ML031770219

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Firstenergy Nuclear Power Company Public Meeting Presentation with NRC Davis-Besse Nuclear Power Station
ML031770219
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 06/03/2003
From:
FirstEnergy Nuclear Operating Co
To:
Office of Nuclear Reactor Regulation
References
Download: ML031770219 (64)


Text

June 3, 2003 Davis-Besse Nuclear Power Station 1

IMC 0350 Meeting Davis-Besse Nuclear Power Station

June 3, 2003 Davis-Besse Nuclear Power Station 2

Desired Outcome

  • Provide an Update on Plant Performance and Management

& Human Performance Progress Since the Last Meeting

  • Provide Information Concerning Decision on the High Pressure Injection Pump
  • Provide an Update on the Quality Oversight Perspective
  • Provide Status on Several Engineering Design Issues
  • Status our Overall Schedule and Performance Indicators Lew Myers FENOC Chief Operating Officer

June 3, 2003 Davis-Besse Nuclear Power Station 3

Meeting Agenda Pressure Test Results; Containment Closure...Mark Bezilla Management & Human Performance Plan Update....Lew Myers Electrical Distribution; SFAS Relays.....Jim Powers HPI Pump Modification; Corrective Action Program Performance.....Bob Schrauder Quality Assessment Activity..Steve Loehlein Remaining Issues Focus.....Mike Ross Schedule MilestonesMike Stevens Restart Action Performance...Clark Price

June 3, 2003 Davis-Besse Nuclear Power Station 4

Reactor Coolant System Pressure Tests and Containment Closure Mark Bezilla Vice President/Plant Manager

June 3, 2003 Davis-Besse Nuclear Power Station 5

Desired Outcome

June 3, 2003 Davis-Besse Nuclear Power Station 6

  • Completed 50 psig Leak Test - May 6, 2003
  • Completed 250 psig Leak Test - May 25, 2003
  • Accomplishments:

- Determined that we could only heat up the Reactor Coolant System (RCS) due to decay heat, to <140 degrees

- Placed Makeup and Purification System in service

- Verified Pressurizer Heaters and spray functions

- Ran each Reactor Coolant Pump

- Gained confidence in the performance of the RCS and support systems Reactor Coolant System Pressure Tests

June 3, 2003 Davis-Besse Nuclear Power Station 7

  • Containment Health Actions
  • Containment Work
  • Containment Closure
  • Containment Ownership Turnover from Containment Health to Operations Containment Closure

June 3, 2003 Davis-Besse Nuclear Power Station 8

Management & Human Performance Plan Update Lew Myers FENOC Chief Operating Officer

June 3, 2003 Davis-Besse Nuclear Power Station 9

Desired Outcome

  • Demonstrate Strong Actions Taken to Date to Address Management and Human Performance
  • Demonstrate Plan for Site Alignment and Leadership Going Forward Management & Human Performance Plan Update

June 3, 2003 Davis-Besse Nuclear Power Station 10 Actions to Date

  • FENOC Corporate Organization Changes
  • Davis-Besse Management Changes
  • Independent Quality Assessment Organization
  • Established and Communicated Standards
  • Added/Enhanced Internal Oversight Groups

- Engineering Assessment Board

- Project Review Committee

- Corrective Action Review Board

- Management Review Board Management & Human Performance Plan Update

June 3, 2003 Davis-Besse Nuclear Power Station 11 Actions to Date (continued)

  • Added/Enhanced External Oversight Groups

- Restart Overview Panel, Company Nuclear Review Board

  • Improved Corrective Action Program and Oversight
  • Management Observation Program
  • All-hands Case Study Training
  • Leadership Team Training Management & Human Performance Plan Update

June 3, 2003 Davis-Besse Nuclear Power Station 12 Actions to Date (continued)

  • Employee Concerns Program Improvements
  • Increased Technical Rigor

- Calculation Program

- FENOC Problem Solving and Decision Making Nuclear Operating Procedure

- Operability Evaluations Management & Human Performance Plan Update

June 3, 2003 Davis-Besse Nuclear Power Station 13 Actions to Date (continued)

  • Initiated Several Employee Communication Mechanisms Cs, Town Hall & All-hands meetings
  • Section Specific Improvement Initiatives
  • Developed Performance Indicators for Monitoring Performance Management & Human Performance Plan Update

June 3, 2003 Davis-Besse Nuclear Power Station 14 That assembly of characteristics and attitudes in organizations and individuals which establishes an overriding priority towards nuclear safety activities and that these issues receive the attention warranted by their significance.

