IR 05000277/1996004

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Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-277/96-04 & 50-278/96-04
ML20134Q298
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 11/25/1996
From: Pasciak W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Danni Smith
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
References
NUDOCS 9612020220
Download: ML20134Q298 (3)


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.. November 25, 1996 Mr.- D. M. Smith,' President PECO Nuclear Nuclear Group Headquarters-Correspondence Control Desk P. O. Box 195 Wayne, Pennsylvania 19087-0195 SUBJECT: COMBINED INSPECTION REPORT NOS. 50-277/96-04; 50-278/96-04

Dear Mr. Smith:

This. refers to your September 5,1996 correspondence, in response to our August 6,1996 letter.

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Thank you for informing us of the corrective and preventive actions documented in your letter.

These actions will be examined during a future inspection of your licensed program.

t Your cooperation with us is appreciated. ,

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Sincerely, t

ORIGINAL SIGNED BY:

Walter J. Pasciak, Chief

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Projects Branch 4 l

Division of Reactor Projects l

Do':ket Nos. 50-277; 50-278

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Mr. cc: l T. Mitchell, Vice President G. Rainey, Senior Vice President, Nuclear Operations G. Edwards, Plant Manager, Peach Bottom Atomic Power Station !

D. Fetters, Vice President, Nuclear Station Support I G. A. Hunger, Jr., Chairman, Nuclear Review Board and Director, Licensing )

J.W. Durham, Sr., Senior Vice President and General Counsel T. Neissen, Director, Nuclear Engineering Division G. Lengyel. Manager, Experience Assessment cc w/cy of licensee's ltr:

C. D. Schaefer, External Operations - Nuclear, Delmarva Power & Light Co.

B.W. Gorman, Manager-External Affairs, Public Service Electric & Gas Co. !

P. MacFarland Goelz, Manager, Joint Generation, Atlantic Electric '

R. McLean, Power Plant Siting, Nuclear Evaluations J. H. Walter, Chief Engineer, Public Service of Maryland R. Ochs, Maryland Safe Energy Coalition J. Vannoy, Acting Secretary of Harford County Council L. Jacobson, Peach Bottom Alliance TMI - Alert (TMIA)

Nuclear Safety Information Center (NSIC)

NRC Resident inspector l Commonwealth of Pennsylvania i State of Maryland

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l Mr. i Distribution w/cy of licensee's itr:

Region l Docket Room (with concurrences)

W. Dean, OEDO J. Shea, NRR J. Stolz, PDI-2, NRR Inspection Program Branch, NRR (IPAS)

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PUBLIC D. Screnci, PAO

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l DOCUMENT NAME: a: reply.pb "E" = Copy with attachment / enclosure To receive a copy of this do nt. Indicate in tl's box: "C" = Copy without attachment / enclosure

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OFFICE RI:Df)P p // lA/ RI:DRP l NAME WPe%gfak///

DATE a1/ eff 96/

OFFICIAL RECORD COPY f

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F ch B tt Atornic Ibwer Station

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PECO NUCLEAR ni L"Tft"*"" .

A Unit of PECO Energy "'

$745$jN 2 Fax 717 456 4243 September 5, 1996 ,

Docket Nos. 50-277 50-278 License Nos. DPR-44 DPR-56 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 Subject: Peach Bottom Atomic Power Station Units 2 & 3 Response to Notice of Violation (Combined Inspection Report No.

50-277/96-04 & 50-278/96-04)

Gentlemen:

In response to your letter dated August 6,1996, which transmitted the Notice of Violation concerning the referenced inspection report, we submit the attached response. The subject report concerned a Routine Resident Integrated Safety inspection that was conducted May 5 through July 6,1996.

If you have any questions or desire additional information, do not hesitate to contact us.

b + $# VM Thomas N. Mitchell Vice President,

Peach Bottom Atomic Power Station Attachments I

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cc: B. W. Gorman, Public Service Electric & Gas R. R. Janati, Commonwealth of Pennsylvania

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H. J. Miller, US NRC, Administrator, Region I W. L. Schmidt, US NRC, Senior Resident inspector H. C. Schwemm, VP - Atlantic Electric

R. I. McLean, State of Maryland A. F. Kirby 111, DelMarVa Power

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CCN#96-14073 7-

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RESPONSE TO NOTICE OF VIOLATION Restatement of Violation Technical specification 5.4.1 requires, in part, that written procedures be implemented to cover technical specification required surveillance testing, operation of the reactor I protection system, and for maintaining secondary containment integrity.

