ML050870319

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Plant Status Report with Handwritten Notations
ML050870319
Person / Time
Site: Point Beach  
(DPR-024, DPR-027)
Issue date: 05/05/2004
From:
Nuclear Management Co
To:
Office of Nuclear Reactor Regulation
References
FOIA/PA-2004-0282
Download: ML050870319 (2)


Text

-, -4 Committed to Nuclear Excetlenc Plant Status Report Plant: Point Beach Nuclear Plant Date: Wednesday, May 05, 2004 Operations Report (Summary of Last 24 Hours of Operations):

Unit I is in refueling shutdown (Mode 6). Unit 2 is at 100% power.

Days Without LTA: 591 Homeland Security Condition: Yellow Unit 1 '

Unit2-PNVR PWR MWE1 MVE PVR PWSR MNNT1 MWNTE Mode Level (Gross)

(Net)

Mode Level (Gross)

(Net) 6 0%

0 0

1 100%

542.1 520.1 Days On Line: 0 Days Since Last Reactor Trip: 292 Days On Line: 166 Days Since Last Reactor Trip: 298

_______Technical pecification Action Conditions -

Item Unit Condition Out of Service Length Tech Expires Responsibility Equip (Hr/Days)

Spec Expected Number RTS Date Date Time Date Time Source I

Out of 5/3/04 2221 Immediate 3.9.2.C No None B. Dungan 5/5/04 Range service.

Expiration Audible Count Rate___

2RC-508, 2

Out of 11/9/03 0749 31 Days 3.6.3.A 5/23/04 1600 M. Rosseau 8/27/04 U2C RMW service.

lOPS 2

Out of 5/3/04 2123 72 Hours TLCO 5/5/04 1700 5/5/04 B. Dungan service 3.7.6 Ma or Equipment Out of Service or Degraded Item Unit Condition Date Time Work Order Number l Due Date Responsibility NONE l

Operational Problems / Concerns Item Unit Condition Actions Needed Due Date Responsibility C-01 Buzzer 0

Buzzer doesn't work, no sound.

Replace buzzer.

5/4/04 J. Helbing 2RC-508, U2C 2

Valve comes off shut seat Coordinate plan with Plant 5/7/04 C. Hill Reactor Makeup momentarily when RMW pump Manager.

Supply starts.

Unit 2, Excess 2

Inadequate excess letdown flow.

Open and inspect, 2CV-285.

5/7/04 N. Stuart Letdown Flow 2RE-215, 2HX-46 Air 2

Elevated indication, temperature 4 step action plan is developed.

5/14/04 B. Carberry Ejector Gas Monitor related.

Scheduled completion is 5/14/04.

2TE-2259, 2P-28B 2

Minor steam leak.

Prepare work package to repair leak 5/7/04 J. Brander SGFP Discharge weekend of 05/22/04.

Temperature Element WO Initiation Tag #204297 l ___________________

A ggregate Review of Issues

-_-___-_-_-_-_:_-a

___- _ :-_ l N

Item j Unit j Condition j

Actions Planned Due Date lResponsibility lNONEl lllll

'e 8g, Page 1 of 2

Committed to Nuclear Excellence Plant Status Report Reportable Events Inadvertent TSAC 3.9.2.C, Source Range Audible Count Rate

-Outstanding Operability Determinations NONE Protected Equipment 2P-29, Aux Feedwater Turbine-Driven Pump I P-38A/B Aux Feedwater Motor-Driven Pump I P-32A,B,C,D,E,F Service Water Pumps I K-2A/B Instrument Air Compressors I K-3A/B Service Air Compressors I G-021G-03/G-04 Emergency Diesel Generators / Unit 1 Nozzle Dam Panels and Associated Equipment Load Changes (Planned or Unplanned)

NONE Reactor Coolant System Leakage Unit 1 Unit 2 Unidentified (gpm) 0 0.12 (No leak rate determined due to draindown)

Identified (gpm) 0 0.03 Major Tests and Evolutions Scheduled in Next 24 Hours Unit 2, 2RMP 9071-1, 2RMP 9071-2, Train A/B undervoltage relays.

Unit 2, 21CP 2. 1, reactor protection and safeguards analog. (White)

Unit 2, 2P-I A, component cooling water pump maintenance.

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