Management & Human Performance Plan Update FENOC Definition Safety Culture

June 3, 2003 Davis-Besse Nuclear Power Station 15 That part of a Safety Culture addressing employee willingness to raise issues and managements response to these issues.

Management & Human Performance Plan Update FENOC Definition Safety Conscious Work Environment

June 3, 2003 Davis-Besse Nuclear Power Station 16 Management & Human Performance Plan Update Site Integration Plan: May-December 2003 Timeline Site Alignment and Leadership Development Interventions May -

July Response to Haber Report Interviews with SMT members and Managers Transition / Restart Plan Work Management Safety-Focus Process Development Plans for Directors and Managers -- completed and approved Exelon Benchmark Management Observation Prog.

Improvement Rollout Focus on Safety as a Leadership Team 3-Day SMT Intervention (Haber Report Review) 3-Day Intervention w/Mgrs 360° Feedback (SMT and Mgrs)

Fill Open Supv. Positions Form Design Team for Cross-functional 1-day all-site trg One-on-One Coaching Starts with SMT Members and Managers Facilitative Leadership Training?

SCWE Training Cross-functional 1 day all-site training day August -

September 1-2 Day Intervention with both SMT and Managers All-Leadership Session - Supvs.

Bi-monthly FENOC internal Safety Culture Tool -- format to use post restart Assessment Process for internalizing capabilities to assess supervisors Form Cross-Functional Design Team for 2-Day All-Site Large Scale Meeting 1 - Day SMT Follow Up Intervention 1 - Day Managers Follow Up Intervention Reinstate MRM, Business Plan, Performance Indicators 2 - Day All Site Large Scale Meeting (Vision Map?)

Leadership Academy for SMT and Managers (Pilot?)

Long-term Safety Culture Improvement Plan October -

December 1 - Day SMT Follow Up Intervention 1-Day Managers Follow Up Intervention SCWE - 6 month follow-up survey QA focused-assessment of safety Culture All Leadership Session - Supvs.

Bi-monthly Form Cross-Functional Design Team for 1-Day All-Site Large Scale Meeting 1-Day All Site Large Scale Meeting

June 3, 2003 Davis-Besse Nuclear Power Station 17 Upcoming Safety Culture Actions

  • Improve the Work Management Safety Oversight Process
  • Facilitated Site Alignment Activities

- Leadership development and coaching

- Department/section activities

- All-site meetings

  • Site Safety Conscious Work Environment Training

- Prior to Mode 2 - during all-site training day Management & Human Performance Plan Update

June 3, 2003 Davis-Besse Nuclear Power Station 18 Upcoming Safety Culture Actions (continued)

  • Focused Organizational Development Activities

- Engineering

- Maintenance

  • Continued Employee Communications

- Reinstate weekly managers meeting

- Initiate monthly department/section meetings

- Continue monthly site meetings

- Conduct weekly Senior Management Team strategy meetings Management & Human Performance Plan Update

June 3, 2003 Davis-Besse Nuclear Power Station 19 Safety Culture Monitoring

  • Safety Conscious Work Environment Surveys

- 3rd quarter 2003, then annually for 2 years

  • Internal Quality Assurance Assessments

- 4th quarter 2003, then annually for 2 years

  • FENOC Internal Safety Culture Assessment

- Prior to Mode 4 (Restart Readiness)

- Prior to Mode 2 (Restart Readiness)

