ENS 45088
ENS Event | |
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00:15 May 22, 2009 | |
Title | Rps Actuation (Reactor Trip) Due to Generator Phase Differential Lockout |
Event Description | Event: Oconee Unit 3 Reactor Protection System (RPS) actuation due to Anticipatory Trip.
At 2015 hrs on 5-21-2009, Oconee Nuclear Station Unit 3 experienced a RPS actuation due to an anticipatory trip caused by a generator phase differential lockout. At the time of the RPS actuation, Unit 3 was exiting a planned refueling outage and power was at 42%. Immediately after the trip, Operators entered the appropriate emergency operating procedure and post-trip response was determined to be normal. Operators transitioned to the normal shutdown procedure at 2056 hours0.0238 days <br />0.571 hours <br />0.0034 weeks <br />7.82308e-4 months <br />. Unit 3 is currently in Mode 3 and stable. This event is being reported as a 4-Hour Non-Emergency per 10 CFR 50.72(b)(2)(iv)(B). Initial Safety Significance: No Emergency Action Limits (EALs) were met and there was no safety significance as a result of the Unit 3 trip. Units 1 and 2 remain at 100% power (Mode 1) and were unaffected by the Unit 3 trip. Corrective Actions(s): Planned corrective actions are to maintain Unit 3 in Mode 3 (Hot Standby) until completion of the post-trip evaluation. The NRC Resident Inspector has been notified. All control rods fully inserted. The reactor is currently subcritical and shutdown margin within Technical Specification limits. RCS Inventory Control is via normal makeup. PORV and Pressurizer Code Safeties are closed. SG inventory control is being maintained via Main Feedwater. Heat is being removed from the Steam Generators to the Main Condenser via Turbine Bypass Valves. |
Where | |
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Oconee South Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
LER: | 05000287/LER-2009-002 |
Time - Person (Reporting Time:+-1.1 h-0.0458 days <br />-0.00655 weeks <br />-0.00151 months <br />) | |
Opened: | Stephen Newman 23:09 May 21, 2009 |
NRC Officer: | Donald Norwood |
Last Updated: | May 21, 2009 |
45088 - NRC Website
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Unit 3 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (42 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 557502022-02-22T03:07:00022 February 2022 03:07:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 557332022-02-05T08:57:0005 February 2022 08:57:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared Due to Visual Observation of Smoke and Multiple Fire Alarms in the West Penetration Room ENS 556382021-12-10T05:49:00010 December 2021 05:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 546612020-04-11T01:25:00011 April 2020 01:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip ENS 536772018-10-19T04:00:00019 October 2018 04:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Steam Seal Header Pressure Malfunction ENS 533292018-04-13T06:27:00013 April 2018 06:27:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Following Main Feedwater Control Problem ENS 528702017-07-24T20:38:00024 July 2017 20:38:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Load Rejection ENS 517702016-03-06T20:20:0006 March 2016 20:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Emergency Declaration Due to Fire/Explosion in the Main Transformer ENS 507812015-01-31T19:31:00031 January 2015 19:31:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Rps Actuation Due to Oscillations in the Feedwater System ENS 494712013-10-24T09:53:00024 October 2013 09:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip from Full Power Due to Feedwater System Oscillations ENS 461592010-08-07T18:51:0007 August 2010 18:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip After Reactor Coolant Pumps High Vibration ENS 450882009-05-22T00:15:00022 May 2009 00:15:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Rps Actuation (Reactor Trip) Due to Generator Phase Differential Lockout ENS 446382008-11-07T13:34:0007 November 2008 13:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 441092008-03-31T17:52:00031 March 2008 17:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Turbine Trip During Maintenance Activities ENS 431692007-02-15T21:54:00015 February 2007 21:54:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 and Unit 2 Reactor Trip ENS 424932006-04-12T17:35:00012 April 2006 17:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit 2 Experienced an Automatic Reactor Trip Following the Loss of the "2B2" Reactor Coolant Pump ENS 419662005-08-31T18:28:00031 August 2005 18:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unit 3 Experienced an Automatic Reactor Trip During Routine Testing ENS 405482004-02-26T16:51:00026 February 2004 16:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Rps Actuation While Critical 2022-02-05T08:57:00 | |