ML032300442
| ML032300442 | |
| Person / Time | |
|---|---|
| Site: | Davis Besse |
| Issue date: | 08/12/2003 |
| From: | FirstEnergy Corp |
| To: | Office of Nuclear Reactor Regulation, NRC/RGN-III |
| References | |
| IMC 0350 | |
| Download: ML032300442 (4) | |
Text
August 12, 2003 Davis-Besse Nuclear Power Station 1
IMC 0350 Meeting Davis-Besse Nuclear Power Station
August 12, 2003 Davis-Besse Nuclear Power Station 2
Meeting Agenda
- High Pressure Injection Pumps......Bob Schrauder
- Electrical Distribution System........Jim Powers
- Plant Readiness for Mode 4......Mark Bezilla
- Operations Start-Up Plan.....Rick Dame
- Restart Milestones/Actions...........Mark Bezilla
- Safety Culture Assessment Results and Readiness for Mode 4/3.
.....Lew Myers
- Quality Assurance Oversight.....Steve Loehlein Lew Myers Chief Operating Officer - FENOC
August 12, 2003 Davis-Besse Nuclear Power Station 3
High Pressure Injection Pumps Bob Schrauder Director - Support Services
August 12, 2003 Davis-Besse Nuclear Power Station 4
Desired Outcome
- Provide you with an understanding of our solution path for the High Pressure Injection Pumps. This solution assures the Davis-Besse HPI pumps will be operable for all conditions
August 12, 2003 Davis-Besse Nuclear Power Station 5
- Topics
-Defense-in-Depth Design Solution
-Project Progress
-Key Preliminary Test Findings
-Final Test Loop Criteria
-Project Completion Plans High Pressure Injection Pumps High Pressure Injection Pump
August 12, 2003 Davis-Besse Nuclear Power Station 6
- Use Defense-in-Depth Approach Increases Safety Margin
-Incorporates and improves hydrostatic bearing design qualified by Pump Guinard and used as the standard design in French PWRs
-Locates bearing supply line on discharge side of impeller to reduce concentration and size of debris reaching hydrostatic bearing
-Use 50 or 90 mil strainer to protect hydrostatic bearing orifices
-Includes escape grooves in hydrostatic bearing to allow debris to exit pockets and prevent plugging
-Hardface all critical wear surfaces: wear rings, bushing, hydrostatic bearing High Pressure Injection Pumps
August 12, 2003 Davis-Besse Nuclear Power Station 7
- Project Progress
-Modification design concept developed and preliminary verification testing performed
-Verification testing provided information to finalize design and properly characterize debris loading for qualification testing
-Currently, optimizing design and finalizing the qualification test criteria High Pressure Injection Pumps
August 12, 2003 Davis-Besse Nuclear Power Station 8
- Preliminary Test Findings
-Debris larger than hydrostatic bearing clearance can become lodged in bearing pockets, plugging pockets
-Fibrous material in significant quantities is problematic for tight clearances and strainer performance
-Unrealistic LBLOCA debris characterization combined with SBLOCA pump flow resulted in excessive debris loading High Pressure Injection Pumps
August 12, 2003 Davis-Besse Nuclear Power Station 9
Original Hydrostatic Bearing Unmodified High Pressure Injection Pumps
August 12, 2003 Davis-Besse Nuclear Power Station 10 Original Hydrostatic Bearing with Grooves High Pressure Injection Pumps
August 12, 2003 Davis-Besse Nuclear Power Station 11 Hydrostatic Bearing High Pressure Injection Pumps
August 12, 2003 Davis-Besse Nuclear Power Station 12 Volute with Strainers on Discharge Side of Impeller High Pressure Injection Pumps
August 12, 2003 Davis-Besse Nuclear Power Station 13
- Final Qualification Test Criteria
- Conservative and realistic approach matches pump operation requirements with debris generation conditions
- Limiting case is long-term operation at boron precipitation control flow rate (250 gpm) following a LBLOCA (i.e., LBLOCA debris)
- Based on verification test results, nearly all fibrous insulation removed from containment and from test loop
- Revised debris transport analysis to account for settling of concrete particles in sump and low flow areas High Pressure Injection Pumps
August 12, 2003 Davis-Besse Nuclear Power Station 14
- Project Completion Plans
- HPI pumps returned to site unmodified for Normal Operating Pressure test
- Test loops being modified for qualification testing
- Qualification test debris characterization being finalized
- Qualification testing to begin in late August
- Pump Guinard hydrostatic bearing design being adapted and improved for Davis-Besse HPI pumps
- Hardfaced replacement parts ordered
- Final pump modifications to be made following Normal Operating Pressure test High Pressure Injection Pumps
