ML040220282

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Firstenergy Nuclear Operating Company Public Meeting Presentation Davis-Besse Nuclear Power Station
ML040220282
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 01/21/2004
From: Myers L
FirstEnergy Nuclear Operating Co
To:
Office of Nuclear Reactor Regulation, NRC/RGN-III
References
Download: ML040220282 (27)


Text

January 21, 2004 Davis-Besse Nuclear Power Station 1

IMC 0350 Meeting Davis-Besse Nuclear Power Station

January 21, 2004 Davis-Besse Nuclear Power Station 2

Desired Outcomes

  • Demonstrate that Davis-Besse continues to take conservative actions needed to support safe plant restart
  • Provide information on changes in leadership and programs that ensure fleet consistency in Conduct of Operations
  • Demonstrate the Operations Improvement Action Plan supports meeting Industry Standards
  • Provide information on the NOP restart assessment Lew Myers Chief Operating Officer - FENOC

January 21, 2004 Davis-Besse Nuclear Power Station 3

Meeting Agenda Lew Myers Chief Operating Officer - FENOC

  • Update of Plant Activities...Lew Myers
  • Plant Status...Mark Bezilla
  • Operations IssuesBarry Allen
  • Operations Performance.Kevin Ostrowski

January 21, 2004 Davis-Besse Nuclear Power Station 4

Update of Plant Activities Lew Myers Chief Operating Officer - FENOC

January 21, 2004 Davis-Besse Nuclear Power Station 5

  • Successful plant heat-up completed January 5
  • Plant was stabilized at NOP for ~ 3 days
  • Three Administrative Control issues were identified
  • An emergent AFW issue required plant cool-down
  • Successful plant cool-down completed January 9
  • COO requested deferral of RRATI Team inspection
  • Plant equipment issues being resolved
  • Administrative Control issues being resolved
  • Preparing for plant heat-up this weekend Davis-Besse is Progressing Toward Restart

January 21, 2004 Davis-Besse Nuclear Power Station 6

Management Changes

  • Effective Saturday, January 10, 2004 new management assignments were made to strengthen leadership team

-Kevin Ostrowski is the new Manager of Plant Operations

-SRO License, Shift Supervisor, Operations Manager and Plant Manager at Beaver Valley

-Director of Nuclear Maintenance and Nuclear Services at Perry

-Regulatory Affairs Manager at Davis-Besse

January 21, 2004 Davis-Besse Nuclear Power Station 7

Management Changes

-Dave Imlay is the new Shift Superintendent of Plant Operations

-Holds SRO license at Davis-Besse

-Superintendent of Maintenance

-Fifteen years experience at Davis-Besse

-Held various management positions in Operations, Training and Maintenance

-Has experience at other nuclear plants

January 21, 2004 Davis-Besse Nuclear Power Station 8

Management Changes

-Bill Mugge is the new Manager of Work Management

-Holds SRO license at Davis-Besse

-Seventeen years of experience at Davis-Besse and has held various management positions in Operations, Training and Security

-Served as an industry evaluator at INPO

January 21, 2004 Davis-Besse Nuclear Power Station 9

Plant Status Mark Bezilla Vice President

January 21, 2004 Davis-Besse Nuclear Power Station 10

  • Various Turbine Building Doors
  • Formed Mode 2/1 Look Ahead Team Recent Items Addressed for Heat-up Reactor Coolant Valve

January 21, 2004 Davis-Besse Nuclear Power Station 11

  • Current plant status

-Mode 4 (~ 250 psig/~ 260 0F)

-Two Reactor Coolant Pumps inservice

-Other two Reactor Coolant Pumps ready for operation

-Steam Generators removing heat

-Secondary plant in service with Condenser vacuum

-Plant safety systems ready to support Mode 3/NOPT

-Presently reinforcing nine Turbine Building doors Davis-Besse Materiel Condition Will Support Safe Restart

January 21, 2004 Davis-Besse Nuclear Power Station 12

  • Conclusion

-The material condition of the plant will support safe restart

-As issues arise, they will be addressed using our Corrective Action Program with a focus on improving the margins of safety Davis-Besse Materiel Condition Will Support Safe Restart

January 21, 2004 Davis-Besse Nuclear Power Station 13 Operations Issues Barry Allen Plant Manager

January 21, 2004 Davis-Besse Nuclear Power Station 14

  • Detail of Operations work schedule
  • One Technical Specification log entry not made
  • One Technical Specification Action not taken Administrative Control Issues Identified in Mode 4/3

