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MONTHYEARL-PI-03-094, 2003 Steam Generator Inspection Results, 15-Day Report2003-10-24024 October 2003 2003 Steam Generator Inspection Results, 15-Day Report Project stage: Request L-PI-03-095, 2003 Unit 2 Steam Generator Category C-3 Inspection Results 30-Day Report2003-11-0707 November 2003 2003 Unit 2 Steam Generator Category C-3 Inspection Results 30-Day Report Project stage: Request L-PI-04-009, Inservice Inspection Summary Report, Interval 3, Period 3, Refueling Outage Dates: 9-13-2003 to 10-10-2003 Fuel Cycle 21: 3-3-2002 to 10-10-20032004-01-0707 January 2004 Inservice Inspection Summary Report, Interval 3, Period 3, Refueling Outage Dates: 9-13-2003 to 10-10-2003 Fuel Cycle 21: 3-3-2002 to 10-10-2003 Project stage: Request ML0408604472004-03-29029 March 2004 Prairie, Unit 2, Request for Additional Information Re Steam Generator Tube Inspection Summary Reports from the Spring 2002 and Fall 2004 Refueling Outages Project stage: RAI ML0428800262004-10-28028 October 2004 Steam Generator Tub Inspection Summary Reports for Their 2002 and 2003 Outages Project stage: Other 2004-01-07
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Category:Letter type:L
MONTHYEARL-PI-23-034, Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3.7.8, Cooling Water (Cl) System,2024-01-0202 January 2024 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3.7.8, Cooling Water (Cl) System, L-PI-23-035, Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specifications Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report2023-12-20020 December 2023 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specifications Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report L-PI-23-033, Supplement to License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 32023-12-0505 December 2023 Supplement to License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 3 L-PI-23-025, License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 32023-09-28028 September 2023 License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 3 L-PI-23-023, Baffle Former Bolts Alternate Aging Management Strategy2023-09-11011 September 2023 Baffle Former Bolts Alternate Aging Management Strategy L-PI-23-018, License Amendment Request to Revise ISFSI Technical Specification 4.4 to Allow Use of a Code Alternative to ASME Code, NB-5130, Examination of Weld Edge Preparation Surfaces, for the TN-40HT2023-07-14014 July 2023 License Amendment Request to Revise ISFSI Technical Specification 4.4 to Allow Use of a Code Alternative to ASME Code, NB-5130, Examination of Weld Edge Preparation Surfaces, for the TN-40HT L-PI-23-006, License Amendment Request to Revise Technical Specification 3.7.8 Required Actions2023-06-22022 June 2023 License Amendment Request to Revise Technical Specification 3.7.8 Required Actions L-PI-23-016, 2022 10 CFR 50.46 LOCA Annual Report2023-06-14014 June 2023 2022 10 CFR 50.46 LOCA Annual Report L-PI-23-010, Annual Report of Individual Monitoring2023-04-27027 April 2023 Annual Report of Individual Monitoring L-PI-23-007, Supplement to Application to Revise Technical Specification Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (PTLR)2023-03-28028 March 2023 Supplement to Application to Revise Technical Specification Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (PTLR) L-PI-23-005, CFR 50.55a Requests Nos. 1-RR-5-15 and 2-RR-5-15, Proposed Use of Subsequent ASME Code Edition and Addenda in Accordance with 10 CFR 50.55a(g)(4)(iv)2023-03-0303 March 2023 CFR 50.55a Requests Nos. 1-RR-5-15 and 2-RR-5-15, Proposed Use of Subsequent ASME Code Edition and Addenda in Accordance with 10 CFR 50.55a(g)(4)(iv) L-PI-23-001, Day Steam Generator Tube Inspection Report2023-01-30030 January 2023 Day Steam Generator Tube Inspection Report L-PI-22-047, Resubmittal of Prairie Island Nuclear Generating Plant (PINGP) 2018 Unit 1 