August 12, 2003 Davis-Besse Nuclear Power Station 15 Jim Powers Director - Engineering Electrical Distribution System
August 12, 2003 Davis-Besse Nuclear Power Station 16
- ETAP is a state-of-the-art computer software program used to model the effects of plant transients on the electrical distribution system
- Results evaluated to ensure electrical distribution system has sufficient capacity and capability to accomplish plant safety functions
- Implement design modifications to improve voltage of essential busses and increase safety margin Electrical Distribution System
August 12, 2003 Davis-Besse Nuclear Power Station 17
- Operability Evaluation for first Mode 4
- Use Administrative Controls for Technical Specifications Degraded Voltage Relay Setpoint Change
- Limit non-essential loads to prevent voltage degradation
- Require two qualified off-site to on-site circuits to be operable
- Require grid voltage restrictions Electrical Distribution System
August 12, 2003 Davis-Besse Nuclear Power Station 18
- Project Status
- Finalize grid voltage criteria
- Implement modifications to eliminate restriction on non-essential loads Electrical Distribution System
August 12, 2003 Davis-Besse Nuclear Power Station 19 Plant Readiness for Mode 4/3 Mark Bezilla Vice President/Plant Manager
August 12, 2003 Davis-Besse Nuclear Power Station 20 Purpose
- Discuss Plant Readiness for Mode 4/3 and introduce the Restart Test Plan Manager responsible for the Start-Up Plan
August 12, 2003 Davis-Besse Nuclear Power Station 21
- Demonstrated confidence in plant systems and equipment
- Primary systems
- Pressurized reactor coolant system
- Ran reactor coolant pumps
- Conducted 50 psig (May 6) and 250 psig (May 25) Leak Tests
- Containment closure (July 3)
- Secondary systems
- Exercised Circulating Water, Condensate, Feedwater Systems
- Established Main Condenser Vacuum
- Plant modifications
- Human performance
- Preparation for Mode 4/3 Test Plant Readiness for Mode 4/3
August 12, 2003 Davis-Besse Nuclear Power Station 22
- Restart Test Plan Manager is Rick Dame
- Graduate of Ohio State University (B.S. Mechanical Engineering)
- 18 years nuclear experience (Perry Nuclear Power Plant)
- Previously Licensed Senior Reactor Operator
- Experienced in Start-up Testing, System Engineering, Functional Leakage Testing, and ASME Section XI Test Programs
- Project Manager for RFO Plant Shutdown and Startup Sequences Plant Readiness for Mode 4/3
August 12, 2003 Davis-Besse Nuclear Power Station 23 Rick Dame Reliability Unit - Supervisor Operations Start-Up Plan
August 12, 2003 Davis-Besse Nuclear Power Station 24 Operations Start-Up Plan
- Role of Restart Test Plan Manager
-Assist Operations Staff in detailing existing Restart Plan
-Will serve as a direct report to the Operations Manager who is responsible for approval and implementation of the plan
-During the organizational readiness assessments, will be a direct report to the FENOC Chief Operating Officer
August 12, 2003 Davis-Besse Nuclear Power Station 25 Operations Start-Up Plan
- Objectives of plan
- Conduct Plant startup safely and event-free
- Successfully perform required post-maintenance and modification testing
- Assess organizational readiness to effectively implement Plant processes when challenged by any emergent issues
August 12, 2003 Davis-Besse Nuclear Power Station 26 Operations Start-Up Plan
- Initial Observations
- Operations Staff is well-trained, experienced, and competent
- Innovative simulator training for Plant heat-up has been completed
- Material condition of Plant is very good
- Equipment that has been returned to service has performed well
August 12, 2003 Davis-Besse Nuclear Power Station 27 Operations Start-Up Plan
- Conduct Plant start-up safely and event-free
- Detailed activity plan (Initial Mode 4 to 100 percent power)
- Operator start-up task assignments and expectations
- Plan includes 7 day rated pressure/temperature Reactor Coolant System (RCS) Integrity Test
- All key activities will have dayshift/nightshift owners
- Engage entire organization in support of Operations
- 24/7 Management oversight throughout start-up sequence
August 12, 2003 Davis-Besse Nuclear Power Station 28 Operations Start-Up Plan
- Successfully conduct required post-maintenance and modification testing (PMTs)
- Ownership of retests (Roles and responsibilities of Maintenance/Engineering/Radiation Protection)
-PMTs assigned with Owner
- Vigilant monitoring of equipment
- Contingency plans
- We will exercise effective operational decision making principles if unexpected results are encountered