January 21, 2004 Davis-Besse Nuclear Power Station 15

  • FENOC Root Cause Team formed to evaluate Davis-Besse operational issues against FENOC and industry standards

-Assess the issues

-Determine the causes

-Recommend corrective actions

  • Eighteen member team assembled

-Sponsor: Jim Powers, Davis-Besse Engineering Director

-Team Members, included:

-Team Lead: Russ Kearney, Perry Operations Manager

-Pete Sena, Beaver Valley Operations Manager

-George Storolis, Mike Mouser from Beaver Valley Shift Manager

-Ray Hruby, Manager at Beaver Valley

-Thomas Veitch, FENOC Operations Program Manager Plant Manager Actions

January 21, 2004 Davis-Besse Nuclear Power Station 16

  • Inconsistent implementation of the work control and surveillance test programs
  • Inconsistent reinforcement of Operating staff roles and responsibilities
  • Ineffective correction of some performance deficiencies Root Causes

January 21, 2004 Davis-Besse Nuclear Power Station 17

  • Chartered high-impact team to assess the differences in Conduct of Operations among FENOC plants and industry
  • Strengthened Administrative Controls in Operations
  • Changes in Operations Leadership
  • Implemented Shift Manager Peer Verifiers to provide effectiveness review of Operator Actions
  • Assigned managers to monitor specific corrective actions
  • Added detailed Operations activities into plant integrated schedule Actions Taken

January 21, 2004 Davis-Besse Nuclear Power Station 18 Barriers Strengthened to Prevent Events FENOC Vision:

People with a strong safety focus delivering top fleet operating performance Competent Individual Independent Oversight Experienced Management Strong Programs

January 21, 2004 Davis-Besse Nuclear Power Station 19 Operations Performance Kevin Ostrowski Manager - Plant Operations

January 21, 2004 Davis-Besse Nuclear Power Station 20

  • Charter from Management - COO / VP / Plant Manager
  • Assessment of Operations
  • Strengthened controls and accountability for strict compliance in the implementation of Conduct of Operations
  • Corrective Actions effectiveness assessment during NOP Changes in Operations Leadership and Programs

January 21, 2004 Davis-Besse Nuclear Power Station 21 Safety-focused plant operation through consistent implementation of a rigorous Conduct of Operations Charter from Management

January 21, 2004 Davis-Besse Nuclear Power Station 22

  • Assessment tools

-Operations Improvement Plan Assessments

-Feedback from management observers

-Face to face communications and observations Assessment of Operations

January 21, 2004 Davis-Besse Nuclear Power Station 23

  • Initial Observations

-Improved performance in most recent heat-up and cool-down

-Improved organizational leadership by Shift Managers

-Noted improvements in shift turnover, pre-job briefs, and log entries

-Shift Managers engaging the organization in plant issues

-Strict adherence to plant procedures

-Operated the plant consistent with training

-A few areas of Conduct of Operations did not meet fleet standards

-Inconsistencies in ownership and accountability Assessment of Operations

January 21, 2004 Davis-Besse Nuclear Power Station 24

  • Reactor Operators co-sign for authorization of maintenance on safety instrumentation
  • Peer checks on Technical Specification (TS) actions
  • Improved turnover of TS actions
  • Improved log entries for TS
  • Operations management briefings
  • Use of peer reviewers
  • Individual accountability handled in accordance with FENOC policies Conduct of Operations Corrective Actions

January 21, 2004 Davis-Besse Nuclear Power Station 25

  • Corrective Actions support heat-up
  • Operations performance during NOP assessment period will confirm our effectiveness Effectiveness of Corrective Actions

January 21, 2004 Davis-Besse Nuclear Power Station 26 Closing Comments Lew Myers Chief Operating Officer - FENOC

  • We continue to implement our Return to Service and Operations Improvement Action Plan
  • Plant materiel condition is good
  • Improved operator performance was demonstrated during heat-up and cool-down of plant
  • Strong actions have been taken to ensure consistent implementation of conduct of operations activities

January 21, 2004 Davis-Besse Nuclear Power Station 27 Closing Comments

  • NOP Assessment Criteria

-No inadvertent safety system actuations...

-No significant events...

-No integrated plant operating procedure content errors...

-No unplanned entry into technical specification...

-Consistent implementation of Conduct of Operations...

-Actions taken by management show an improving trend...

-Work implementation schedule adherence at 90% or above...

-Risk profile matches the schedule

  • Satisfaction of this criteria will result in FENOC requesting restart