Contrary to the above, PECO did not properly implement written procedures for:

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Technical specification required testing on a control room emergency ventilation system filter train. Specifically, on May 9,1996, PECO contractor technicians, under the supervision of a PECO maintenance technician, did not implement procedure ST-M-40D-905-2 properly.

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Operation of the reactor protection system. Specifically, on May 22,1996 a plant equipment operator did not properly implement procedure SO 60F.6.A-2 dunng restoration of the 2B reactor protection s loss of power and a half reactor scram. ystem motor generator set, resulting in a

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Maintaining secondary containment integrity. Specifically, on June 12, a chemistry technician did not implement procedure A-C-134 properly, resulting in an improperly controlled breach of the secondary containment.

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This is a Severity Level IV violation (Supplement 1).

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/ r Reason for the Violation (Example 1)

On May 9,1996, at approximately 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br />, ST-M-40D-905-2, Control Room Emergency Ventilation Filter Train 'A' Test, was identified as being performed out of sequence. ST-M-40D-905-2 is a Level 1 procedure which requires the procedure to be in hand, and the performance and completion of steps to be documented as they are )

performed. The filter train test was being perfomled by an outside contractor with the '

support of Peach Bottom Atomic Power Station (PBAPS) maintenance. The contractor is utilized for their expertise on charcoal filter train testing, results analysis, knowledge of safety-related ventilation systems and the regulatory requirements of these systems. The vendor performs these tests with generic procedures and guidelines developed by the vendor for these tasks. PBAPS has specific surveillance tests that delineate the steps required to perform the filter testing. The result of this process was that the PBAPS

, maintenance procedure and the vendor procedure did not agree with respect to sequence and chronological order of the steps. The testing was performed on the filter train until the evolution was questioned by the NRC resident inspector. The testing was

' stopped and reviewed by the maintenance technicians, maintenance supervision and the i vendor. It was determined that the Control Room Emergency Filter Train ST was not I i being performed as written.

Corrective Steps That Have Been Taken and the Results Achieved

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Upon discovery of the issue, the test was stopped and the procedure was revised using the Temporary Procedure Change process. Vendor personnel assisted in this process to

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ensure that the PBAPS ST was revised to the proper test methodology and sequence. l The temporary change and permanent revision to the procedure was approved and the I

test completed satisfactorily at 2030 hours0.0235 days <br />0.564 hours <br />0.00336 weeks <br />7.72415e-4 months <br /> on May 9,1996.

A meeting was held with the work team on August 2,1996 where management expectations and requirements of A-C-79 were communicated. The maintenance division also conducted an all-hands meeting on August 9,1996 to discuss this issue and communicate management expectations for procedure usage and compliance.

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A review of other procedures associated with vendor test performance was performed.

Several procedures were identified with similar situations of potential conflict and 1 Procedure Problem Identification Process (PPIS) action items were initiated to resolve these issues.

Corrective Steps That Will Be Taken to Avoid Further Violations i Vendor input and comment will be obtained prior to test performance to ensure station procedures are consistent with vendor and industry practices. Appropriate procedures will

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be revised prior to test performance to ensure consistency.

l Date When Full Compliance Was Achieved '

Full compliance on ST-M-40D-905-2 was achieved on May 9,1996 when the test procedure was revised to sequentially correspond to the activities required to be performed. The test was then satisfactorily performed and completed.

