ML021440220

From kanterella
Jump to navigation Jump to search
April 2002 Monthly Operating Report for Beaver Valley Power Station
ML021440220
Person / Time
Site: Beaver Valley
Issue date: 05/07/2002
From: Pearce L
FirstEnergy Nuclear Operating Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
GL-97-002, L-02-056
Download: ML021440220 (6)


Text

FENOC Beaver Valley Power Station P. 0. Box 4 Shippingport, PA 15077 L-02-056 May 7, 2002 Beaver Valley Power Station Unit 1 - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73 Monthly Operating Report U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

In accordance with NRC Generic Letter 97-02, "Revised Contents of the Monthly Operating Report", and Unit 1 and 2 Technical Specification 6.9.4, the "Monthly Operating Report" is submitted for Unit 1 and Unit 2 for the month of April 2002.

Respectfully, W. Pearce Acting Site Vice-President DTJ/caj Enclosures cc:

NRC Regional Office King of Prussia, PA "U, q)

UNIT SHUTDOWNS DOCKET NO.

50-334 UNIT NAME BVPS Unit #1 DATE May 2,2002 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD:

April 2002 No.

Date Type Duration Reason Method of Cause / Corrective Actions (YIM/D)

F: Forced (Hours)

(1)

Shutting S: Scheduled Down (2)

Comments NONE.

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip / Scram C - Refueling 3 - Automatic Trip I Scram D - Regulatory Restriction 4-Continuation E - Operator Training / License Examination 5 - Other (Explain)

F - Administrative G - Operational Error (Explain)

H - Other (Explain)

SUMMARY

The Unit began the report period operating at approximately 95% output. This was being done in order to maintain reduced loading on the outboard motor bearings of the "A" Main Feedwater Pump until a planned power reduction to replace the motor bearings could be started on 4/2/02. Outboard motor bearing temperatures had been running higher in the previous month. At 0052 hours6.018519e-4 days <br />0.0144 hours <br />8.597884e-5 weeks <br />1.9786e-5 months <br /> on 4/2/02, the Unit began a power reduction to approximately 63% output in order to replace the motor bearings on the "A" Main Feedwater Pump. An output of approximately 63% was achieved at 0353 hours0.00409 days <br />0.0981 hours <br />5.83664e-4 weeks <br />1.343165e-4 months <br /> on 4/2/02. Cleaning of the "C" and "D" Main Unit Condenser Waterboxes was also performed during this planned reduction. Upon completion of repairs, the Unit commenced a return to full power at 0446 hours0.00516 days <br />0.124 hours <br />7.374339e-4 weeks <br />1.69703e-4 months <br /> on 4/5/02. A nominal value of 100% output was achieved at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on 4/5/02.

The Unit continued to operate at a nominal value of 100% output until 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br /> on 4/12/02 when a planned power reduction to approximately 90% output was begun in order to clean the "A" and "B" Main Unit Condenser Waterboxes. An output of approximately 90% was achieved at 2215 hours0.0256 days <br />0.615 hours <br />0.00366 weeks <br />8.428075e-4 months <br /> on 4/12/02.

However, with the "A" Condenser Waterbox isolated and degrading Condenser vacuum conditions indicated, the Unit performed several unplanned incremental load reductions between 0750 and 1247 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.744835e-4 months <br /> on 4/13/02 as a conservative action based on available Condenser vacuum indications, until the "A" Condenser Waterbox was returned to service. With the Unit operating at approximately 80% output, a return to approximately 90% output was commenced at 1532 hours0.0177 days <br />0.426 hours <br />0.00253 weeks <br />5.82926e-4 months <br /> on 4/13/02.

An output of approximately 90% was achieved at 1656 hours0.0192 days <br />0.46 hours <br />0.00274 weeks <br />6.30108e-4 months <br /> on 4/13/02.

The "B" Condenser Waterbox was removed from service and cleaned without any degrading Condenser vacuum conditions occurring. At 1331 hours0.0154 days <br />0.37 hours <br />0.0022 weeks <br />5.064455e-4 months <br /> on 4/14/02, the Unit commenced a return to full power.