180-Day Steam Generator Tube Inspection Report2022-12-21021 December 2022 Resubmittal of Prairie Island Nuclear Generating Plant (PINGP) 2018 Unit 1 180-Day Steam Generator Tube Inspection Report L-PI-22-020, Application to Revise Technical Specification Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (PTLR)2022-12-0202 December 2022 Application to Revise Technical Specification Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (PTLR) L-PI-22-040, Supplement to Application to Revise Technical Specifications to Adopt TSTF-577, Revised Frequencies for Steam Generator Tube Inspections2022-10-0606 October 2022 Supplement to Application to Revise Technical Specifications to Adopt TSTF-577, Revised Frequencies for Steam Generator Tube Inspections L-PI-22-037, Updated Approach for Prairie Island Unit 1 and Unit 2 Baffle Former Bolts2022-09-20020 September 2022 Updated Approach for Prairie Island Unit 1 and Unit 2 Baffle Former Bolts L-PI-22-032, CFR 50.46 LOCA Annual Report2022-06-16016 June 2022 CFR 50.46 LOCA Annual Report L-PI-22-033, Response to Request for Additional Information Prairie Island Nuclear Generating Plant, Units 1 and 2, Amendment to Adopt 24-Month Operating Cycles2022-06-10010 June 2022 Response to Request for Additional Information Prairie Island Nuclear Generating Plant, Units 1 and 2, Amendment to Adopt 24-Month Operating Cycles L-PI-22-003, Application to Revise Technical Specifications to Adopt TSTF-577, Revised Frequencies for Steam Generator Tube Inspections2022-06-0707 June 2022 Application to Revise Technical Specifications to Adopt TSTF-577, Revised Frequencies for Steam Generator Tube Inspections L-PI-22-024, Supplement to Application for License Amendment to Implement 24-Month Operating Cycle2022-03-0707 March 2022 Supplement to Application for License Amendment to Implement 24-Month Operating Cycle L-PI-21-047, Response to Request for Additional Information 24-Month Cycle Amendment Prairie Island Nuclear Generating Plant, Units 1 and 22021-12-0707 December 2021 Response to Request for Additional Information 24-Month Cycle Amendment Prairie Island Nuclear Generating Plant, Units 1 and 2 L-PI-21-045, Response to Request for Additional Information Cooling Water System License Amendment Request2021-11-0404 November 2021 Response to Request for Additional Information Cooling Water System License Amendment Request L-PI-21-029, Exigent License Amendment Request to Revise Technical Specification 3.7.8 to Allow a One-Time Extension of the Completion Time of Required Action B.12021-10-0707 October 2021 Exigent License Amendment Request to Revise Technical Specification 3.7.8 to Allow a One-Time Extension of the Completion Time of Required Action B.1 L-PI-21-006, License Amendment Request to Revise Technical Specification 3.3.1, Reactor Trip System (RTS) Instrumentation, to Incorporate Installed Bypass Test Capability for the Power Range RTS Functions2021-10-0202 October 2021 License Amendment Request to Revise Technical Specification 3.3.1, Reactor Trip System (RTS) Instrumentation, to Incorporate Installed Bypass Test Capability for the Power Range RTS Functions L-PI-21-032, Response to Request for Additional Information Amendment Request to Adopt TSTF-471 and 571-T for Prairie Island2021-09-30030 September 2021 Response to Request for Additional Information Amendment Request to Adopt TSTF-471 and 571-T for Prairie Island L-PI-21-016, Application for License Amendment to Implement 24-Month Operating Cycle2021-08-0606 August 2021 Application for License Amendment to Implement 24-Month Operating Cycle L-PI-21-027, 2020 10 CFR 50.46 LOCA Annual Report2021-06-28028 June 2021 2020 10 CFR 50.46 LOCA Annual Report L-PI-21-023, Independent Spent Fuel Storage Installation - 2020 Annual Radiological Environmental Monitoring Program Report2021-05-14014 May 2021 Independent Spent Fuel Storage Installation - 2020 Annual Radiological Environmental