05000456/LER-2004-002, Regarding 1 C Reactor Containment Fan Cooler Discovered to Be Inoperable Greater than Required Technical Specification Allowed Outage Time

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Regarding 1 C Reactor Containment Fan Cooler Discovered to Be Inoperable Greater than Required Technical Specification Allowed Outage Time
ML042230220
Person / Time
Site: Braidwood 
Issue date: 08/02/2004
From: Joyce T
Exelon Generation Co, Exelon Nuclear
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
BW040076 LER 04-002-00
Download: ML042230220 (5)


LER-2004-002, Regarding 1 C Reactor Containment Fan Cooler Discovered to Be Inoperable Greater than Required Technical Specification Allowed Outage Time
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
4562004002R00 - NRC Website

text

Exe n SM Exelon Generation Company, LLC www.exeloncorp.coM Nuclear Braidwood Station 35100 South Rt 53, Suite 84 Braceville, IL 60407-9619 Tel. 815-417-2000 August 2, 2004 BW040076 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Braidwood Station, Unit 1 Facility Operating License No. NPF-72 NRC Docket No. STN 50-456

Subject:

Submittal of Licensee Event Report Number 2004-002-00, "1 C Reactor Containment Fan Cooler Discovered to be Inoperable Greater Than Required Technical Specification Allowed Outage Time" The enclosed Licensee Event Report (LER) is being submitted in accordance with 10 CFR 50.73, "Licensee event report system", paragraph (a)(2)(i)(B). 10 CFR 50.73(a) requires an LER to be submitted within 60 days after discovery of the event; therefore, this report is being submitted by August 2, 2004.

Should you have any questions concerning this submittal, please contact Scott Butler, Acting Regulatory Assurance Manager, at (815) 417-2815.

Respectfully, Thomas Joy Site Vice President Braidwood Station

Enclosure:

LER Number 2004-002-00 cc:

Regional Administrator - Region IlIl NRC Braidwood Senior Resident Inspector

NRC FQRM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7-2001)

COMMISSION

, the NRC may not conduct or sponsor, and a person Is not required to respond to, the Information collection.

I 3. PAGE Braidwood, Unit 1 STN 05000456 1

1 of 4

4. TITLE iC Reactor Containment Fan Cooler discovered to be inoperable greater than required Technical Specification Allowed Outage Time
5. EVENTDATE
6. LER NUMBER
7. REPORTDATE
8. OTHER FACILITIES INVOLVED M

O YY EI YtQUtN IAU L IRVO i

H Y:ARIUTY NAhILNMEGKET NUMBER NUMBER NO N/A N/A 06 01 20041 2004-002-00 08 02 2004 N/A (N/A

.PEAING 1

. THIS REPORT IS BMITTED PURSUANT TTHE REQUIREMENTS OF 10 CFR §: (Check all that apply)

MODE 20.2201(b) 20.2203(aX3Xi) 50.73(aX2XiXC) 50.73{aX2XvIi)

10. POWER 100 20.2201f(d)

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12. LICENSEE CONTACT FOR THIS LER NAME i TELEPHONE NUMBER (Include Area Code)

Gary Dudek, Operations Director l(815) 417-2200

13. COMPLETE ONE UNE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT

CAUSE

l SYSTEM I COMPONENT MANU REPORTABL CA SYSTEM l COMPONENT l AUFACTURER l REPORTABLE IIFACTURER TO i

CAUSE

SYTE COPNN MAUACUE TOEPORTBL N/A N/A N/A N/A N/A N/A N/A N/A N/A N/A

14. SUPPLEMEN rALREPORT EXPECTED 0
15. EXPECTED MONTH DAY YEAR iYes(f yes, complete EXPECTED SUBMISSION DATE).

X NO 1

SUBMISSION x I j

DATE

ABSTRACT

On June 1, 2004, during the monthly Reactor Containment Fan Cooler the iC RCFC Essential Service Water (SX) flow rate was found below Specification (TS) 3.6.6 limit of 2660 gpm due to low flow through Flow had been last adjusted on May 6, 2004.

(RCFC) surveillance, the Technical one bank of the RCFC.

The investigation determined that SX flow indicator lF-SX118 was inaccurate when the flow was set on May 6, 2004 due to flow indicator fouling.

