ENS 55572
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ENS Event | |
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15:07 Nov 12, 2021 | |
Title | Manual Reactor Trip Due to Increasing Steam Generator Water Levels |
Event Description | At 1007 EST on November 12, 2021, with Unit 2 in Mode 1 at approximately 17 percent power following a refueling outage, the reactor was manually tripped due to increasing steam generator water levels due to an oscillating Main Feedwater Pump Recirculation Valve. Additionally, the Main Steam Isolation Valves were manually closed to prevent excessive reactor coolant system cooldown. Decay heat is being removed by discharging steam to the atmosphere using the Atmospheric Dump Valves.
The trip was not complex, with all systems responding normally post-trip. There was no equipment inoperable prior to the event that contributed to the reactor trip or adversely impacted plant response. Operations responded and stabilized the plant. Beaver Valley Power Station Unit 1 is unaffected and remains at 100 percent power in Mode 1. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification, per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
Where | |
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Beaver Valley Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
LER: | 05000412/LER-2021-004 Manual Reactor Trip |
Time - Person (Reporting Time:+-1.25 h-0.0521 days <br />-0.00744 weeks <br />-0.00171 months <br />) | |
Opened: | Sean Mcgee 13:52 Nov 12, 2021 |
NRC Officer: | Donald Norwood |
Last Updated: | Nov 12, 2021 |
55572 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (17 %) |
After | Power Operation (0 %) |
Beaver Valley with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | |
WEEKMONTHYEARENS 571322024-05-19T04:30:00019 May 2024 04:30:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 570752024-04-13T04:35:00013 April 2024 04:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 559432022-06-15T11:24:00015 June 2022 11:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Automatic Auxiliary Feedwater Actuation ENS 555862021-11-17T18:13:00017 November 2021 18:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Automatic Auxiliary Feedwater Actuation ENS 555722021-11-12T15:07:00012 November 2021 15:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Increasing Steam Generator Water Levels ENS 555072021-10-05T10:32:0005 October 2021 10:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip and Auxiliary Feedwater Actuation ENS 543692019-11-04T10:35:0004 November 2019 10:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Steam Dump Transient ENS 530562017-11-07T10:04:0007 November 2017 10:04:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Automatic Reactor Trip Due to Main Unit Generator Over Current ENS 501242014-05-20T12:35:00020 May 2014 12:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip During Reactor Startup ENS 496972014-01-06T21:59:0006 January 2014 21:59:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Main Transformer Fault ENS 495052013-11-05T23:28:0005 November 2013 23:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Notification of Unusual Event Due to Explosion and Fire in the Turbine Building ENS 467442011-04-10T07:45:00010 April 2011 07:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Manual Reactor Trip While Performing a Technical Specification Required Shutdown ENS 428342006-09-08T01:57:0008 September 2006 01:57:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Following Spurious Opening of a Reactor Trip Breaker ENS 424672006-04-02T18:02:0002 April 2006 18:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Main Generator Trip ENS 403202003-11-13T16:35:00013 November 2003 16:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip from 100% Power with Cause Being Investigated ENS 402472003-10-15T03:55:00015 October 2003 03:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Low "B" Steam Generator Water Level. 2024-05-19T04:30:00 | |
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