Monitoring Program Report L-PI-21-007, Application to Revise Technical Specifications to Adopt TSTF-471, Eliminate Use of the Term Core Alterations in Actions and Notes2021-04-19019 April 2021 Application to Revise Technical Specifications to Adopt TSTF-471, Eliminate Use of the Term Core Alterations in Actions and Notes L-PI-20-050, Request for a One-Time Exemption from 10 CFR 50, Appendix E, Biennial Emergency Preparedness Exercise Requirements, Due to COVID-19 Pandemic2020-10-0707 October 2020 Request for a One-Time Exemption from 10 CFR 50, Appendix E, Biennial Emergency Preparedness Exercise Requirements, Due to COVID-19 Pandemic L-PI-20-051, Supplement to Application to Revise Technical Specifications to Adopt TSTF-547, Clarification of Rod Position Requirements2020-09-28028 September 2020 Supplement to Application to Revise Technical Specifications to Adopt TSTF-547, Clarification of Rod Position Requirements L-PI-20-026, Response to Request for Additional Information: License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiativ2020-09-0101 September 2020 Response to Request for Additional Information: License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4 L-PI-20-035, = Request for Revision to Reactor Vessel Material Surveillance Capsule Removal Schedule2020-07-28028 July 2020 = Request for Revision to Reactor Vessel Material Surveillance Capsule Removal Schedule L-PI-20-023, Independent Spent Fuel Storage Installation, Response to Request for Additional Information: License Amendment Request to Expand the Storage Capacity of the Independent Spent Fuel Storage Installation (ISFSI)2020-06-10010 June 2020 Independent Spent Fuel Storage Installation, Response to Request for Additional Information: License Amendment Request to Expand the Storage Capacity of the Independent Spent Fuel Storage Installation (ISFSI) L-PI-20-014, Supplement to License Amendment Request: Expand the Storage Capacity of the Independent Spent Fuel Storage Installation (ISFSI2020-04-29029 April 2020 Supplement to License Amendment Request: Expand the Storage Capacity of the Independent Spent Fuel Storage Installation (ISFSI L-PI-20-004, License Amendment Request to Revise Technical Specifications (TS) to Remove Note I from Limiting Condition for Operating (LCO) 3.4.12 and LCO 3.4.132020-03-30030 March 2020 License Amendment Request to Revise Technical Specifications (TS) to Remove Note I from Limiting Condition for Operating (LCO) 3.4.12 and LCO 3.4.13 L-PI-20-001, License Amendment Request to Address Issues Identified in Westinghouse Nuclear Safety Advisory Letter NSAL-09-5, Revision 1, and NSAL-15-12020-01-29029 January 2020 License Amendment Request to Address Issues Identified in Westinghouse Nuclear Safety Advisory Letter NSAL-09-5, Revision 1, and NSAL-15-1 L-PI-19-041, Application to Revise Technical Specifications to Adopt TSTF-547, Clarification of Rod Position Requirements2019-12-23023 December 2019 Application to Revise Technical Specifications to Adopt TSTF-547, Clarification of Rod Position Requirements L-PI-19-031, License Amendment Request: Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b2019-12-16016 December 2019 License Amendment Request: Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b L-PI-19-040, License Amendment Request: Revise Technical Specification 5.5.14 to Permanently Extend Containment Leakage Rate Test Frequency2019-10-0707 October 2019 License Amendment Request: Revise Technical Specification 5.5.14 to Permanently Extend Containment Leakage Rate Test Frequency L-PI-19-038, Submittal of Revised Pressure and Temperature Limits Report2019-09-19019 September 2019 Submittal of Revised Pressure and Temperature Limits Report L-PI-19-037, Response to Request for Additional Information: 10 CFR 50.55a Requests Nos. 1-RR-5-10 and 2-RR-5-10, Proposed Alternative to Reactor Vessel Inservice Inspection (ISI) Intervals2019-09-16016 September 2019 