The inaccurate flow indication was not recognized due to inadequate management decisions relating to the effects of the Braidwood lake precipitation event that occurred in February 2004.

Organizational and programmatic issues were identified that contributed to the failure to recognize the flow degradation of the lF-SX118 indication loop and related piping following the lake precipitation event.

The consequence of this event is the failure to meet the TS Limiting Condition for Operation due to inoperability of the lC RCFC.

The low flow condition in the lC RCFC may have resulted in silt build-up of the lC RCFC cooling coils with a resulting failure of the IC RCFC thermal performance test.

The safety consequences of this event are minimal.

This event is being reported pursuant to 10CFR50.73(a)(2)(i)(B).U.S. NUCLEAR REGULATORY COMMISSION (1-200.)

LICENSEE EVENT REPORT (LER)

FACILITY NAME (1)

DOCKET (2)

LER NUMBER (6)

PAGE (3)

YEAR SEQUeTI RRVISION NtMBfl NUMBE Braidwood, Unit 1 STN 05000456 l

l 2 of 4 ff:2004

- 002 - 00 l

A.

Plant Operating Conditions Before The Event

Unit: 1 Event Date: June 1, 2004 Event Time: 1338 MODE: 1 Reactor Power: 100 percent Reactor Coolant System (RCS)[AB] Temperature: 587 degrees F, Pressure: 2236 psig B.

Description of Event

There were no additional systems or components inoperable at the beginning of this event that contributed to the severity of the event.

On May 6, 2004, during performance of lBwOSR 3.6.6.2, "Reactor Containment Fan Cooler Surveillance," the as found Essential Service Water (SX) [BIE flow values to the two cooling coil banks for the lC Reactor Containment Fan Cooler (RCFC)

[IK] were 1420 gpm on flow indicator lF-SX124 and >1700 gpm on flow indicator lF-SX118.

Since the flow to the IC RCFC was greater than the specified band in the surveillance, the Shift Manager authorized adjusting the lF-SX118 flow.

A non-licensed operator (NLO) adjusted 1SX021C (the throttle valve for 1F-SX118) to reduce flow.

The procedure is performed by two NLOs inside of containment.

The "valve NLO" is on one elevation and the "gauge NLO" is on another elevation (valve lSX021C is physically located on one elevation and the flow gauge lF-SX118 is located on another elevation).

As the valve NLO adjusted lSX021C, the gauge NLO monitored flow on lF-SX118.

The valve NLO made several small adjustments to ISX021C before the flow indicated on lF-SX118 responded and returned from the pegged high condition (gauge band is from 0 to 1700 gpm) to within the gauge band.

Flow on lF-SX118 stabilized at 1400 gpm.

The gauge NLO monitored the flow on IF-SX118 for one to two minutes to ensure the flow was stable so that the NLOs would not have to re-perform the surveillance.

The valve NLO locked lSX021C in the throttled position.

The gauge NLO verified SX flow was still stable at 1400 gpm, then went to lSX021C and verified the valve was locked.

The NLOs did not check valve position because IBwOSR 3.6.6.2 stated to adjust the flow to a specified flow range and not to a valve position.

It was later determined that valve 1SX021C was locked at the 8* open position.

The NLOs checked the other flow gauge lF-SX124 and found flow at 1400 gpm.

On June 1, 2004, lBwOSR 3.6.6.2 was performed as part of the monthly scheduled surveillance.

The NLOs in containment noted that the SX flows to the lC RCFC were below the Technical Specification (TS) limit for flow of 2660 gpm with SX flow to lF-SX124 at 1440 gpm and SX flow to lF-SX118 at 475 gpm (total flow =

1915 gpm).

The surveillance was stopped, the Shift Manager was notified and TS Limiting Condition for Operation (LCO) 3.6.6 was entered.

The SX flow to the lC RCFC was not adjusted at this time to preserve the as-found conditions for troubleshooting purposes.U.S. NUCLEAR REGULATORY COMMISSION L(1-20011) l0 LICENSEE EVENT REPORT (LER)

FACILITY NAME (1)

DOCKET (2)

LER NUMBER (6)

PAGE (3)

YEAR SEQUENTIAL REVISION NNUMBER Braidwood, Unit 1 STN 05000456 l l 3 of 4 2004 - 002 - 00 l

Investigation and testing identified that the flow indicated on lF-SX118 had a delayed time response due to flow indicator fouling.

