JAFP-86-0957, Monthly Operating Rept for Oct 1986
| ML20213F661 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 10/31/1986 |
| From: | Radford Converse, Jackie Cook POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | NRC OFFICE OF ADMINISTRATION (ADM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
| References | |
| JAFP-86-0957, JAFP-86-957, NUDOCS 8611140374 | |
| Download: ML20213F661 (13) | |
Text
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3 JAMES A. FITZPATRICK NUCLEAR POWER FIANT OPERATING DATA REPORT DOCKEI No.
50-333 UNIT NAME F m PATRICK DATE NOV 1986 CCNPIRIED BY JOHN COOK TELEPHONE (315)342-3840 OPERATING STATUS 1.
UNIT NAME:
FITZPATRICK NOIES 2.
REPORTING PERIOD: 861001-861031 3.
LICENSED THERMAL POWER (&TI):
2436 4.
NAMEPIATE RATING (GROSS MWE):
883 5.
DESIGN ELECTRICAL RATING (NET MWE):
816 6.
MAXIMUM DEPENDABLE CAPACITY (GROSS MWE):
823 7.
MAXIMUM DEPENDAELE CAPACITY (NET MWE):
796 8.
IF CHANGES OCCUR IN CAPACITY RATINGS (ntNS 3 - 7) SINCE LAST REPORT, GIVE REAS0hF NONE 9.
PDRER 12; VEL 'iU WHICH REMIUrw, IF ANY (Nt;r NE):
NONE 10.
RFASONS FOR RESIR1CTIONS, IF ANY:
THIS FDNIH YR-TO-DATE CUMULATIVE 11.
HOURS IN REPORTING PERIOD:
745 7296 98737 12.
NUMBER OF HOURS REACIOR WAS CRITICAL:
550.6 6611.8 72027.4 13.
REACIOR RESERVE SHUTDOWN HOURS:
0 0
0 14.
HCURS GENERATOR ON-LINE:
536 6468.2 69994.3 15.
UNIT RESERVE SHUrDOWN HOURS:
0 0
0 16.
GROSS THERMAL ENERGY GENERATED (EE):
1198920 15322248 151035922 17.
GROSS ELECTRICAL ENERGY GENERATED (MWH):
404870 5183000 51776210 18.
NET ELECIRICAL ENERGY GENERATED (&R):
391515 5007980 49572505 19.
UNIT SERVICE FACIOR:
71.9%
88.7%
70.9%
20.
UNIT AVAIIABILITY FACIOR:
71.9%
88.7%
70.9%
21.
UNIT CAPACITY FACIOR (USING MDC NET):
66.0%
86.2%
64.8%
22.
UNIT CAPACITY FACIOR (USING DER NET):
64.4%
84.1%
61.5%
23.
UNIT FORCED OUTAGE RATE:
0%
2.2%
12.4%
24.
SHUIIGUS SCHEDULED OVER NEXT 6 FDNIES (TYPE, DATE AND DURATION OF EACH):
Refuel outage to cmmence January 15, 1987 and last approximately 88 days.
25.
IF SHUR DCMN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARIUP:
26.
UNITS IN TEST STATUS (PRIOR TO 00FNERCIAL OPERATION):
FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECIRICITY CDNERCIAL OPERATION jfM 0611140374 861031 PDR ADOCK 05000333 y
R PDR Ig
.=
j JMES A. FITZPATRICK NUCLEAR POWER PUNT AVERAGE MILY UNIT POWER IEVEL DOCKET No.
50-333-UNIT N.
MTE NUV 1936 03 H EfED BY JOHN MAA TEEPHONE (315)34z-35W i
3 s
M)NIH OCIDBER 1986 s%
MY AVERAGE MILY POWER LEVEL MY AVERAGE MILY POWER LEVEL'
'MJe NET M4e NET 1
0 17 778 2
0 18 731 3
0 19 733 4
0 20 730 i
5-0 21 727 6
0 22 728 7
0 23 730 8
0 24 728 9
60 25 730 a
10 541 26 762 11 719 27 729 12 751 28 729 13 795 29 727 14 800 30 732 i'
15 801 ai 754 16 798 SIM %RY: =The FitzPatrick plant was started up and ran at near full thermal power l
for this reporting period.
L
= -.
.--s JAMES A. FITZPATRICK NUCLEAR POWER FIANT UNIT SHUIV0WNS AND POWER REDUCTIONS
'hi
~
DOCKET No.
