05000457/LER-2023-001, Train B Auxiliary Feedwater Pump Was Inoperable Due to Degraded Oil in the Crank Case

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Train B Auxiliary Feedwater Pump Was Inoperable Due to Degraded Oil in the Crank Case
ML23321A224
Person / Time
Site: Braidwood Constellation icon.png
Issue date: 11/17/2023
From:
Constellation Energy Generation
To:
Office of Nuclear Reactor Regulation
Shared Package
ML23321A222 List:
References
BW230053 LER 2023-001-00
Download: ML23321A224 (1)


LER-2023-001, Train B Auxiliary Feedwater Pump Was Inoperable Due to Degraded Oil in the Crank Case
Event date:
Report date:
4572023001R00 - NRC Website

text

Abstract

On September 1, 2023, an oil sample from the 2B auxiliary feedwater (AF) pump diesel engine was obtained. On September 21, 2023, the oil sample results were received which indicated oil viscosity and fuel percent in the Fault range, and a confirmatory sample was drawn. On September 22, 2023, resample results were received confirming the original analysis, and at 1157 Operations declared the 2B AF train INOPERABLE and entered Technical Specification (TS) Limiting Condition for Operation (LCO) 3.7.5, "Auxiliary Feedwater (AF) System," Condition A, "One AF train inoperable." Maintenance was performed to repair fuel leaks and crankcase oil was changed. The 2B AF train was returned to service on September 23, 2023, at 1340, and at 1501 LCO 3.7.5 was exited.

The cause of the event was vendor performance and quality control gap in refurbishing fuel injectors. The corrective action was repair of the 2B AF diesel engine lube oil fuel leaks. A supplement to this report will be provided as more information is available.

(See Page 2 for required number of digits/characters for each block)

(See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1022/r3/) Page 3 of 3

E. Corrective Actions

The 2B AF diesel engine fuel leaks into lube oil were repaired and performed a crankcase oil change.

Further corrective actions are still under consideration and any revisions or additions will be reported in a supplement to this report.

F. Previous Occurrences

April 10, 2019, Braidwood Unit 1, the 1B AF pump engine degrading trend in fuel oil content was identified. Evaluation identified the cause as most likely a leaking fitting within the rocker/valve cover. No operability or reportability issues resulted. The cause of the leakage in 2019 is unrelated to the current issue.

G. Component Failure Data

Manufacturer Nomenclature Model Mfg. Part Number Paragon Energy Solutions Diesel engine - fuel injector 16V149T1 R5229660