3F0602-04, May 2002 Monthly Operating Report for Crystal River Unit 3
| ML021710182 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 06/12/2002 |
| From: | Franke J Florida Power & Light Co |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| 3F0602-04, ITS 5.7.1.2 | |
| Download: ML021710182 (3) | |
Text
j Florida Power A Progress Energy Company Crystal River Nuclear Plant Docket No. 50-302 Operating License No. DPR-72 Ref: ITS 5.7.1.2 June 12, 2002 3F0602-04 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001
Subject:
Crystal River Unit 3 - Monthly Operating Report
Dear Sir:
Florida Power Corporation hereby submits the Crystal River Unit 3 (CR-3) May 2002 Monthly Operating Report in accordance with CR-3 Improved Technical Specification 5.7.1.2.
If you have any questions regarding this submittal, please contact Mr. Sid Powell, Supervisor, Licensing and Regulatory Programs at (352) 563-4883.
Sincerely, ZJ. A. Franke Plant General Manager JAF/ff Attachment xc:
Regional Administrator, Region II Senior Resident Inspector NRR Project Manager Crystal River Nuclear Pla it i 5760 V Po wer Liwe Street Crys al River, FL 34428
APPENDIX A OPERATING DATA REPORT DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE REPORTING PERIOD (Month/Year):
50-302 FLCRP-3 June 3, 2002 J.E. Lane '
ý70 (352) 795-6486 x3698 May 2002 MONTH DESIGN ELECTRICAL. RATING (MWe-Net)
MAXIMUM DEPENDABLE CAPACITY (Mwe-Net)
NUMBER OF HOURS REACTOR WAS CRITICAL NUMBER OF HOURS THE GENERATOR WAS ON LINE UNIT RESERVE SHUTDOWN HOURS NET ELECTRICAL ENERGY GENERATED (MWH) 1 2
3 4
5 6
YEAR TO DATE 825 834 CUMULATIVE 725.0 717.4 0.0 594,143 3,604.0 3,596.4 0.0 3,037,149 153,011 150,719 0
117,006,412
APPENDIX B UNIT SHUTDOWNS DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE 50-302 FLCRP-3 June 3, 2002 J. E. Lane (352) 795-6486 x3698 REPORTING PERIOD:
May 2002
SUMMARY
Crystal River Unit 3 operated at full power for the majority of the month of May.
There was a planned outage from 5/17/02 to 5/19/02 to repair an oil leak on Reactor Coolant Pump 1A (RCP-1A) motor.
(1) Reason:
A-EQUIPMENT FAILURE (Explain)
B-MAINTENANCE OR TEST C-REFUELING D-REGULATORY RESTRICTION E-OPERATOR TRAINING / LICENSE EXAMINATION F-ADMINISTRATIVE G-OPERATIONAL ERROR (Explain)
H-OTHER (Explain)
(2) Method:
1-MANUAL 2-MANUAL TRIP / SCRAM 3-AUTO TRIP / SCRAM 4-CONTINUATION 5-OTHER (Explain)
No.
Date Type Duration Reason Method of Cause / Corrective Actions F: Forced (Hours)
(1)
Shutting S: Scheduled Down (2)
Comments 2002-01 5/18/02 S
26.6 B
1 The unit was taken off-line to repair an oil leak on RCP-1A motor lower oil reservoir. Total generation lost was 34,543 MWHs. During the ramp down, 5,013 MWHs were lost, 23,582 MWHs were lost while at 0%
power, and 5,948 MWHs were lost during escalation back to 100% power.