ENS 43923
ENS Event | |
---|---|
18:41 Jan 14, 2008 | |
Title | Invalid Actuation of Group 5 and Group 10 Primary Containment Valves During Surveillance Testing |
Event Description | This is not an LER. The reports being made to the NRC under 10 CFR 50.73(a)(2)(iv)(A), and the 60 day telephone notification option under 10 CFR 50.73(a)(1). The event included invalid '. . .general isolation signals affecting containment isolation valves in more than one system. . .' as discussed in 10 CFR 50.73(a)(2)(iv)(B).
The following information is provided as requested in NUREG-1022: (a) The specific train(s) and systems that were actuated? On January 14, 2008 at 13:41 hours. Unit 2 received invalid Division 1 Primary Containment isolation signals to both Group 5 (RHR Shutdown Cooling Isolation valves) and Group 10 (Reactor Core Isolation Cooling [RCIC] system isolation valves) during Division 1 instrumentation surveillance testing. While performing testing, an incorrect lead was lifted causing this invalid actuation. (b) Whether each train actuation was complete or partial. The event resulted in closure of the RCIC steam supply header outboard containment isolation valve. The Division 1 RHR Shutdown Cooling System isolation valves were already closed at the time of the isolation signal. (b) Whether or not the system started and functioned as designed. The Primary Containment isolation instrumentation logic and associated valve closure function (for RCIC) actuated as designed. The licensee took prompt actions to recover the RCIC and RHR systems. The licensee notified the NRC Resident Inspector. |
Where | |
---|---|
Nine Mile Point New York (NRC Region 1) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+193.58 h8.066 days <br />1.152 weeks <br />0.265 months <br />) | |
Opened: | Anthony Petrelli 20:16 Jan 22, 2008 |
NRC Officer: | Jason Kozal |
Last Updated: | Jan 22, 2008 |
43923 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 43923\u003C/a\u003E - \u003Ca href=\"/Nine_Mile_Point\" title=\"Nine Mile Point\"\u003ENine Mile Point\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EInvalid Actuation of Group 5 and Group 10 Primary Containment Valves During Surveillance Testing\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 43923 - Nine Mile Point\n","link":"","lat":43.52021388888889,"lon":-76.40656388888888,"icon":"/w/images/b/be/Constellation_icon.png"}],"imageoverlays":null} | |
Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 535842018-03-19T04:00:00019 March 2018 04:00:00
[Table view]10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 527472017-03-20T06:16:00020 March 2017 06:16:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephone Notification for an Invalid High Pressure Coolant Injection System Actuation ENS 509092015-01-21T15:00:00021 January 2015 15:00:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Notification - Invalid Containment Isolation Signal ENS 490842013-04-02T13:46:0002 April 2013 13:46:00 10 CFR 50.73(a)(1), Submit an LER 6O-Day Optional Telephone Notification for an Invalid Specified System Actuation ENS 485702012-10-12T14:12:00012 October 2012 14:12:00 10 CFR 50.73(a)(1), Submit an LER Temperature Switch Failure Causes Division I Isolation Signal ENS 481132012-05-24T14:20:00024 May 2012 14:20:00 10 CFR 50.73(a)(1), Submit an LER 60 - Day Optional Telephone Notification of an Invalid Division 2 Containment Isolation Signal ENS 475472011-11-08T03:31:0008 November 2011 03:31:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation Due to a Possible Faulty Temperature Switch ENS 457792010-03-15T16:43:00015 March 2010 16:43:00 10 CFR 50.73(a)(1), Submit an LER Inadvertent Start of Emergency Diesel Generator ENS 439232008-01-14T18:41:00014 January 2008 18:41:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Group 5 and Group 10 Primary Containment Valves During Surveillance Testing ENS 438552007-11-08T15:21:0008 November 2007 15:21:00 10 CFR 50.73(a)(1), Submit an LER Invalid Primary Containment Isolation System (Pcis) Actuation ENS 407182004-04-01T07:06:0001 April 2004 07:06:00 10 CFR 50.73(a)(1), Submit an LER Invalid Automatic Start of Emergency Diesel Generator During Surveillance Test 2018-03-19T04:00:00 | |