ENS 46159
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ENS Event | |
|---|---|
18:51 Aug 7, 2010 | |
| Title | Manual Reactor Trip After Reactor Coolant Pumps High Vibration |
| Event Description | At 1451 on 8/7/2010, Oconee Unit 1 initiated a manual reactor trip from approximately 17% power due to indicated vibrations on 1A1 and 1A2 reactor coolant pumps [RCP] reaching the high vibration trip criteria. All systems responded normally following the reactor trip. Unit 1 is currently stable in MODE 3. An investigation is in progress to determine the cause of the elevated reactor coolant pump vibrations.
All control rods fully inserted on the trip. Decay heat is being removed via the turbine bypass valves to the main condenser. Steam generator water level is being maintained with main feedwater. There is no evidence that the PORVs or safety valves lifted. The plant is in its normal shutdown electrical lineup. There were no indications on the loose parts monitor except for the RCP high vibration. There was no affect on units 2 or 3. The licensee notified the NRC Resident Inspector. |
| Where | |
|---|---|
| Oconee South Carolina (NRC Region 2) | |
| Reporting | |
| 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
| Time - Person (Reporting Time:+-0.07 h-0.00292 days <br />-4.166667e-4 weeks <br />-9.5886e-5 months <br />) | |
| Opened: | Bob Meixell 18:47 Aug 7, 2010 |
| NRC Officer: | Mark Abramovitz |
| Last Updated: | Aug 7, 2010 |
| 46159 - NRC Website
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Unit 1 | |
|---|---|
| Reactor critical | Critical |
| Scram | Yes, Manual Scram |
| Before | Power Operation (100 %) |
| After | Hot Standby (0 %) |
Oconee | |
WEEKMONTHYEARENS 580412025-11-15T03:54:00015 November 2025 03:54:00
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