- Prior to restart from subsequent outages

- FENOC going-forward process Management & Human Performance Plan Update

June 3, 2003 Davis-Besse Nuclear Power Station 20 Other Activities

  • Create a New Vision Map
  • Align Station Business Plan Activities/Incorporate into Monthly Review Meeting
  • Future State Stand-down Management & Human Performance Plan Update

June 3, 2003 Davis-Besse Nuclear Power Station 21 Electrical Distribution and Safety Features Actuation System Relays Jim Powers Director - Engineering

June 3, 2003 Davis-Besse Nuclear Power Station 22 Emergency Diesel Generator (EDG) Issues/Resolution

  • Completed

- Operations accepted Operability Evaluation on May 15

- EDGs operable for all Modes

  • Plant Start-up

- Revise EDG Steady State Loading Calculation

- Revise EDG Transient Loading Calculation

- Prepare and issue USAR change; in draft

- Define acceptance criteria for EDG voltage and frequency response

  • Post-restart

- Evaluate actions to improve EDG voltage and frequency response during Safety Features Actuation System load sequencing Electrical Distribution

June 3, 2003 Davis-Besse Nuclear Power Station 23 AC System Issues/Resolution

  • First Mode 4

- Prepare Electrical Transient Analysis Program (ETAP) calculation

- Complete Evaluation Impacts of plant equipment

- Complete independent industry team review of ETAP analysis

- Evaluate conditions with unusual lineups to determine actions necessary going forward Electrical Distribution

June 3, 2003 Davis-Besse Nuclear Power Station 24 Safety Features Actuation System Relays

  • Originally Characterized as an Obsolescence Issue

- Supplier stopped manufacturing replacements

  • Reviews Found the Predominant Reason for Replacement was Coil Related

- Replacements were random with respect to age

  • Testing of Installed Relays has been Conducted

- Outliers were removed and will be replaced

- Relay population will gain improved reliability

  • Action Plan has been approved

- Obtain replacement relays from another utility

June 3, 2003 Davis-Besse Nuclear Power Station 25

  • Technical Evaluation (TE) is in Progress

- Industry experts are reviewing maintenance history

  • Average replacement rate has been at relatively the same level of 2% per year for about the last 20 years

- Temperature related aging does not appear to be an issue; further tests are under way to confirm

- Relay material condition is being assessed to further confirm suitability to function for another fuel cycle

- Independent review of TE will be conducted

  • Conclusion

- Operability evaluation will contain technical evaluation and confirm operability

  • Confirm that relays are acceptable for operation through the next operating cycle Safety Features Actuation System Relays

June 3, 2003 Davis-Besse Nuclear Power Station 26 High Pressure Injection Pump Modification and Corrective Action Program Performance Bob Schrauder Director -Support Services

June 3, 2003 Davis-Besse Nuclear Power Station 27 High Pressure Injection Pump Modification

  • Background

- Identified an issue that fine debris could impact the existing internal pump clearances

  • Selected Approach

- Modify the existing pump to add internal strainer to prevent debris from entering hydrostatic bearing

- This will allow the pumps to perform all design functions without replacement

  • Project Milestones

- Strainer design and testing

- Pump performance validation

- Field implementation

June 3, 2003 Davis-Besse Nuclear Power Station 28

  • Strainer Design and Testing

- Strainer allows water to pass through and supply the hydrostatic bearing and seal

  • flushes strainer surface

- Relocate ports that supply water to the hydrostatic bearing

  • supported by testing performed by pump manufacturer, Pump Guinard of France
  • reduce debris concentration at strainer

- MPR Associates performing design work

  • mock-up testing at Wyle Labs to verify performance High Pressure Injection Pump Modification

June 3, 2003 Davis-Besse Nuclear Power Station 29 High Pressure Injection Pump Modification

June 3, 2003 Davis-Besse Nuclear Power Station 30

  • Pump Performance Validation

- Rotordynamics analysis performed to predict satisfactory pump operation

  • includes worn condition after debris service

- In-plant testing is being performed to validate rotordynamics model

- Post-modification testing will be performed prior to returning the pumps to service High Pressure Injection Pump Modification