50-333
~"
UNIT NAME N DAIE IT N 1986 REPORT IONIH OCI0BER 1986 00MPIErED BY JOHN 000K TELEPHONE (315)342-3840 5
t D
C
?
UH R
MEIBOD S
O R0 E
OF YC MC CAUSE AND CORRECTIVE ACTION AU A
SHUITING LICENSEE SO PO 10 NO.
DATE TYPE TR S
DOWN EVENT TD 0D PREVENT RECURRENCE IS 0
THE REPulu EE NE O
N REACIOR M
E N
N T
5 861001 S
209 B
1 N/A N/A N/A 860928 SHUrDOWN FOR MAINriNANCE AND LP ROIOR INSPECTION (CLNUIATIVE HRS 273.6)
I i
I j
1 2
3 4
j F: FORCED REASON:
MEIBOD:
EXHIBIT G.- INSIRUCTIONS j
S: SCHEDULED A. EQUIPMENT FAILURE (EXPIAIN) 1-MANUAL FOR PREPARATION OF DATA i
B. MAINIENANCE OR TEST 2-MANUAL SCRAM ENIRY SHEETS FOR LICENSEE C. REFUELING 3-AUIT ATIC SCRAM EVENT REPOKr (LER) FIIE.
D. REGULAIORY RESIRICTION 4-0THER (EXPIAIN)
E. OPERATOR TRAINING AND LICENSE EXAMINATION F. AININISTRATIVE G. OPERATIONAL ERROR (EXPIAIN)
H. OTHER (EXPIAIN) 4 4
NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE OCTOBER 1986 The FitzPatrick plant returned to service on-October 9, 1986 after completion of a maintenance outage.
The unit then ran at near full thermal power for the remainder of the reporting period.
At the end of the reporting period the plant is operating at approximately 754 MW,.
NEW YORK P0(ER AUIHORITY JAMES A. FITZPATRICK NUCLEAR POWER FIANT MAINIENANCE SlM4ARY FOR THE FONIH OF: OCIOBER 1986 WORK REQUEST NO.
HOW CAUSE OF RESULTS OF ACTION TAKEN TO REPAIR DATE SYSTEM COMPONENT NO.
DEIECIED MALEUNCTION MALFUNCTION PRECLUDE RECURRENCE TIFE HOURS 861014 03 044494 OPS STICKY REIAY "B" RBM SEES NO CHECKED OPEPATION, 2
ROD 18-19 ROD SELECT FUNCTIONING 861008 05 043204 JIC FAULTY REIAY (DNTACTS, KEEP REPIACED K-128C 09-93 0.5 K-128C A1/A2 VERIFIED ANNUNCIA10R ENERGIZED 861010 07 041536 OPS DIRIY CONNECIOR FAILED DOWNSCALE PEREORMED TDR; 2
LPRM28-05D CLEANED CONNECIOR 861006 07 042809 OPS OPEN DETECIOR OR NO SIGNAL REPAIRED CONNECIOR; 99 NM-31B CONNECIOR PERFORMED TDR 861006 07 043223 JIC CRD WORK REbOVE TIP TUBING; REF0VED, REINSTALLED, 94 TIP TUBING SRM/IRM CABLES CABLES, IMP 7.26 861005 07 044336 OPS DIRTY CONNECIOR FAILED DOWNSCALE CLEANED CONNECIOR; 8
LPRM44-45A DURING INSERT PERFORMED TDR 861003 07 045586 JIC WORN P0r. R2 METER IND. WENT REPIACED POWER Por.R2; 6
NM-80E TO O AT 80% PWR FUNCTIONAL TEST SAT.
861006 07 045673 OPS DIRTY CONNECIOR SPURIOUSLY UPSCALE CLFRED CONNECIOR; 6
LPRM20-21A PEREORMED TDR
NEW YORK POWER AITIHORITY JAMES A. FITZPATRICK NUCLEAR POWER FIANT MAINI1! NANCE SIM4ARY FOR THE FDNIH OF: OCIOBER 1986 WORK REQUEST NO.
HOR CAUSE OF RESULTS OF ACTION TAKEN TO REPAIR DATE SYSTEM COMPONENT NO.
