The following information was provided by the licensee via e-mail:
On February 10, 2005, plant operators observed an abnormal flow condition on Unit 2 Train 'B' Component Cooling Water (CCW) from the Shutdown Cooling Heat (SDC) exchanger and, at about 2315 PST, declared Train 'B' of Containment Spray inoperable. This caused Unit 2 to enter a seven-day action statement (TS 3.6.6.1).
Although it may have been possible to correct the abnormal flow condition on-line, SCE has elected to shutdown Unit 2. Plant Operators initiated the shutdown at about 2155 PST on February 14, 2005. SCE in reporting this occurrence in accordance with 10CFR50.72(b)(2)(i).
At the time the shutdown was initiated, Unit 2 was operating at about 100% power. Unit 3 continues to operate at about 100 % power. The NRC Resident Inspectors have been briefed on the shutdown plans and will be provided with a copy of this report.