A nominal value of 100% output was achieved at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> on 4/14/02. The Unit continued to operate at a nominal value of 100% output for the remainder of the report period.

OPERATING DATA REPORT DOCKET NO.:

UNIT NAME:

REPORT DATE:

COMPLETED BY:

TELEPHONE:

REPORTING PERIOD:

APRIL 2002 DESIGN ELECTRICAL RATING (Net MWe):

MAX.

DEPENDABLE CAPACITY (Net MWe):

835 821 50-334 BVPS UNIT #1 05/02/02 DAVID T. JONES (724) 682-4962 Notes:

Rated thermal power at BVPS-1 was uprated from 2652 MWt*

to 2689 MWt on 10/20/01.

Net MDC was also uprated from 810 MWe to 821 MWe.

HOURS IN REPORTING PERIOD:

NO.

OF ERS.

REACTOR WAS CRITICAL:

SERVICE HOURS GENERATOR ON LINE:

UNIT RESERVE SHUTDOWN HOURS:

NET ELECTRICAL ENERGY GEN.

(MWH):

GROSS ELECT.

ENERGY GEN.

(MWH):

GROSS THERMAL ENERGY GEN.

(KWH):

UNIT AVAILABILITY FACTOR (M):

UNIT CAPACITY FACTOR (MDC)

(M):

UNIT FORCED OUTAGE RATE (M):

THIS MONTH 719.0 719.0 719.0 0.0 567550.0 601370.0 1837779.0 100.0 96.1 0.0 YEAR TO DATE 2879.0 2879.0 2879.0 0.0 2367910.0 2505980.0 7619403.0 100.0 100.2 0.0 CUMULATIVE 227903.0 154960.5 152500.9 0.0 114034053.0 121772766.0 375254208.5 68.4 63.7 16.2 la.

1.

2.

3a.

3.
4.
5.
6.
7.
8.
9.
10.

11.

UNIT SHUTDOWNS DOCKET NO.

50-412 UNIT NAME BVPS Unit #2 DATE May 2, 2002 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD:

April 2002 No.

Date Type Duration Reason Method of Cause / Corrective Actions (Y/M/D)

F: Forced (Hours)

(1)

Shutting S: Scheduled Down (2)

Comments 3

020405 F

17.9 A

I The Unit was shut down to Mode 2 (Reactor remained critical) due to degraded chemistry conditions in the Steam Generators caused by a tube leak in the *C" Waterbox of the Main Unit Condenser. The tube leak was repaired, and once chemistry conditions in the Steam Generators improved, the Unit was returned to full power.

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip Scram C - Refueling 3 - Automatic Trip I Scram D - Regulatory Restriction 4 - Continuation E - Operator Training t License Examination 5 - Other (Explain)

F - Administrative G - Operational Error (Explain)

H - Other (Explain)

SUMMARY

The Unit began the report period operating at a nominal value of 100% output until 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on 4/4/02 when a planned power reduction to approximately 90% output was begun in order to remove the "C" Main Unit Condenser Waterbox from service for cleaning. An output of approximately 90%

was achieved at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> on 4/4/02.

With the "C" Condenser Waterbox isolated, the Unit commenced to return to full power at 0358 hours0.00414 days <br />0.0994 hours <br />5.919312e-4 weeks <br />1.36219e-4 months <br /> on 4/4/02. A nominal value of 100% output was achieved at 0455 hours0.00527 days <br />0.126 hours <br />7.523148e-4 weeks <br />1.731275e-4 months <br /> on 4/4/02.

The Unit continued to operate at a nominal value of 100% output until 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on 4/5/02 when a planned power reduction to approximately 90% output was begun in order to remove the "B" Main Unit Condenser Waterbox from service for cleaning. An output of approximately 90% was achieved at 0150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br /> on 4/5/02. With the "B" Condenser Waterbox isolated, the Unit commenced a return to full power at 0236 hours0.00273 days <br />0.0656 hours <br />3.902116e-4 weeks <br />8.9798e-5 months <br /> on 4/5/02. A nominal value of 100% output was achieved at 0347 hours0.00402 days <br />0.0964 hours <br />5.737434e-4 weeks <br />1.320335e-4 months <br /> on 4/5/02.

