An Appendix R non-compliance issue was identified. When the plant automatically tripped on September 25, 2011, an unexpected
automatic trip was identified in
DC shunt trip breakers 72-01 and 72-02. This automatic trip function was not considered in the Appendix R electrical coordination evaluation. Preliminary analysis has shown that if the
shunt trip breaker would have automatically opened due to fire induced fault currents, then Appendix R credited equipment may have been lost unexpectedly. The operability evaluation performed, resulted in increasing the
shunt trip settings to maximum, and implementing compensatory measures to isolate some non-safety related electrical loads, which restored compliance with
10 CFR 50 Appendix R.
The licensee notified the NRC Senior Resident Inspector.
CR#
PLP2011-04835