June 3, 2003 Davis-Besse Nuclear Power Station 31

  • Field Implementation

- Both pumps must be removed; each weighs 6,000 pounds

- Removal of HPI pump 2 requires detailed planning due to its location in the Emergency Core Cooling Pump Room

- A team involving six different craft disciplines will be used to remove the pumps and interference

- Design and Plant Engineering are key groups involved with the removal plans High Pressure Injection Pump Modification

June 3, 2003 Davis-Besse Nuclear Power Station 32 High Pressure Injection Pump Modification A full scale pump mock-up was used to determine rigging needs and pathway

June 3, 2003 Davis-Besse Nuclear Power Station 33 High Pressure Injection Pump Modification Rigging needs determined through the use of a full scale HPI pump mock-up

June 3, 2003 Davis-Besse Nuclear Power Station 34 Summary

  • Implementation of this Modification will Resolve the Debris Issue
  • Current Schedule shows completion supports Pressure Test in mid-to-late July High Pressure Injection Pump Modification

June 3, 2003 Davis-Besse Nuclear Power Station 35 Corrective Action Program Corrective Action Program Review Items

  • Corrective Action Categorization
  • Corrective Action Quality
  • Corrective Action Timeliness
  • Rollover Process

June 3, 2003 Davis-Besse Nuclear Power Station 36 Corrective Action Program Categorization

  • New Process Effective March 1, 2003

- Issued revision to NOP-LP-2001, Condition Report Process

- New Condition Reports issued since ~ 2,500

  • Restart Goal is to Maintain a 12-Week Rolling Average Level of 90% or Better
  • Management Review Board Upgrades

- Category changed to a higher level ~5%

June 3, 2003 Davis-Besse Nuclear Power Station 37 Corrective Action Program Categorization CONDITION REPORT CATEGORY ACCURACY 50%

60%

70%

80%

90%

100%

1/ 5 1/ 12 1/ 19 1/ 26 2/ 2 2/ 9 2/ 16 2/ 23 3/ 2 3/ 9 3/ 16 3/ 23 3/ 30 4/ 6 4/ 13 4/ 20 4/ 27 5/ 4 5/ 11 5/ 18 5/ 25 6/ 1 6/ 8 6/ 15 6/ 22 6/ 29 Category Recommendations Not Escalated 12 Week Avg Good Goal > 90 %

June 3, 2003 Davis-Besse Nuclear Power Station 38 Corrective Action Program Corrective Action Review Board

  • Apparent Cause - CARB Acceptable Rate ~ 62%

Restart Goal = positive trend Long -term Goal 90%

0%

20%

40%

60%

80%

100%

CARB Accepted 0

5 10 15 20 25 Accept Reject Goal 12 Week Avg Reject 0

0 0

5 1

0 0

0 0

6 3

1 Accept 0

0 0

0 4

0 0

2 0

14 5

1 12 Week Avg 62%

Goal 90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

90%

1/ 5 1/ 12 1/ 19 1/ 26 2/ 2 2/ 9 2/ 16 2/ 23 3/ 2 3/ 9 3/ 16 3/ 23 3/ 30 4/ 6 4/ 13 4/ 20 4/ 27 5/ 4 5/ 11 5/ 18 5/ 25 6/ 1 6/ 8 6/ 15 6/ 22 6/ 29 Good Restart Goal = positive trend Long-term Goal 90%

June 3, 2003 Davis-Besse Nuclear Power Station 39 Corrective Action Program Corrective Action Review Board