Following venting, blowing down and back flushing the sensing lines and recalibrating the gauges, accurate flow indicated on lF-SX118 was restored and verified by an ultrasonic measurement.

Based on accurate flow indication of approximately 450 gpm, it was identified that 1SX021C had been throttled too far closed on May 6, 2004.

lSX021C was throttled open until proper flow was established, and LCO 3.6.6 was exited at 1955 on June 2, 2004.

The last recorded flow for both banks of SX cooling for iC RCFC was performed on May 6, 2004.

Since no valve position had been changed since the last performance, the IC RCFC was determined to be inoperable since May 6, 2004.

The LCO allowed outage time for the RCFCs per LCO 3.6.6 is seven days.

Therefore, the IC RCFC was determined to be inoperable for greater than the allowed LCO outage time per LCO 3.6.6.

C.

Cause of Event

The root cause for this event was inadequate management decisions relating to the effects of the February 2004 Braidwood lake precipitation event.

This caused management to focus on identifying another lake precipitation event which prevented the Station from adequately monitoring the IC RCFC performance.

The following are aspects of the inadequate technical rigor discussed above.

There were missed opportunities to identify the inaccurate indications on iF-SX118. An Adverse Condition Monitoring (ACM) plan was initiated on February 2, 2004, to monitor the SX flows to various safety related components and to identify if additional degradation of safety related equipment was occurring due to the February 2004 lake precipitation event.

The ACM plan did not initially identify the RCFCs as part of the plan to monitor RCFC performance. After the RCFCs were incorporated into the ACM plan, the plan did not adequately monitor the RCFCs nor provide direction on what to do with the data once it was recorded.

In addition, the plan did not monitor or record throttle valve positions on the RCFCs.

Other opportunities to identify problems with the IC RCFC flow indication were also missed on three occasions when significant adjustments of flow were made but not recognized as indicative of potential flow indication inaccuracies.

D.

Safety Consequences

The low flow condition in the IC RCFC, from May 6, 2004, to June 2, 2004, resulted in silt build-up on the iC RCFC cooling coils with a subsequent failure of the IC RCFC thermal performance test on June 29, 2004.

The safety consequences of this event are minimal.

A risk assessment was performed and concluded the associated risk was low.

The containment cooling system design is analyzed for a loss of one train of containment spray (CS) and one train of RCFCs (one train contains two RCFCs).

The inoperability of one RCFC is within the plant design criteria.

A 100 percent capacity redundant RCFC train was operable during the event.

Although the lC RCFC failed its thermalU.S. NUCLEAR REGULATORY COMMISSION (1;.20W.)

LICENSEE EVENT REPORT (LER)

FACILITY NAME (I)

DOCKET (2)

LER NUMBER (6)

PAGE (3)

YA SEQWUNTIAL REVISION BaMiwR NU004ER Braidwood, Unit 1 STN 05000456 l 4 of 4 2004 - 002 -

00 performance test on June 29, 2004, subsequent evaluation demonstrated that, based on actual SX temperatures, the 1C RCFC could have performed its design function at all times with the exception of a cumulative period of three days and five hours (the longest consecutive period was two days and eleven hours) in June 2004.

This was within the acceptable LCO 3.6.6 completion time.

This event did not result in a safety system functional failure.

E.

Corrective Actions

The corrective action to prevent recurrence was the implementation of the new process for increased technical rigor in creating adverse condition monitoring plans in accordance with the procedure titled "Technical Task Risk/Rigor Assessment Pre-Job Brief, Independent Third Party Review, and Post-Job Brief."

In addition, a case study of the decision making deficiencies identified during this event will be developed and will be presented to appropriate personnel.

Additional actions include cleaning each of the annubar flow elements on both unit RCFCs and recalibrating the SX flow instruments to ensure correct flow rates are provided.

F.

Previous Occurrences

There have been no similar Licensee Event Report events at Braidwood Station.

In February 2002, Braidwood Station had a lake precipitation event that affected the non-essential service water system (WS)

[KG] but not the SX system.

G.

Component Failure Data

Manufacturer Nomenclature Model Mfg. Part Number N/A N/A N/A N/A