135,542,329.0 UNIT SHUTDOWNS Type Method of F: Forced Duration Shutting Cause & Corrective Action No.
Date S: Scheduled (Hours)
Reason 1 Down 2 Comments NONE.
1 2
Reason:
A.Equipment Failure (Explain)
B Maintenance or Test C
Refueling D
Regulatory Restriction E
Operator Training & License Examination F
Administration G
Operational Error (Explaln)
H Other (Explain)
Method:
1 Manual 2
Manual Trip/Scram 3
Automatic Trip/Scram 4
Continuation 5
Other (Explain)
SUMMARY
The-Unit began the-Teport period -operating at a 'nominal value of-1O0%-output.-On -7/25105-at ---
1332 hours0.0154 days <br />0.37 hours <br />0.0022 weeks <br />5.06826e-4 months <br />, the Unit reduced output byapproximately 0.5% due to high Steam Generator blowdown temperature and elevated hotwell temperature caused by unusually warm atmospheric conditions present. Once plant conditions improved, the Unit was returned to full power at 2020 hours0.0234 days <br />0.561 hours <br />0.00334 weeks <br />7.6861e-4 months <br /> on 7/25/05. The Unit continued to operate at a nominal value of 100% output for the remainder of the report period.
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OPERATING DATA REPORT DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE REPORTING PERIO 50-412 Beaver Valley 2 Aug9us-t 01-,2005 David T. Jones 724-682-4962 July 2005
- 1. Design Electrical Rating
- 2. Maximum Dependable Capacity (MWe-Net) 836.00 831.00 This Month Yr-to-Date Cumulative
- 3. Number of Hours the Reactor was Critical 744.00 4,510.75 130,903.23
- 4. Number of Hours Generator On-line 744.00 4,496.17 130,144.55
- 5. Reserve Shutdown Hours 0.00 0.00 0.00
-6:-Net Electrical-Energy Generated (MWHrs)-=---610,373.00 -- 3,609,995.00 ---102,744,225.0 UNIT SHUTDOWNS Type Method of F: Forced Duration R Shutting Cause & Corrective Action No.
Date S: Scheduled (Hours)
Reason 1 Down 2 Comments NONE.
1 2
Reason:
A Equipment Failure (Explain)
B Maintenance or Test C
Refueling D
Regulatory Restriction E
Operator Training & License Examination F
Administration G
Operational Error (Explain)
H Other (Explain)
Method:
1 Manual 2
Manual Trip/Scram 3
Automatic Trip/Scram 4
Continuation 5'
Other (Explain)
SUMMARY
-The Unit began the report period operating at a nominal value of-100% output:-On-7/23/05 at 0728-hours, output was reduced to approximately 98% in oder to perform planned Turbine valve testing.
Upon completion of satisfactory Valve testing, the Unit was returned to full power at 0947 hours0.011 days <br />0.263 hours <br />0.00157 weeks <br />3.603335e-4 months <br /> on 7/23/05. The Unit continued to operate at a nominal value of 100% output until 7/25/05 when output was incrementally reduced beginning at 1111 hours0.0129 days <br />0.309 hours <br />0.00184 weeks <br />4.227355e-4 months <br /> to an output of approximately 94% due to high hotwell temperature caused by unusually warm atmospheric conditions present. Once atmospheric conditions improved, the Unit was returned to full power at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br /> on 7/25/05. The Unit continued to operate at a nominal value of 100% output until 7/26/05 when output was incrementally reduced beginning at 1355 hours0.0157 days <br />0.376 hours <br />0.00224 weeks <br />5.155775e-4 months <br /> to an output of approximately 95% due to high hotwell temperature caused by unusually warm atmospheric conditions present. Once atmospheric conditions improved, the Unit was returned to full power at 2020 hours0.0234 days <br />0.561 hours <br />0.00334 weeks <br />7.6861e-4 months <br /> on 7/26/05. The Unit continued to operate at a nominal value of 100% output for the remainder of the report period.
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