August 12, 2003 Davis-Besse Nuclear Power Station 29 Operations Start-Up Plan
- Organizational readiness to effectively implement Plant processes when faced with an emergent issue
- Employ techniques used at peer stations to improve Plant operational focus/Operations leadership
- Conduct emergent issue exercises during 7 day RCS Integrity Test (Procedure changes, equipment issues, Significant Root Cause Reports, use of Problem Solving Nuclear Operating Procdure)
- Assess organizational performance
August 12, 2003 Davis-Besse Nuclear Power Station 30 Restart Milestones/Actions Mark Bezilla Vice President/Plant Manager
August 12, 2003 Davis-Besse Nuclear Power Station 31 Restart Milestones/Actions
- Four nozzles removed from original reactor vessel head and sent to Pacific Northwest National Laboratory in Washington (August 2003)
Framatome ANP and NPS Employees Remove Nozzles
August 12, 2003 Davis-Besse Nuclear Power Station 32
- Transitioning from Return to Service Plan to normal processes
- Installation of HPI Pumps
- Completing remaining work required for Mode 4/3
- Perform 7 day Full Pressure Test of Reactor Coolant System
- Execute Restart Test Plan
- Return to Mode 5 and assess results Restart Milestones
August 12, 2003 Davis-Besse Nuclear Power Station 33
- Items completed to date
-62 Modifications
-7763 Work Orders
-6242 Condition Report Evaluations
-6582 Corrective Actions Restart Actions for Mode 4/3
August 12, 2003 Davis-Besse Nuclear Power Station 34
- 31 Checklist Items
-16 Complete
-5 Restart Actions Complete/Inspection in Progress
-3 Waiting Plant Conditions to Complete
-6 Restart Actions in Progress
-1 Closure of Confirmatory Action Letter NRC 0350 Oversight Panels Restart Checklist
August 12, 2003 Davis-Besse Nuclear Power Station 35 Results of Safety Culture Assessment and Readiness for Mode 4/3 Lew Myers Chief Operating Officer - FENOC
August 12, 2003 Davis-Besse Nuclear Power Station 36 That assembly of characteristics and attitudes in organizations and individuals which establishes an overriding priority towards nuclear safety activities and ensures that issues receive the attention warranted by their significance.
Safety Culture
August 12, 2003 Davis-Besse Nuclear Power Station 37 Recent Safety Culture Assessment
- In July, Management team completed a two day assessment of Safety Culture in preparation of Mode 4/3
-Each Safety Culture commitment area was assessed
- Assessment oversight received
-Independent Industry Experts
-Company Nuclear Review Board Member
-Restart Overview Panel Member
-Quality Assurance
August 12, 2003 Davis-Besse Nuclear Power Station 38 Recent Safety Culture Assessment Safety Culture Safety Culture Individual Commitment Area Plant Management Commitment Area Policy or Corporate Level Commitment Area Goals, Roles and Teamwork Ownership and Accountability Qualification and Training Commitment to Continuous Improvement Questioning Attitude Rigorous Work Control and Prudent Approach Open Communications Statement of Safety Policies Management Value Structure Resources Self Assessment Commitment to Safety Drive for Excellence Nuclear Professionalism Independent Oversight Cross-Functional Work Management
& Communication Environment of Engagement and Commitment Color Key All major areas are accept-able with a few minor indi-cator deviations All major areas are accept-able with several indica-tors requiring prompt man-agement action All major areas are accept-able with a few indicators requiring management at-tention Several major areas do not meet acceptable standards and require immediate management action
August 12, 2003 Davis-Besse Nuclear Power Station 39 Barriers to Assure Safety Independent Oversight Management Programs Individual Breakdown Breakdown Breakdown Breakdown
August 12, 2003 Davis-Besse Nuclear Power Station 40
- Enhanced Quality Assessment Organization
- Vice President Oversight
- Company Nuclear Review Board Rechartered
- Nuclear Committee of the Board
- Quality Control Realignment
- Safety Conscious Work Environment Program
- Employee Concerns Program
- INPO Assist Visits
- Restart Overview Panel
- Quality Assurance Quarterly Assessment
- Safety Culture Assessment Accomplishments Independent Oversight
August 12, 2003 Davis-Besse Nuclear Power Station 41
- New Leadership Team
- Management Alignment
- Improved Operational Focus
- Management Observation Program
- Safety Conscious Work Environment Review Team
- Added and Realigned Resources
- Engineering Assessment Board
- Improved Regulatory Affairs Rigor