DETECTED MALFUNCTION MALFUhUTION PRECLUDE RECURRENCE TIME 10URS 861005 07 045670 OPS H O IN CONNECIOR SPURIOUSLY CLEANED CONNECIOR; 6
2 LPRM12-21A UPSCALE PERFORMED IDR 861007 07 046388 JIC DEIECIOR CONNECIOR INDICATION REPIACED DETECIOR 24 IRM-G ERRATIC 00NNECIOR 861007 07 046411 JIC CONNECIOR DIRIY SPURIOUS AIARMS CLEANED CONNECIOR UNDER 6
SRM-C VESSEL 861012 07 046460 OPS CLUTCH TORQUE TIP MACHINE WON'T IMP-7.26; TT REPIACED 9
NM-101C REQUIRES AI11UST.
DRIVE IN SEE WR-42698 861006 14 043360 JIC NEEDS REPIACEMENT ISOIATION VALVE REPIACES ISOLATION 5
DPIS-43A APPEARS TO LEAK VALVE: IMP-G10 861006 14 045504 OPS NEEDS TO BE HI PRES. ISOL.
REPIACED IS01ATION 5
DPIS-43B TIGHTENED VALVE LEAKING VALVE: IMP-G10 861005 17 030685 OPS REQUIRES B FDNTIOR OUT OF PERFORMED ISP-19-1 16 RM-150A,B ALIGNMENT TOLERANCE 861008 17 043235 JIC DRIFT RECALB. RAD FDN MADE REQUIRED AllIUST.
47 RM-150A REVSD ISP-19-1 ISP-19-1
NEW YORK ECWER AUIHORITY JAMES A. FITZPATRICK NUCLEAR POWER FIANT MAINTENANCE S& MARY FOR THE FDNIH OF: OCIOBER 1986 HORK REQUEST NO.
HOW CAUSE OF RESULTS OF ACTION TAKEN TO REPAIR DATE SYSTEM C W PONENT NO.
DETturtu MALFUNCTION MALFUNCTION PRECLUDE RECURRENCE TIME HOURS 861031 20 046542 OPS BAD AMPLIFIER PEN (RED) DOESN'T REPIACED AMPLIFIER, 13 FR-52B INDICATE Fw W RAN IMP-G14 861002 23 042478 OPS AGE /MISADJUS'INENT SIIM TIME FOR AIUUSTED RELAY 15 SEC.
29 23A-K14 REIAY/23-F0V-14 861008 29 042825 OPS FAULTY LIMIT 90% LIMIT SWITCH REPIACED SWrIm; MANUAL 24
~UV H6A SWITCH WON'T RESET OPERATOR IIVEL A
861005 29 045300 OPS DIRTY SPEED VALVE SIIM TO REPIACED FILTER ASBLY; 9
A0V-80A CONTROL FILTER PICK UP LIMIT ADJUSTED SWITCH 861005 29 045301 OPS SPEED 00NTROL MSIV SIIM CWSURE REPIACES FILTER; 8
PNS-86C FILTER ASSEMBLY TEST 100 SIIM AIUUSTED 861009 29 046452 OPS NO PROBLEM; SWITCH MSIV 90% LIMIT ISP-65-1; SWIT m 3
A0V-86A DID RESET FAILED RESET RESET 5 TIMES 861021 70 033207 OPS PIANr FDD.
INSTALL /FOUNr FDUNTED DRYER INCLINE 26 DPI-103 F1-86-040 DRYER MAN 0MEIER MAN W ETER 861002 71 028718 OPS METER OUT OF CURRENT FETER INSTALLED AND 7.5 LPCI BATTERY TOLERANCE NEEDS CALIBRATED NEW METER RECALIBRATION I
NEW WRK POWER AUINORITY 4
JAMES A. FITZPATRICK NUCLEAR POWER PIANT MAINIENANCE SLM4ARY FOR THE MNIH OF: OCIORER 1986 l
4 CAUSE OF RESULTS OF ACTION TAKEN TO REPAIR i
WRK REQUEST NO.
- HOW, MALFUNCTION MAIRNCTION PRECLUDE RECURRENCE TIME DATE SYSTEM C[EPONENT NO.
