ENS 42555
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ENS Event | |
---|---|
21:50 May 4, 2006 | |
Title | Unexpected Reactor Protection System (Rps) Actuation During Testing |
Event Description | On May 4, 2006, at 1750 hrs, with the plant in Mode 5, an actuation of the reactor protection system occurred with a single control rod fully withdrawn for testing. The actuation occurred when operators opened the main steam isolation valves (MSIVs) for a separate testing activity, which caused an apparent pressure perturbation with the steam generator level transmitters. The pressure perturbation resulted in the indicated level of 2 of 4 'A' Steam Generator level transmitters oscillating to below the steam generator low level reactor trip setpoint, before returning to the pre-event level. As a result of the reactor protection system actuation, the control rod inserted into the core as expected.
The steam generators were aligned in lay-up condition with a nitrogen blanket present at the time the MSIVs were opened. The event is reportable in accordance with 10 CFR 50.72(b)(3)(iv), as a valid actuation of the reactor protection system. The licensee informed the NRC Resident Inspector. |
Where | |
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Palisades Michigan (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+0.07 h0.00292 days <br />4.166667e-4 weeks <br />9.5886e-5 months <br />) | |
Opened: | Daniel Malone 21:54 May 4, 2006 |
NRC Officer: | Steve Sandin |
Last Updated: | May 4, 2006 |
42555 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Not Critical |
Scram | A/R |
Before | Cold Shutdown (0 %) |
After | Cold Shutdown (0 %) |
WEEKMONTHYEARENS 538192019-01-09T05:00:0009 January 2019 05:00:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip from Full Power Due to Rps Testing ENS 538132019-01-03T05:00:0003 January 2019 05:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Cycling of Turbine Governor Valve ENS 527642017-05-19T06:06:00019 May 2017 06:06:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Reactor Protection System Actuation While Shutdown ENS 513972015-09-16T05:17:00016 September 2015 05:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 475232011-12-14T20:10:00014 December 2011 20:10:00 Other Unspec Reqmnt, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Both Main Feedpumps ENS 472902011-09-25T19:06:00025 September 2011 19:06:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Loss of Two 120 Volt Ac Instrument Busses ENS 465642011-01-22T22:35:00022 January 2011 22:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Generator Load ENS 442372008-05-23T16:49:00023 May 2008 16:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Possible Generator Lockout ENS 439002008-01-13T10:21:00013 January 2008 10:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip After Loss of Main Feedwater Pump ENS 433512007-05-08T17:22:0008 May 2007 17:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Steam Generator Water Level ENS 425552006-05-04T21:50:0004 May 2006 21:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unexpected Reactor Protection System (Rps) Actuation During Testing ENS 419672005-09-01T14:25:0001 September 2005 14:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Main Generator Hydrogen Leak ENS 413192005-01-09T16:27:0009 January 2005 16:27:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Lowering Main Condenser Vacuum ENS 410022004-08-31T11:18:00031 August 2004 11:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rps Actuation Due to Fire in 2B Condensate Pump 2019-01-09T05:00:00 | |
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