Response to Request for Additional Information: 10 CFR 50.55a Requests Nos. 1-RR-5-10 and 2-RR-5-10, Proposed Alternative to Reactor Vessel Inservice Inspection (ISI) Intervals L-PI-19-025, Request to Approve Site-Specific Probabilistic Risk Assessment (PRA) Model for Flowserve N-Seal Abeyance Seal and Dynamic Testing for the Prairie Island Nuclear Generating Plant (PINGP)2019-08-27027 August 2019 Request to Approve Site-Specific Probabilistic Risk Assessment (PRA) Model for Flowserve N-Seal Abeyance Seal and Dynamic Testing for the Prairie Island Nuclear Generating Plant (PINGP) L-PI-19-029, Supplement to Response to Request for Additional Information: Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components For...2019-08-0505 August 2019 Supplement to Response to Request for Additional Information: Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components For... L-PI-19-002, 10 CFR 50.55a Requests Nos. 1-RR-5-10 and 2-RR-5-10, Proposed Alternative to Reactor Vessel Inservice Inspection (ISI) Intervals for Prairie Island, Unit 1 and Unit 22019-06-13013 June 2019 10 CFR 50.55a Requests Nos. 1-RR-5-10 and 2-RR-5-10, Proposed Alternative to Reactor Vessel Inservice Inspection (ISI) Intervals for Prairie Island, Unit 1 and Unit 2 L-PI-19-014, Response to Request for Additional Information: Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors2019-04-29029 April 2019 Response to Request for Additional Information: Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors L-PI-19-003, Request for Revision to Reactor Vessel Material Surveillance Capsule Removal Schedule for Prairie Island Nuclear Generating Plant (PINGP)2019-02-0404 February 2019 Request for Revision to Reactor Vessel Material Surveillance Capsule Removal Schedule for Prairie Island Nuclear Generating Plant (PINGP) L-PI-19-006, Emergency License Amendment Request Regarding One-Time Extension for Technical Specification Completion Time Requirements2019-01-29029 January 2019 Emergency License Amendment Request Regarding One-Time Extension for Technical Specification Completion Time Requirements L-PI-19-005, Online Reference Portal for NRC Review of License Amendment Request to Implement 10 CFR 50.692019-01-15015 January 2019 Online Reference Portal for NRC Review of License Amendment Request to Implement 10 CFR 50.69 L-PI-18-063, Response to Request for Additional Information: Revise License Condition Associated with Implementation of NFPA 8052018-12-0606 December 2018 Response to Request for Additional Information: Revise License Condition Associated with Implementation of NFPA 805 2024-01-02
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Commid tdPraie Island Nuclear Generating Plant Committed to Nudarelen Operated by Nuclear Management Company, LLC L-PI-03-095 November 7, 2003 Technical Specification 5.6.7.3 U S Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555 PRAIRIE ISLAND NUCLEAR GENERATING PLANT DOCKET 50-306 LICENSE No. DPR-60 2003 UNIT 2 STEAM GENERATOR CATEGORY C-3 INSPECTION RESULTS 30-DAY REPORT In accordance with Technical Specification 5.6.7.3 this special report due to Category C-3 inspection results of the Unit 2 steam generator tubing is provided for the information of the NRC Staff.
The results of the inspection of 21 Steam Generator and 22 Steam Generator were classified as Category C-3 in accordance with Technical Specification 5.6.7.3 because more than 1% of the inspected tubes in each Steam Generator were defective. The NRC Staff was informed of the Category C-3 classification by telephone on September 22, 2003. In accordance with Technical Specification 5.6.7.3, the 30-day special report on the Category C-3 steam generator inspection results is provided as Attachment 1 to this letter.
Inthis letter, we have made no new Nuclear Regulatory Commission commitments.
Please contact Jeff Kivi (651-388-1121) if you have any questions related to this letter.