  • Root Causes - CARB Acceptable Rate ~ 90%

0%

20%

40%

60%

80%

100%

CARB Approval 0

2 4

6 8

10 Approved Approved with comments Reject 12-Week % Apvd & Apvd w/ comments 12-Week % Apvd Avg Re je c t 0

0 0

0 0

1 1

2 0

0 0

0 0

1 1

0 0

0 0

0 0

Appr ove d with c omme nts 0

0 0

1 1

1 0

2 1

0 1

1 3

2 3

2 1

0 1

0 0

Appr ove d 0

0 0

0 0

0 0

0 0

1 0

0 2

0 1

0 0

0 0

0 0

12-We e k % Apvd Avg 57%

57%

40%

33%

17%

13%

13%

8%

8%

15%

8%

8%

17%

14%

15%

15%

15%

16%

16%

19%

20%

12-We e k % Apvd & Apvd w/ c omme nts 100% 100% 100% 100% 100%

88%

75%

67%

67%

69%

67%

69%

78%

76%

77%

78%

78%

80%

84%

90%

90%

1/ 5 1/ 12 1/ 19 1/ 26 2/ 2 2/ 9 2/ 16 2/ 23 3/ 2 3/ 9 3/ 16 3/ 23 3/ 30 4/ 6 4/ 13 4/ 20 4/ 27 5/ 4 5/ 11 5/ 18 5/ 25 6/ 1 6/ 8 6/ 15 6/ 22 6/ 29 Good Restart Goal = improving trend Long -term Goal 90%

June 3, 2003 Davis-Besse Nuclear Power Station 40 Corrective Action Program Timeliness

  • Goal: < 5% overdue corrective actions 0%

20%

40%

60%

80%

Open Corrective Actions Overdue Overdue %

Goal Good Goal < 5%

Overdue

June 3, 2003 Davis-Besse Nuclear Power Station 41 Corrective Action Program Investigation Timeliness

  • Goal: < 5% overdue corrective action investigation 0%

20%

40%

60%

80%

Open Investigations Overdue Overdue %

Goal Good Goal < 5%

Overdue

June 3, 2003 Davis-Besse Nuclear Power Station 42 Corrective Action Program Supervisor Review Timeliness

  • Goal: 90 % or more supervisor reviews completed one day or less

- 89% completed within one day or less CONDITION REPORT SUPERVISORY REVIEW 20%

40%

60%

80%

100%

Supervisory Reviews Completed Within 1 Day 12 Week Avg Goal > 90%

Good

June 3, 2003 Davis-Besse Nuclear Power Station 43 Corrective Action Program SRO Review Timeliness

  • Restart goal: > 95% of the SRO reviews to be completed within one day

- 86% of SRO completed within one day CONDITION REPORT SRO REVIEW 20%

40%

60%

80%

100%

SRO Reviews Completed Within 1 Day 12 Week Avg Goal > 95%

Good

June 3, 2003 Davis-Besse Nuclear Power Station 44 Corrective Action Program Rollover Process

  • Rollover Definition

- The method of transferring the evaluation (complete or partial) of issues(s) addressed in one Condition Report (CR) to another, more encompassing CR

  • Difficulties Identified

- Paper trail is hard to follow at times

- Exacerbated by the large number being processed

- Generally concentrated in specific areas

- Few isolated cases actually have not been effectively resolved

  • Recommended Improvements

- Perform independent assessment

- Recently revised NOP-LP-2001, Condition Report Process, has rollover criteria

- Strengthened rollover criteria in future Nuclear Operating Procedure revision based on lessons-learned

June 3, 2003 Davis-Besse Nuclear Power Station 45 Quality Assessment Update Steve Loehlein Manager - Quality Assessment

June 3, 2003 Davis-Besse Nuclear Power Station 46 Independent Review of Condition Reports

  • Led by Nuclear Quality Assessment
  • Team Members from other Departments and other FENOC Sites
  • Scope Includes all 0350 Restart Condition Reports/Corrective Actions Quality Assessment Update

June 3, 2003 Davis-Besse Nuclear Power Station 47 Objectives

  • Confirm that Initially Identified Condition has been Evaluated
  • Track/Confirm that Issues Rolled to Another Condition Report were not lost
  • Document any Resulting Concerns in the Corrective Action Process for Resolution Quality Assessment Update

June 3, 2003 Davis-Besse Nuclear Power Station 48 Status of Review (as of May 27)

  • 1783 - 0350 Restart Condition Reports (CRs)
  • 7700 Associated Corrective Actions (CAs )
  • 510 Associated Rollovers Quality Assessment Update

