05000389/LER-2013-001, Regarding Unplanned Manual Reactor Trip Due to Algae

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Regarding Unplanned Manual Reactor Trip Due to Algae
ML13219A841
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 07/29/2013
From: Jensen J
Florida Power & Light Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
L-2013-204 LER 13-001-00
Download: ML13219A841 (4)


LER-2013-001, Regarding Unplanned Manual Reactor Trip Due to Algae
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
3892013001R00 - NRC Website

text

0FPL.

July 29, 2013 L-2013-204 10 CFR 50.73 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C. 20555 Re:

St. Lucie Unit 2 Docket No. 50-389 Reportable Event: 2013-001-00 Date of Event: May 31, 2013 Unplanned Manual Reactor Trip Due to Algae The attached Licensee Event Report 2013-001 is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.

Very truly yours, Joseph N. Jensen Site Vice President St. Lucie Plant JJ/rcs/mkm Attachment Florida Power & Light Company 6501 S. Ocean Drive, Jensen Beach, FL 34957

TRC FORM 366 U.S.

NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

I. FACILITY NAME

2.

DOCKET NUMBER 73. PAGE St. Lucie Unit 2 05000389 OF 3

4. TITLE Unplanned Manual Reactor Trip Due to Algae
5.

EVENT DATE

6.

LER NUMBER r

7.

REPORT DATE I

8.

OTHER FACILITIES INVOLVED YSEQUENTIA REV FACILITY NAME DOCKET YEAR YEAR LQNUMBER NO. I MONTH DAY YEAR NA NUMBER LNUMBERNNOBER 5

31 201 2013 001 00 I07 29 2013 FCLTNAED KT I

FACILITY NAME DOCKET NUMBER

9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR§: (Check all that apply)

[1 20.2201(b)

El 20.2203(a)(3)(i)

[I 50.73(a)(2)(i)(C)

El 50.73(a)(2)(vii)

El 20.2201(d)

El 20.2203(a)(3)(ii)

El 50.73(a)(2)(ii)(A)

[] 50.73(a)(2)(viii)(A)

El 20.2203(a)(1)

El 20.2203(a)(4)

El 50.73(a)(2)(ii)(B)

El 50.73(a)(2)(viii)(B)

[I 20.2203(a)(2)(i)

El 50.36(c)(1)(i)(A)

[I 50.73(a)(2)(iii)

El 50.73(a)(2)(ix)(A)

10. POWER LEVEL El 20.2203(a)(2)(ii)

El 50.36(c)(1)(ii)(A)

Z 50.73(a)(2)(iv)(A)

C] 50.73(a)(2)(x)

El 20.2203(a)(2)(iii)

El 50.36(c)(2)

El 50.73(a)(2)(v)(A)

El 73.71(a)(4) 40%

El 20.2203(a)(2)(iv)

El 50.46(a)(3)(ii)

El 50.73(a)(2)(v)(B)

El 73.71(a)(5)

El 20.2203(a)(2)(v)

El 50.73(a)(2)(i)(A)

El 50.73(a)(2)(v)(C)

OTHER El 20.2203(a)(2)(vi)

El 50.73(a)(2)(i)(B)

El 50.73(a)(2)(v)(D)

Specify in Abstract below or in

Corrective Actions

The corrective actions listed below are entered into the site corrective action program.

Any changes to the actions will be managed under the corrective action program.

1. Replace the DPMS flush water check valves with a more robust design to be more reliable.
2.

Revise the preventative maintenance for the DFS to establish a replacement frequency of once per operating cycle for DFS flush water check valves.

Similar Events

A similar event occurred at St. Lucie on April 1, 2009 involving ingress of algae.

St. Lucie has experienced similar plant trips as a result of intake and jelly fish intrusion and/or related equipment failures.

Prior troubleshooting did not identify this possible degradation mechanism for the DPMS and flush water check valves.

A review of nuclear industry events also identified several similar events associated with traveling water screens and intake system blockage/intrusion resulting from algae and intake debris.

Failed Component(s)

Flush Water Check Valve Manufacturer The DPMS design was part of the original Taprogge modification to install the DFS strainers.

The flush water check valves are Nupro stainless steel poppet check valves (Part number SS6C4-l).