ML052010109

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June 2005 Monthly Operating Report for Oyster Creek Generating Station
ML052010109
Person / Time
Site: Oyster Creek
Issue date: 07/11/2005
From: Swenson C
AmerGen Energy Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
2130-05-20147, GL-97-002
Download: ML052010109 (2)


Text

e AmerGenlm AmerGen Energy Company, LLC Oyster Creek US Route 9 South, P.O. Box 388 Forked River, NJ 08731-0388 www.exeloncorp.corn An Exelon Company GL 97-02 July 11, 2005 2130-05-20147 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 - 0001 Oyster Creek Generating Station Facility Operating License No. DPR-1 6 NRC Docket No. 50-219

Subject:

Monthly Operating Report - June 2005 Enclosed is the June 2005 Monthly Operating Report for Oyster Creek Generating Station. The content and format of information submitted in this report is in accordance with the guidance provided by Generic Letter 97-02.

If any further information or assistance is needed, please contact David Fawcett at 609-971-4284.

Sincerely, Nwenson Vice President, Oyster Creek Generating Station CNS/DIF Enclosure cc:

S. J. Collins, Administrator, USNRC Region I P. S. Tam, USNRC Senior Project Manager, Oyster Creek R. J. Summers, USNRC Senior Resident Inspector, Oyster Creek File No. 05002



e45, 4'

1.

OPERATING DATA REPORT DOCKET NO.

50 UNIT NAME 01 DATE MI COMPLETED BY TR TELEPHONE REPORTING PERIOD:

-219 yster Creek 1 ly 08, 2005 oger B Gayley

)9) 971-4406 June 2005

1. Design Electrical Rating
2.

Maximum Dependable Capacity (MWe-Net) 650.00 619.00 This Month

3.

Number of Hours the Reactor was Critical 675.97

4.

Number of Hours Generator On-line 666.85

.5 Resere ShutdowniHouris 0.00

6.

Net Electrical Energy Generated (MWHrs) 401,539.00 Yr-to-Date Cumulative 4,298.97 230,778.47 4,289.85 226,460.30 0.00 918.20 2,674,996.00 129,916,720.0 UNIT SHUTDOWNS Type Method of F: Forced Duration Shutting Cause & Corrective Action No.

Date S: Scheduled (Hours)

Reason 1 Down 2 Comments 1FO8 06/0112005 F

53.15 H

3 06/01/2005 - CAP 02005-2337. Reactor scrammed due to apparent load reject.

First Energy closed in bad lightning arrestors inside the Manitou Substation.

This caused a voltage transient on the 230KV system which lead to a generator lockout (from a loss of two of three 230KV lines exiting the substation) and subsequent turbine trip and reactor scram.

SUMMARY

The planned losses for June, which include operating the plant with margin to the license limit and condenser losses, totaled 6,628.9 MWhrs. A forced outage (1 F08) caused by a grid disturbance occurred June 1 at 21:09 Hours and ended June 4 at 02:18 hours. The 53.15-hour forced outage was beyond Plant Management's control, therefore, the lost generation associated with the outage (38,655 MWhrs) is not included in the Forced Loss Rate calculation 1

2 Reason:

A Equipment Failure (Explain)

B Maintenance or Test C

Refueling D

Regulatory Restriction E

Operator Training & License Examination F

Administration G Operational Error (Explain)

H Other (Explain)

Method:

1 Manual 2

Manual Trip/Scram 3

Automatic Trip/Scram 4

Continuation 5

Other (Explain)

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