05000425/LER-2007-002

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LER-2007-002, Unit 2 Main Generator tripped, resulting in an automatic reactor trip
Docket Number(S)
Event date: 04-23-2007
Report date: 00-0-5000
4252007002R00 - NRC Website

A. REQUIREMENT FOR REPORT

10 CFR 50.73 (a)(2)(iv)(A) requires this report because an unplanned actuation of the reactor protection system (RPS) occurred.

B. UNIT STATUS AT TIME OF EVENT

At the time of this event, Unit 2 was in Mode 1 (Power Operation) at approximately 54% rated thermal power during power ascension following completion of refueling outage 2R12. Other than that described herein, there was no inoperable equipment that contributed to the occurrence of this event.

C. DESCRIPTION OF EVENT

On April 23, 2007, at 1024 EDT, Unit 2 experienced an automatic reactor trip from approximately 54% power during power ascension following completion of refueling outage 2R12. The main generator neutral overcurrent relay actuated resulting in a Generator/Turbine/Reactor trip. All safety related systems responded as designed, and the plant was stabilized in Mode 3. The NRC Operations Center was notified of this event on April 23, 2007 at 1125 EDT.

Investigation of the event revealed that a ground fault had occurred as a result of stator water leaking out of the tang area of the main generator 'A' phase bushing and saturating the bushing insulation. The wet insulation provided the ground fault path. The fault started tracking through the wet insulation and carbonized the path, which then led to increased tracking and eventually reaching a level which caused the main generator neutral overcurrent relay to actuate. This caused a lockout relay to actuate which resulted in a Generator/Turbine/ Reactor trip.

D. CAUSE OF EVENT

Investigation determined that the primary cause of this event was the design of the main generator bushing tang assembly due to the use of a cast copper tang assembly and braze material that is susceptible to crevice corrosion. The bushing tang connects the bushing to the phase connection. The tang is water cooled along with the remainder of the bushing assembly. The leak locations were at the top of the tang where a rectangular plate was brazed to the cast tang assembly. Possible causes of the leak include crevice corrosion, porosity in the copper casting, or a bad braze. The various other joints in the bushing assembly are field brazed. All the brazed connections in the main generator utilize the same braze process.

To compensate for this design susceptibility, operating procedures should have required the main generator hydrogen pressure to be maintained at a higher pressure than stator water. This operating strategy was not a requirement of the original design but was a result of stator water leaks encountered in the industry. The procedure changes recommended by GE Technical Information Letter (TIL) 1098, "Inspection of Generators with Water Cooled Stator Windings" in May, 1991 were implemented into the operating procedures. However, revisions made to the operating procedures in 2001 relaxed these requirements by allowing the main generator hydrogen pressure to be at a lower pressure than stator water for short periods of operation (i.e. less than one week).

The 2R12 refueling outage did not include any significant main generator maintenance activities. A major factor in this event was that stator cooling was run for approximately 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> after the main generator was degassed at the beginning of 2R12 refueling outage. Given the leaks in the bushing tang, these 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> of stator cooling operation would have allowed the insulation to become saturated. Since this connection is taped and epoxy coated, it would not have dried out appreciably during the 2R12 refueling outage. Once the unit was started up from 2R12, current started tracking through the wet insulation, carbonizing the path, which eventually resulted in the electrical fault to ground on the 'A' phase bushing.

E. ANALYSIS OF EVENT

The Reactor Protection System (RPS) is designed to generate a reactor trip signal due to a generator / turbine trip when the reactor is operating above the P-9 permissive. When the main generator neutral overcurrent relay actuated, the RPS functioned as designed to trip the reactor. All safety related systems responded as designed, and the plant was stabilized in Mode 3. Based on these considerations, there was no adverse effect on plant safety or on the health and safety of the public as a result of this event.

This event does not represent a safety system functional failure.

F. CORRECTIVE ACTIONS

1. The leak in the 'A' phase bushing tang assembly was repaired prior to restart.

2. Helium tracer gas testing was performed on all three bushing tang assemblies prior to restart.

3. Stator Cooling System and Generator Gas System operating procedures have been revised to include the appropriate guidance to prevent water intrusion into the main generator from stator cooling in the event of a leak.

G. ADDITIONAL INFORMATION

1) Failed Components:

None 2) Previous Similar Events:

None 3) Energy Industry Identification System Codes:

Main Generator System — TB Main Generator Stator Cooling System — TJ