ENS 44038
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ENS Event | |
|---|---|
09:00 Mar 6, 2008 | |
| Title | Pin Hole Leak Discovered in 1 Inch Instrument Line During Rpv Pressure Test |
| Event Description | With Unit 1 in Mode 4 for a planned refueling outage, a pin hole leak was discovered on a 1 inch line between the 'A' Main Steam Line (MSL) and MSL flow instrument condensing chamber (1B21-D006B) in a weld at a 45 degree elbow. Leakage was identified as approximately 2 gallons per hour (GPH). This leakage was identified during RPV pressure test while test pressure was 1050 psig.
This elbow is near the 1B21-D006B condensing chamber and is located in the Unit 1 drywell (primary containment). This item constitutes a primary coolant boundary leak discovered while shutdown. The licensee notified the NRC Resident Inspector. |
| Where | |
|---|---|
| Hatch Georgia (NRC Region 2) | |
| Reporting | |
| 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded | |
| Time - Person (Reporting Time:+-3.25 h-0.135 days <br />-0.0193 weeks <br />-0.00445 months <br />) | |
| Opened: | Edwen Urquhart 05:45 Mar 6, 2008 |
| NRC Officer: | Jeff Rotton |
| Last Updated: | Mar 6, 2008 |
| 44038 - NRC Website
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Unit 1 | |
|---|---|
| Reactor critical | Not Critical |
| Scram | No |
| Before | Cold Shutdown (0 %) |
| After | Cold Shutdown (0 %) |
WEEKMONTHYEARENS 575672025-02-22T16:11:00022 February 2025 16:11:00
[Table view]10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Primary Containment Degraded ENS 569592024-02-11T15:11:00011 February 2024 15:11:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Primary Containment Degraded ENS 563422023-02-07T22:38:0007 February 2023 22:38:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Primary Containment Degraded ENS 544632020-01-04T16:09:0004 January 2020 16:09:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Primary Containment Degraded ENS 525672017-02-20T04:23:00020 February 2017 04:23:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Containment Penetration Exceeded Allowable Leakage ENS 517422016-02-16T11:31:00016 February 2016 11:31:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Weld Overlay Flaw Did Not Meet Acceptance Criteria ENS 487952013-02-28T16:55:00028 February 2013 16:55:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Closed Cooling Water Isolation Valve Fails Local Leak Rate Test ENS 487722013-02-20T10:28:00020 February 2013 10:28:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Degraded Condition - Containment Penetration Fails Local Leak-Rate Testing ENS 440382008-03-06T09:00:0006 March 2008 09:00:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Pin Hole Leak Discovered in 1 Inch Instrument Line During Rpv Pressure Test ENS 440052008-02-23T21:00:00023 February 2008 21:00:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Unacceptable Flaw in Rpv Cap-To-Pipe Weld ENS 432242007-03-09T05:30:0009 March 2007 05:30:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Main Steam Line Flow Instrument Line Pressure Boundary Leakage ENS 423722006-02-23T23:50:00023 February 2006 23:50:00 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Degraded Condition of Shroud Tie Rods 2025-02-22T16:11:00 | |
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