Joseph M.Solymossy Site Vice President, Prairie Island Nuclear Generating Plant CC Regional Administrator, USNRC, Region IlIl Project Manager, Prairie Island Nuclear Generating Plant, USNRC, NRR NRC Resident Inspector - Prairie Island Nuclear Generating Plant Attachment 1717 Wakonade Drive East Welch, Minnesota 55089-9642 Telephone: 651.388.1121
ATTACHMENT I NUCLEAR MANAGEMENT COMPANY, LLC PRAIRIE ISLAND NUCLEAR GENERATING PLANT DOCKET 50-306 November 7, 2003 PRAIRIE ISLAND UNIT 2 STEAM GENERATOR CATEGORY C-3 TUBE INSPECTION SPECIAL REPORT 2 pages follow
PRAIRIE ISLAND UNIT 2 STEAM GENERATOR CATEGORY C-3 TUBE INSPECTION SPECIAL REPORT Purpose This report fulfills the special reporting requirements of Prairie Island Technical Specification 5.6.7.3. This report is required whenever the steam generator tube inservice inspection finds more than 10% of the total tubes inspected are degraded tubes or more than I % of the inspected tubes are defective. This report summarizes the inspection results, the investigation into causes of major tube degradation and corrective measures. Corrective measures to prevent recurrence of Category C-3 inspections are discussed. Steam generator inspection results continue to exceed the category C-3 limits, so corrective measures do not prevent recurrence. However, careful inspections and repairs coupled with chemistry controls and low operating temperature provide assurance of safe and reliable operation of Unit 2 steam generators.
Summary of Inspection Results The inservice inspection for Unit 2 Steam Generators occurred from September 17, 2003 through October 1,2003. The inservice inspection consisted of inspection of 100% of the full length of tubing with the bobbin coil (except rows 1 through 4 u-bends),
100% of the hot leg tubesheet region, 25% of the hot leg Inconel 690 roll plugs, 25% of the cold leg tubesheet region and the rows 1 through 11 u-bends with mechanical rotating probes with +PointTM coil.
As a result of the eddy current inspections, 5.2% (165 of 3165) of the inspected tubes in 21 Steam Generator contained defects requiring repair. Seven of these tubes were plugged and the remaining 158 tubes were left in service using the F* and EF* repair criteria.
As a result of the eddy current inspections, 2.9% (92 of 3148) of the inspected tubes in 22 Steam Generator contained defects requiring repair. Ten of these tubes were plugged and the remaining 82 were left in service using the F* repair criteria.
Investigation into Causes of Major Tube Degradation There are two major causes of tube degradation in Unit 2 steam generators:
Secondary side intergranular attack and stress corrosion cracking (IGA/SCC or ODSCC) is occurring in the hot leg tubesheet crevice region and at the top of the hot leg tubesheet.
This was confirmed by metallurgical examination of three tube samples removed from Steam Generator 12 in January 1985. This was also confirmed by examination of a parent tube section removed during the sleeve pulls in Steam Generator 12 in 1996. In 1
PRAIRIE ISLAND UNIT 2 STEAM GENERATOR CATEGORY C-3 TUBE INSPECTION SPECIAL REPORT addition, three tubes were removed from Unit 1 for GL 95-05 Voltage Based Repair Criteria in 1997 and ODSCC was confirmed at the hot leg tube support plates.
Primary water stress corrosion cracking (PWSCC) at the roll transition region has been confirmed by metallurgical examination of one roll transition zone removed during sleeve pulls in Steam Generator 12 in 1996.
Corrective Measures Prairie Island participates in utility funded research on steam generator related issues.
Corrective measures to reduce and/or prevent tube degradation due to primary water stress corrosion cracking and secondary side IGASCC have been used by the industry with limited success. Prairie Island corrective measures include:
Chemistry Control: Prairie Island follows both the original equipment manufacturer's water chemistry guidelines and the EPRI secondary water chemistry guidelines.
The PWSCC degradation appears to be relatively independent of chemistry and occurs in regions of high residual stress.
High Hydrazine Control: Prairie Island maintains a hydrazine control band of 100 to 125 ppb as measured in the feedwater system.
Molar ratio control to reduce secondary side corrosion: Molar ratio control has been attempted by adjustments to steam generator blowdown resin ratios.
Conduct Crevice Flushing Operations with Boric Acid: Prairie Island employed crevice flushing from 1986 to 1999.
On-line addition of Boric Acid: Prairie Island began on-line addition of boric acid to Unit 1 steam generators in 1987.
Use of other chemical inhibitors: Titanium chelate has been added since January 1994.
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