Drauau)
HOURS l
I 861002 71 043337 JIC COVER EXPOSED LPCI INSTALL B00 RIES ON 13 INV-3A(B) 600VAC BUS UNINTERRUPTIBLE INV/CH LEGS BARS POWER SUPPLY 1
861007 71 046390 OPS DC LINK VOLTAGE WILL NOT COME AIUUSTED 6
INV-3B NOT HIGI IN SERVICE 4
861004 93 032844 JIC RESET POINT TRIPPED SWIICH PERFORMED F-IMP-93.1 PS-lD OUT OF SYSTEM WITH NORMAL l
PRESSURE PRESSURE l
l i
i
]
i i
1
)
4 4
NEW YORK POWER AUIHORITY JAMES A. FITZPATRICK NUCEAR POWER FIANT SAFELY RELATED ELECTRICAL & MECHANICAL MAINTENANCE SlM4ARY -
OCIOBER 1986 REPAIR TIME WORK REQUEST /
DATE SYSTEM C WPW ENT HOR DEPFCTED CAUSE OF MAIRJNCTION ACTION TAKEN TO PRECLUDE RECURRENCE HOURS 10/5 02-2 30540 OPS
.Imose packing Adjusted packing 2
H W 54B
= --______
_ _ _ _ - - _ _ _ _ - - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ - _ _. = =__
_ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ = _ = = = _
10/5 12 45603 OPS Worn packing Replaced packing 14 HW'T5
- _ _ _ _ _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ = = = = _ = = _ _ _ _ _ - _ _ _ - _ _ - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ _ - _ _ - _ _ _ _
10/5 13 45354 OPS Worn packing Replaced packing 8
lOV I31
_______________-_-_____________-_-__________________________-_____________-___-___d packing and yoke nut 10/5 02 45604 OPS Worn packing and Replace 12 ADV-17 yoke nut
______________________________________-__-___________-_______-_________________________ket 1
10/6 16 46128 OPS Worn gasket Replaced gas GTTEtch
____ = -__-_______-____________________-_-______-_________-__-___-___-__-_-_________-______
________________________-___-_- _=_
10/8 13 45503 OPS
' Worn packing Replaced packing 10 MW I5
________-_s
_______====-=--____________=_=== -
____-__-______-_-_______________-________________________-____________________3 10/7 16 30938 OPS Worn gasket Replaced gasket IF Door
__________-c
_-______________=-
==-______-__--____________-______-_________-_______________________-_______________-__________50 10/6 10 46379 OPS Seat ring backed out Installed new seat ring lHPi2A
_______________-_--__-_______________-c
____-_--_-_-_____________________-___-___________________--________________________--__ king 10/6 23 45255 OPS Worn packing Replaced pac 2
HFI-77C
-__-_-_____-______-__-____-__-___-__-_-__a
==--__-__-_______
__=
==___-__ ___
=
.---__-___-_______-_-_-_==- -
10/5 29 30937 OPS Worn packing Replaced packing 10 KN-77
_________-_s 10/8 03 30464 OPS Worn seals Replaced CRD EIM'T2-43
_______________=--
====-__-----______________--c
-_____-________________-______________________________________-____-__________ laced CRD 80 10/8 03 30466 OPS Worn seals Rep ERD 38-07
====== --_---__-_-----------------------------------------<
= = _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ = _
_______-_______--_--______= _= = =___===___=
e
NEW YORK POWER AUIIIORITY JAMES A. FITZPATRICK NUCLEAR POWER FIANT SAFEIY RF7ATED ELECTRICAL & MECHANICAL MAINTENANCE SINARY OCIOBER 1986 REPAIR WRK REQUEST #
TIME DATE SYSTEM CTPONENT HOR DETECTED CAUSE OF MAIEUNCTION ACTION TAKEN 'IO PRECLUDE RECURRENCE HOURS 10/8 03 42661 OPS Wom seals Replaced CRD 100 CRD 46-15 MD T4-19 10/8 03 42658 OPS Wom seals Replaced CRD 40 CRD 10-11 10/8 03 44449 OPS Wom seals Replaced CRD 80 GD TT6-43
_________c CRD 22-27
_________c GD 30-39
_____________________________________________________________________________________________________________________________c 10/8 03 44316 OPS Wom seals Replaced CRD 80 G D 22-31
_________c CRD 34_11 10/6 13 45341 OPS Worn packing Added 2 rings of packing 5
FDV T6 10/6 46 46387 OPS Seat leakage Lapped seats 4
E59 T6A 10/4 71 31337 PM Worn overloads Replaced overloads 4
U T67-0D3 3A 55
NEW WRK POWER AU110RITY JAMES A. FITZPATRICK NUCLEAR POWER PLANT SAFELY RELATED F7FGRICAL & MECHANICAL MAINTENANCE SitNARY OCIOBER 1986 REPAIR TORK REQUEST f TIME DATE SYSTDI C mPONENT HOW DETECIED CAUSE OF MAIR)NCTION ACTION TAKEN TO PRECLUDE RECURRENCE IK)URS 10/1 12 42618 PM Worn clutch tripper Replaced worn parts 10 R AT 11 assenbly
_-_______ ___ -_- _=__=
.--__- ___======== _-------------_ _-----__._--_--_ _-------_-----__---__-
10/3 23 42621 OPS Broken Sta-Kon Replaced Sta-Kon connection 8
RAT I6 connection
--_ __-----_=
---_----_-------__--____-___ ___-----_-----_._--------_-___ _----__-=______===---_--__---_.-------_----_----__
10/7 10 46386 OPS Motor failure Replaced motor 20 H N 149B
--_-_.------_-==- -. = _ _ _ _ _ _ - =
==-------------_-_-_-------____-___-_---_--_-_-_--_-_------_---_----___----------_----__ --_ -
10/7 29 30934 PM Age and environ-Replaced power cable 60 RN 77 ment Cables
-_---________ ____-_________---__-____________-_--___-___---_____--_---__--__----___--_ = ___==---- --__--_------_--_---_--_.