However, with degrading chemistry conditions occurring in the Steam Generators, an unplanned power reduction to approximately 90% output was begun at 0623 hours0.00721 days <br />0.173 hours <br />0.00103 weeks <br />2.370515e-4 months <br /> on 4/5/02 in order to investigate a potential tube leak in the "C" Waterbox of the Main Unit Condenser. At 0758 hours0.00877 days <br />0.211 hours <br />0.00125 weeks <br />2.88419e-4 months <br /> on 4/5/02, the Unit commenced a shut down due to degraded chemistry conditions in the Steam Generators. The Unit was taken off-line at 1424 hours0.0165 days <br />0.396 hours <br />0.00235 weeks <br />5.41832e-4 months <br /> on 4/5/02 and entered Mode 2 at 1443 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.490615e-4 months <br /> on 4/5/02 with the Reactor remaining critical. Once the tube leak in the "C" Condenser Waterbox was

UNIT SHUTDOWNS DOCKET NO.

50-412 UNIT NAME BVPS Unit #2 DATE May 2, 2002 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD:

April 2002

SUMMARY

(continued):

repaired and chemistry conditions in the Steam Generators improved, the Unit commenced to startup, entering Mode I at 0603 hours0.00698 days <br />0.168 hours <br />9.970238e-4 weeks <br />2.294415e-4 months <br /> on 4/6/02. The Unit was synchronized to the electrical grid at 0817 hours0.00946 days <br />0.227 hours <br />0.00135 weeks <br />3.108685e-4 months <br /> on 4/6/02 and commenced to return to full power.

A nominal value of 100% output was achieved at 2400 hours0.0278 days <br />0.667 hours <br />0.00397 weeks <br />9.132e-4 months <br /> on 4/6/02.

The Unit continued to operate at a nominal value of 100% output until 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> on 4/20/02 when a planned power reduction to approximately 75% output was begun in order to clean the "B" Main Unit Condenser Waterbox. An output of approximately 75% was achieved at 0017 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br /> on 4/21/02.

Upon completion of cleaning the "B" Condenser Waterbox, the Unit commenced to return to full power at 1650 hours0.0191 days <br />0.458 hours <br />0.00273 weeks <br />6.27825e-4 months <br /> on 4/21/02. A nominal value of 100% output was achieved at 1925 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.324625e-4 months <br /> on 4/21/02.

The Unit continued to operate at a nominal value of 100% output for the remainder of the report period.

OPERATING DATA REPORT DOCKET NO.:

UNIT NAME:

REPORT DATE:

COMPLETED BY:

TELEPHONE:

REPORTING PERIOD:

APRIL 2002 DESIGN ELECTRICAL RATING (Net MWe):

MAX.

DEPENDABLE CAPACITY (Net MWe):

836 831 50-412 BVPS UNIT #2 05/02/02 DAVID T.

JONES (724) 682-4962 Notes: Rated thermal power at BVPS-2 was uprated from 2652 MWt*

to 2689 Mwt on 10/30/01.

Net m)C was also uprated from 820 MWe to 831 MWe.

HOURS IN REPORTING PERIOD:

NO.

OF RRS.

REACTOR WAS CRITICAL:

SERVICE HOURS GENERATOR ON LINE:

UNIT RESERVE SHUTDOWN HOURS:

NET ELECTRICAL ENERGY GEN.

(MWH):

GROSS ELECT.

ENERGY GEN.

(MWH):

GROSS THERMAL ENERGY GEN.

(MWH):

UNIT AVAILABILITY FACTOR (%):

UNIT CAPACITY FACTOR (MDC)

(M):

UNIT FORCED OUTAGE RATE (M):

THIS MONTH 719.0 719.0 701.1 0.0 577393.0 608248.0 1842917.0 97.5 96.6 2.5 YEAR TO DATE 2879.0 2319.6 2287.8 0.0 1789764.0 1891744.0 5727455.0 79.5 74.8 0.8 CUMULATIVE 126686.0 103674.1 102980.4 0.0 80367856.0 84966487.0 259135036.0 81.3 76.9 10.3 la.

1.

2.

3a.

3.
4.
5.
6.
7.
8.
9.
10.

11.