The following information was provided by the licensee via phone and email:
At 2250 EST on November 11, 2024, a technical specification required shutdown was initiated at Beaver Valley Power Station Unit 2. The following technical specification limiting conditions of operation (LCOs) were entered at 1939 EST on November 11, 2024:
LCO 3.6.3, containment isolation valves, condition C, one or more penetration flow paths with one containment isolation valve inoperable; required action C.1, isolate the affected penetration flow path by use of at least one closed and de-activated automatic valve, closed manual valve, or blind flange.
LCO 3.7.2, main steam isolation valves (MSIVs), condition C, one or more MSIVs inoperable in mode 2 or 3; required action C.1, close MSIV within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.
These technical specification required actions will not be completed within the completion time; therefore, a technical specification required shutdown was initiated, and this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i).
With one main steam isolation valve inoperable, this condition is also being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v).
There was no impact on the health and safety of the public or plant personnel.
The NRC Resident Inspector has been notified.
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The failure occurred during planned surveillance testing in preparation for reactor startup.
- * * RETRACTION ON 12/30/2024 AT 1025 EST FROM JAMIE SMITH TO JORDAN WINGATE * * *
The following information was provided by the licensee via phone and email:
On 11/12/2024 an 8-hour notification was made describing the failure of one main steam isolation valve (MSIV) to close during testing while the plant was in MODE 3. This notification was made pursuant to 10 CFR 50.72(b)(3)(v) as a condition that could have prevented the fulfillment of a safety function. Further engineering evaluation has determined that this condition was not reasonably expected to prevent the fulfillment of a safety function based on a review of the accident analyses and the redundant equipment which is known to have been capable of performing the safety functions. Therefore, this does not result in a reportable condition under this criterion.
At the same time, a 4-hour notification was made pursuant to 10 CFR 50.72(b)(2)(i) as an initiation of a shutdown required by plant technical specification due to initiating a transition to MODE 4 to exit TS applicability. The plant was in hot standby (MODE 3) at the time of the event and negative reactivity was not added in order to move to MODE 4, therefore, this event is not reportable under this criterion.
The NRC Resident Inspector has been notified.
Notified R1DO (Lilliendahl)