10/7 29 43528 PM Wrong material Replaced geared limit switch 9
RN 77 and torque switch
. - - - - - _. _ _ _ - _ _. _ - _ _ _ _ = = = _ _ - - - - - - - - - - _ _ - - - - - - - _ - _ - - - - - _ - _ - - - - - _ _ _ - - _ _ _ _ _ - = = = - - = _
=
10/5 20 30926 PM Declutch shaft and Replaced parts 2
RN H2 retaining ring
.. _------_ ----------_====- =___=__-------_
__===_-_-----------------______-_-_------.........--___-_--_----______-_-----_-_c 10/6 13 30933 OPS Motor failure Replaced motor 49 RN I5
_---______--________-__-__________-___-_-_-_----__------_----__--_---_------_---c 10/7 34 45688 OPS Burned out SOV coil Replaced SOV 10 NRTI11B SOV
-==-
- = - - _ - - _____--___-----------------_-_-__---_______--_-______ _____...-_--
10/6 10 46381 OPS Motor failure Replaced motor 56 RN 25H
_____________-_______-_-_-______-_____=====_----==_-_-_-____--_______--__-----__------_---_-__---______--_ --_---____-____--_
10/8 34 44337 OPS Worn air cylinder Replaced air cylinder 42 NRV Illa 10/9 34 44338 OPS
. Worn air cylinder Replaced air cylinder 50 NRV IllB
=___
==______._---_._______
-_ _____=._.-----_ ____----___ _-------_-_--_---_ _ -_----------------_---_._-===--- =-----_ -
10/14 23 45337 OPS
-Bent declutch shaft Replaced declutch mechanism 60 M)V-57
_- - -. - - - - - - - ___ __-_--------_---_-====___=_____-===
NEW YORK POWER AUIHORITY JAMES A. FITZPATRICK NUCLEAR POWER PLANT o.
SAFELY RELATED ELECTRICAL & MECHANICAL MAIhTENANCE S& MARY OCIDBER 1986 REPAIR WRK REQUEST f TIME DATE SYSTDI CWPONENT HOR DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE HOURS 10/14 23 33055 EQ None Replaced motor and brake 9
FDV I5 assably
_____________________________________________________________________________________________________________________________c 10/8 02 46391 OPS Torque switch Replaced torque switch 10 FDV 53B
_____________________________________________________________________________________________________________________________c 10/6 29 30932 OPS Torque switch Replaced torque switch 36 FDV IO2
E k
Jrme) A. FitzPctrick Nucirr Pow:r Pirnt PO Ek)x 41 Lycorrung, New York 13093 315 342 3840 Radford J. Converse
- > NewYorkPower
& Authority November 10, 1986 JAFP-86-0957 Director, Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C.
20555 ATTENTION:
DOCUMENT CONTROL DESK
REFERENCE:
DOCKET No. 50-333
Dear Sir:
Enclosed please find the J. A. FitzPatrick Operating Status Report for the month of October, 1986.
Refueling information remains the same as previously submitted.
If there are any questions concerning this report, please cont t John Cook at (315) 342-3840, Ext. 3569.
/% v RADFORD J. CONVERSE RESIDENT MANAGER RJC:JPC:mac Enclosures cc:
Distribution
&V s
s