On September 8, 2009, during performance of quarterly
Core Spray (
CS) system flow rate testing, a pinhole leak was identified in the 1B
Core Spray Minimum Flow Line. The pinhole leak is located just downstream of the 1B
CS minimum flow valve (1-1402-38B) and cannot be isolated from
primary containment.
At 1935, hours it was determined that structural integrity of the piping could not be assured. Technical Specification 3.6.1.1, Required Action B.1, was entered and a plant shutdown was initiated at 2010 hours0.0233 days <br />0.558 hours <br />0.00332 weeks <br />7.64805e-4 months <br />.
In addition, the 1B Core Spray system was declared inoperable. All other ECCS systems remain operable. The NRC Resident Inspector has been notified.
This event is being reported under 50.72(b)(2)(i) due to the initiation of a shutdown required by the plant's Technical Specifications.
The licensee estimates reactor shutdown will be achieved at 0130
CDT.