June 3, 2003 Davis-Besse Nuclear Power Station 49 Reviews Completed to date (as of May 27)

  • 5057 CAs reviewed (includes Rollover CAs)

- 4379 CAs found to be acceptable (87% of those reviewed)

- 678 CAs continue in review (13% of those reviewed)

  • 510 Rollover CAs (100%)

- 415 Rollover CAs found to be acceptable (81%)

- 95 Rollover CAs continue in review (19%)

Quality Assessment Update

June 3, 2003 Davis-Besse Nuclear Power Station 50 Identified Concerns

  • Weaknesses in Documenting Resolution of the Identified Concern
  • Evaluations that do not address Full Scope of Identified Issue
  • Two Isolated Examples of incorrect Actions
  • Concerns have been Identified with the involved Department and reported on Condition Reports Quality Assessment Update

June 3, 2003 Davis-Besse Nuclear Power Station 51 Recent Key Activities

  • Observations of Technical Issues Resolution
  • Quality Control Oversight of Vendor Activities Quality Assessment Update

June 3, 2003 Davis-Besse Nuclear Power Station 52 Current Activities

  • Focused Assessment of Corrective Action Program

- Training drills, controller briefs, actual exercises

  • Management Decision-Making, Safety Culture, Radiation Protection, and Regulation Driven Changes to the Security Program Quality Assessment Update

June 3, 2003 Davis-Besse Nuclear Power Station 53 Mike Ross Restart Director Remaining Issues/Focus

June 3, 2003 Davis-Besse Nuclear Power Station 54 Remaining Issues/Focus Plant Support Center

  • In Full Operation
  • Issue List Developed
  • Action Item Database
  • Issues Needing Decision brought to Senior Management Team in Timely Fashion
  • Developed Issue Resolutions with Fragnet Transferred to Outage Control
  • Director, Nuclear Supply Chain on Site and Part of Plant Support Center Meeting to expedite Supply Requests
  • Listing of Modifications

June 3, 2003 Davis-Besse Nuclear Power Station 55 Remaining Issues/Focus Focus

  • Early Identification of Emergent Issues
  • Review of Plant Issues to ensure Proper Prioritization and Resolution
  • Issue Receiving Extra Focus

- HPI Modification

- Electrical Transient Analysis Program (ETAP)

- Safety Features Actuation System Relays

- Air-Operated Valve Program

- Plant Block Walls Seismic & Tornado Loading

- Thermal Overload Bypass of Safety Related Motors

  • Recent additions to Modification List

- Containment Spray Cyclone Separator

- Boron Precipitation Modification

June 3, 2003 Davis-Besse Nuclear Power Station 56 Schedule Milestones Mike Stevens Director - Maintenance

June 3, 2003 Davis-Besse Nuclear Power Station 57 Upcoming Activities Schedule Milestones

  • Complete Electrical Transient Analysis Program for Mode 4
  • Perform Testing on HPI 1 & 2
  • Refill Circulating Water and draw Condenser Vacuum
  • Conduct Mode 4 Restart Readiness Review
  • Enter Mode 4/Mode 3
  • Complete Train 2 work, followed by Train 1 work
  • Conduct Startup Readiness Review Meeting
  • Startup

June 3, 2003 Davis-Besse Nuclear Power Station 58 Restart Action Performance Clark Price Owner - Restart Action Plan

June 3, 2003 Davis-Besse Nuclear Power Station 59 Field Complete In Progress Hold - Plant Conditions N/A - Not Applicable Restart Action Performance Implementation 99 97 94 100 97 0350 Checklist Item Description 1

Adequacy of Root Cause a Penetration cracking and Reactor Pressure Vessel corrosion b Organizational, Programmatic and Human Performance Issues 2

Adequacy of Safety Significant Structures, Systems and Components a Reactor Pressure Vessel Head Replacement b Containment Vessel Restoration following RPV Head Replacement c Structures, Systems and Components Inside Containment c.1 Containment Emergency Sump d EOC of Boric Acid in Systems Outside of Containment Item No.