- Safety Culture Assessment Process
- Elevated Project Review Committee
- Leadership In Action Continuous Training Accomplishments Management
August 12, 2003 Davis-Besse Nuclear Power Station 42
- Operating Experience Program
- Corrective Action Program
- Boric Acid Control Program
- Integrated RCS Leak Rate Program
- In-Service Inspection Program
- Modification Program
- Radiation Protection Program
- Engineering Program Reviews (65)
- On-going Program Review Procedure
- Latent Issues Reviews
- System Health Reviews
- On-line Risk Procedure
- Problem-solving/Decision Making Accomplishments Programs
August 12, 2003 Davis-Besse Nuclear Power Station 43
- 50.9 Training
- Safety Conscious Work Environment Training
- Operability Evaluation Training
- Corrective Action Program Training
- Root Cause Training
- Ownership for Excellence Development Plans
-Nuclear Safety
-Nuclear Professionalism Development
- SRO Training
- Case Study
- Standards /
Expectations
- Plant Access Training Accomplishments Individual
August 12, 2003 Davis-Besse Nuclear Power Station 44 Barriers to Assure Safety FENOC Vision FENOC Vision:
People with a strong safety focus delivering top fleet operating performance
August 12, 2003 Davis-Besse Nuclear Power Station 45 Quality Assurance Oversight Steve Loehlein Manager - Nuclear Quality Assessment
August 12, 2003 Davis-Besse Nuclear Power Station 46
- Station Readiness
- Quality Assessment Organization Readiness
- Planned Oversight Activities Quality Assessments
August 12, 2003 Davis-Besse Nuclear Power Station 47 Station Readiness for Mode 4/3
- Readiness of Systems/Equipment
-Using Continuous Assessment Process to monitor performance and document concerns
-Readiness will be established through completion of required restart activities
August 12, 2003 Davis-Besse Nuclear Power Station 48 Station Readiness for Mode 4/3
- Readiness of Corrective Action Program
- Corrective Action Review
- 5402 completed Corrective Actions were reviewed
- 4980 (92%) acceptable
- 422 (8%) inconclusive/unacceptable
- Documentation errors (3.8%)
- Documentation linkage to action not clear (4.2%)
- Condition Reports (CRs) were issued for these cases
- Conclusion
- Pending outcome of new CRs, in general, issues were not lost, but documentation of activities needs improvement
August 12, 2003 Davis-Besse Nuclear Power Station 49 Station Readiness for Mode 4/3
- Focused Assessment of Corrective Action Program
- Examined program since March, 2003
- Interviews of managers, analysts, and other personnel
- Oversight of the Corrective Action Review Board and Management Review Board
- Sampled CRs for quality of work, and compliance with procedure
- Sampled rollovers to check that they had been performed correctly
August 12, 2003 Davis-Besse Nuclear Power Station 50 Station Readiness for Mode 4/3
- Conclusions
- Corrective Action Program is currently Satisfactory in finding and fixing identified problems
- Trending needs to be effectively implemented for the future
- Improvement is needed in the use of Performance Indicators
- Organization needs to continue to emphasize improvement in implementation
August 12, 2003 Davis-Besse Nuclear Power Station 51 Station Readiness for Mode 4/3
- Readiness of Plant Staff
- Ongoing assessments of safety culture
- Ongoing assessments of department activities
- Operations
- Radiation Protection
- Engineering
- Maintenance
- Training
August 12, 2003 Davis-Besse Nuclear Power Station 52 Quality Assessment Organization Readiness for Mode 4/3
- Organizational Readiness
- Quality Assurance (QA) has completed corrective actions in response to Root Cause and Detailed Program Review
- Implemented Organizations Structural Independence
- Enhanced oversight of QA by Company Nuclear Review Board
- Responded to weaknesses in Assessment Program and Assessor performance
- Strong relationship established with Management
- V.P. - Oversight meets regularly with Board of Directors
- Site management support of Quality Assessments is evident
August 12, 2003 Davis-Besse Nuclear Power Station 53 Oversight Activities for Mode 4/3
- Assessment Plan for Restart Activities
- Continue Assessment of Return to Service Plan Activities
- Adjusting Assessment Activities based on Organizations activities and plant conditions
- Mode 4 Assessment Activities include:
- Control Room Activities
- Field Activities
- Organizational Response to Emergent Issues
- Training Activities
- Oversight of Restart Test Plan Activities
August 12, 2003 Davis-Besse Nuclear Power Station 54 Closing Comments Lew Myers Chief Operating Officer - FENOC