ENS 41428
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ENS Event | |
---|---|
08:08 Feb 22, 2005 | |
Title | Emergency Diesel Generator and Emergency Feedwater Auto Start on Vital Bus Failure to Transfer |
Event Description | To support routine preventative maintenance on the 4160V Unit Auxiliary Transformer breaker, 4160V Vital Bus 5 did not successfully transfer to the Reserve Auxiliary Transformer. Bus 5 momentarily de-energized and the Emergency Diesel Generator started and loaded as expected supplying Bus 5. The Emergency Feedwater System actuated as expected on momentary undervoltage to Bus 5. The plant remains stable at 100% power. A station troubleshooting team has been established.
The reason that Bus 5 did not transfer to the Reserve Auxiliary Transformer is not known at this time. The licensee notified the NRC Resident Inspector. |
Where | |
---|---|
Seabrook New Hampshire (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-1.8 h-0.075 days <br />-0.0107 weeks <br />-0.00247 months <br />) | |
Opened: | Mike Taylor 06:20 Feb 22, 2005 |
NRC Officer: | Mike Ripley |
Last Updated: | Feb 22, 2005 |
41428 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 574312024-11-19T18:50:00019 November 2024 18:50:00
[Table view]10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 574322024-11-19T18:50:00019 November 2024 18:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 566452023-07-30T19:26:00030 July 2023 19:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to LOW Main Turbine ELECTRO-HYDRAULIC Control (EHC) Oil Level ENS 565652023-05-06T19:52:0006 May 2023 19:52:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuations of Reactor Protection System ENS 565642023-04-12T15:07:00012 April 2023 15:07:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of "B" Emergency Diesel Generator Emergency Power Sequencer ENS 527182017-04-29T22:44:00029 April 2017 22:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Steam Generator Hi-Hi Level Signal and Feedwater Isolation ENS 517652016-03-02T18:12:0002 March 2016 18:12:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of Emergency Feedwater ENS 517622016-03-02T07:53:0002 March 2016 07:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip Causing a Reactor Trip ENS 473272011-10-06T16:26:0006 October 2011 16:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Low Steam Generator Water Level ENS 454032009-10-02T02:39:0002 October 2009 02:39:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit Experienced a Valid Rps Actuation During Plant Cooldown on Low Steam Generator Levels ENS 439212008-01-20T04:02:00020 January 2008 04:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Following Turbine Trip ENS 416552005-05-01T15:09:0001 May 2005 15:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Main Turbine High Vibration ENS 415932005-04-13T08:50:00013 April 2005 08:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation During Core Reload Reactor Trip Breakers Opened ENS 414282005-02-22T08:08:00022 February 2005 08:08:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator and Emergency Feedwater Auto Start on Vital Bus Failure to Transfer ENS 402862003-11-01T00:48:0001 November 2003 00:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip on Low Steam Generator Water Level 2024-11-19T18:50:00 | |
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