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Beason for the Violation (Exampic 2)

On May 22,1996, at approximately 1305 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.965525e-4 months <br />, an unexpected loss of the Unit 2 'B' RPS power supply occurred when an equipment operator mispositioned the voltage

< adjustment rheostat for the RPS Attemate feed transformer. The operator was required, per procedure SO 60F.6A-2," Transferring Reactor Protection System Power Supplies",

to adjust the 'B' RPS MG set rheostat to set-up the 'B' RPS MG set for return to service from maintenance. A pre-job briefing was conducted and the operator was instructed on the appropriate sequence of restoration. The operator proceeded to walk down the SO to ensure he was familiar with all of the locations for restoration, specific actions required, and test equipment installation points. After this evolution was complete, he returned to the 'B' RPS MG set and verified appropriate steps in the SO. The next task described in

the SO was to adjust the rheostat on the 'B' RPS MG set. Instead, the operator

! proceeded to the RPS Alternate feed and turned the rheostat for the RPS Alternate feed i

thus causing the unexpected transient. The cause of this event was the failure of the

operator to follow SO 60F.6.A-2. This resulted in an unanticipated unit half scram and an outboard Group Ill PCIS isolation which required a four hour notification to the NRC.

, Corrective Steos That Have Been Taken and the Results Achieved

Upon loss of the alternate RPS feed, the operating shift investigated the cause of the

transient and restored the RPS feeds in accordance with station procedures.

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The equipment operator was counseed on the expectation to adhere to procedures, be l aware of his surroundings and to fully a plement self-check techniques.

j Corrective Stens That Will Be Taken to Avoid Further Violations The corrective steps that have been initiated as a result of this event will serve to avoid further violations.

Date When Full Compliance Was Achieved i

' Full compliance was achieved on May 22,1996, when the RPS feeds were returned to normal.

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, Reason for the Violation (Exampb 3)

On June 12,1996, at approximately 1005 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.824025e-4 months <br />, the hatch between the Unit #3 refuel ,

floor and the refuel floor roof was propped open to allow access to the roof for '

performance of CH-428," Main Stack and Vent Stack Sampling System Efficiency Determination". Personnel performing this test believed that the only procedural requirement to open the hatch was to have a security guard present. They were not aware that propping this door open resulted in a violation of secondary containment even though this hatch was posted as an A-C-134, " Control of Hazard Barriers" hatch. The security guard also failed to recognize the consequence of propping the hatch door open and the potential to impact secondary containment integrity. This work activity should have been controlled by A-C-134 and GP-16 " Breaching and Establishing Secondary Containment". These procedures do not allow a secondary containment door to be propped secondaryopen without specific controls put in place to ensure compliance with maintaining containment.

Corrective Steps That Have Been Taken and the Results Achieved Upon discovery, the following actions were taken. The hatch to the roof was immediately closed and shift management was notified. Personnel working on the roof were briefed on A-C-134 requirements and the need to keep the hatch closed for secondary containment operability. The security guard was also briefed to ensure the hatch remained closed for secondary containment operability, except for brief passage.

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An evaluation was performed to determine if secondary containment had been compromised during this event. The evaluation concluded there was sufficient margin to ensure the safety function of secondary containment was maintained.

An all-hands meeting was held with the chemistry staff to address the issues of A-C-134 and GP-16 ar.d the need to properly maintain hazard barriers closed except for passage and the neea to ensure secondary containment is maintained.

Nuclear security group issued a bulletin to all security personnel to ensure that designated and posted as A-C-134 doors are not propped open. In addition, the locks to the refuel floor roof hatches have been changed which require a specific key to open these hatches. This key is only issued by nuclear security and contains a tag which warns not to open these hatches without GP-16 and shift supervision's authority.

Procedure CH-428 was revised, using the temporary procedure change process, to obtain permission from shift management to temporarily breach secondary containment in accordance with GP-16 and A-C-134. CH-428 was then permanently revised to reflect the same requirements in the prerequisite section of the procedure as well as adding precautionary notes in the procedure sections that require roof access.

GP-16 was revised to render secondary containment inoperable in modes 1(Power Operation),2(Startup), and 3(Hot Shutdown) as a result of opening either the Unit #2 or

  1. 3 refuel floor hatch to reactor building roof.

The information and causes of this issue were provided to site-wide work groups. Action items were issued to site groups to ensure review of this issue and an understanding A-C-134 and its requirements, as well as the need to control secondary containment as it relates to the PBAPS design basis.

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Corrective Steos That Will Be Taken to Avoid Further Violations The corrective steps that have been initiated as a result of this event will serve to avoid further violations.

Date When Full Compliance Was Achieved Full compliance was reached at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on June 12,1996, when the hatch to the Unit

  1. 3 refuel floor roof was closed.

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