Discovery Technical Root Cause 02-0891 100 100 100 100

June 3, 2003 Davis-Besse Nuclear Power Station 60 Field Complete In Progress Hold - Plant Conditions N/A - Not Applicable Restart Action Performance 0350 Checklist Item Description 3

Adequacy of Safety Significant Programs a Corrective Action Program b Operating Experience Program c.1 Quality Audits c.2 Self-Assessments of Programs d Boric Acid Corrosion Management Program e Reactor Coolant System Unidentified Leakage Monitoring Program f In-Service Inspection Program g Modification Program h Radiation Protection Program i Completeness & Accuracy of Required Records

& Submittals to NRC Item No.

Discovery 100 100 100 100 100 100 100 Implementation 100 100 100 100 100 100 100 100 97 60

June 3, 2003 Davis-Besse Nuclear Power Station 61 Field Complete In Progress Hold - Plant Conditions N/A - Not Applicable Restart Action Performance 0350 Checklist Item Description 4 a-b 5

Readiness for Restart a Review of Licensee's Restart Action Plan b Systems Readiness for Restart b.1 Design Calculation Resolution c Operations Readiness for Restart d Test Program Development and Implementation 6 a-f Licensing Issue Resolution 7 a Confirmatory Action Letter Resolution Item No.

Discovery Adequacy of Organizational Effectiveness

& Human Performance 100 100 Implementation 100 90 72 CAL Resolution & Restart Report Restart Readiness Reviews 91 Included with 5 b

June 3, 2003 Davis-Besse Nuclear Power Station 62 Restart Action Performance TOTAL RESTART CONDITION REPORT EVALUATIONS 0

1000 2000 3000 4000 5000 6000 7000 Number of Restart CRs Add Close Tot a l Close d 3103 3204 3406 3558 3681 3833 3989 4173 4452 4692 4830 4998 5117 5234 5313 5377 5460 5542 5608 5673 5733 5788 Tot a l Ope n 1832 1772 1668 1610 1574 1475 1368 1219 973 786 689 597 516 457 427 400 350 325 349 313 322 294 Close 82 101 202 152 123 152 156 184 279 240 138 168 119 117 79 64 83 82 66 65 60 55 Add 8

41 98 94 87 53 49 35 33 53 41 76 38 58 49 37 33 57 90 29 69 27 1/ 5 1/ 12 1/ 19 1/ 26 2/ 2 2/ 9 2/ 16 2/ 23 3/ 2 3/ 9 3/ 16 3/ 23 3/ 30 4/ 6 4/ 13 4/ 20 4/ 27 5/ 4 5/ 11 5/ 18 5/ 25 6/ 1 6/ 8 6/ 15 6/ 22 6/ 29 Closed Open

June 3, 2003 Davis-Besse Nuclear Power Station 63 Restart Action Performance TOTAL RESTART CORRECTIVE ACTIONS 0

1000 2000 3000 4000 5000 6000 7000 8000 Number of Restart CAs Add Close Total Closed 1313 1457 1619 1817 2009 2262 2448 2701 3082 3401 3751 4097 4272 4497 4771 4879 5088 5394 5575 5677 5840 5957 Total Open 3049 3216 3384 3431 3389 3268 3191 3081 2823 2636 2381 2159 2051 1886 1675 1610 1442 1196 1075 1024 924 809 Close 97 144 162 198 192 253 186 253 381 319 350 346 175 225 274 108 209 306 181 102 163 117 Add 79 311 330 245 150 132 109 143 123 132 95 124 67 60 63 43 41 60 60 51 63 2

1/ 5 1/ 12 1/ 19 1/ 26 2/ 2 2/ 9 2/ 16 2/ 23 3/ 2 3/ 9 3/ 16 3/ 23 3/ 30 4/ 6 4/ 13 4/ 20 4/ 27 5/ 4 5/ 11 5/ 18 5/ 25 6/ 1 6/ 8 6/ 15 6/ 22 6/ 29 Closed Open

June 3, 2003 Davis-Besse Nuclear Power Station 64 Closing Comments Lew Myers Chief Operating Officer - FENOC