05000353/LER-2005-003, Regarding Operation Exceeding License Maximum Power Level

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Regarding Operation Exceeding License Maximum Power Level
ML051790351
Person / Time
Site: Limerick Constellation icon.png
Issue date: 06/28/2005
From: Degregorio R
Exelon Generation Co, Exelon Nuclear
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
FOL 2.E LER 05-003-00
Download: ML051790351 (7)


LER-2005-003, Regarding Operation Exceeding License Maximum Power Level
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
3532005003R00 - NRC Website

text

FOL 2.E June 28, 2005 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Limerick Generating Station, Unit 2 Facility Operating License No. NPF-85 NRC Docket No. 50-353

Subject:

LER 2-05-003, Transient Exceeded Licensed Maximum Power Level This Licensee Event Report (LER) addresses a period of operation between 100% and 107%

of rated thermal power due to a speed control failure on the 2A reactor recirculation pump motor-generator. This event resulted in a license violation regarding the maximum power level limit of 3458 megawatts thermal.

Report Number:

2-05-003 Revision:

00 Event Date:

May 31, 2005 Discovered Date:

May 31, 2005 Report Date:

June 28, 2005 This LER is being submitted pursuant to the requirements of License Condition 2.E, which requires a 30-day written followup in accordance with the procedures described in 10CFR50.73(b), (c), and (e).

If you have any questions or require additional information, please do not hesitate to contact us.

Sincerely, Original signed by Ron J. DeGregorio Vice President - Limerick Exelon Generation Company, LLC cc: S. J. Collins, Administrator Region I, USNRC S. L. Hansell, USNRC Senior Resident Inspector, LGS

SUMMARY OF EXELON NUCLEAR COMMITMENTS LS-AA-117-1003 Rev. 2 The following table identifies commitments made in this document. Any other actions discussed in the submittal represent intended or planned actions. These actions are described to the NRC for the NRCs information and are not intended as regulatory commitments.

Commitment #1 Committed Date (or Outage):

None None

NRC FORM 366 U.S. NUCLEAR REGULATORY (1-2001)

COMMISSION LICENSEE EVENT REPORT (LER)

(See reverse for required number of digits/characters for each block)

APPROVED BY OMB NO. 3150-0104 EXPIRES 6-30-2001 Estimated burden per response to comply with this mandatory information collection request:

50 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br />. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T-6 E6), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to bjs1@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202 (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection FACILITY NAME (1)

DOCKET NUMBER (2)

PAGE (3)

Limerick Generating Station, Unit 2 05000 353 1

OF 4

TITLE (4)

Operation Exceeding License Maximum Power Level EVENT DATE (5)

LER NUMBER (6)

REPORT DATE (7)

OTHER FACILITIES INVOLVED (8)

FACILITY NAME DOCKET NUMBER MO DAY YEAR YEAR SEQUENTIAL NUMBER REV NO MO DAY YEAR 05000 FACILITY NAME DOCKET NUMBER 05 31 2005 2005 003 00 06 28 2005 05000 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) (11)

OPERATING MODE (9) 1 20.2201(b) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(B) 50.73(a)(2)(ix)(A) 20.2201(d) 20.2203(a)(4) 50.73(a)(2)(iii) 50.73(a)(2)(x)

POWER LEVEL (10) 100 20.2203(a)(1) 50.36(c)(1)(i)(A) 50.73(a)(2)(iv)(A) 73.71(a)(4) 20.2203(a)(2)(i) 50.36(c)(1)(ii)(A) 50.73(a)(2)(v)(A) 73.71(a)(5) 20.2203(a)(2)(ii) 50.36(c)(2) 50.73(a)(2)(v)(B) x 20.2203(a)(2)(iii) 50.46(a)(3)(ii) 50.73(a)(2)(v)(C) 20.2203(a)(2)(iv) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(D)

OTHER Specify in Abstract below or in (If more space is required, use additional copies of (If more space is required, use additional copies of (If more space is required, use additional copies of NRC Form 366A) (17)

The scoop tube positioner operates using a servo-amplifier circuit to nullify input error. This circuit is comprised of a set of balanced transistors that provide the firing pulses to opposing SCRs that regulate the positioner drive motor armature current. At steady state, the SCR pulses counteract each other to maintain the scoop tube position at the operator defined setpoint. The inputs to the servo-amplifier circuit are the reactor recirculation pump (RRP) speed controller output and feedback from an internal positioner Linear Variable Displacement Transducer (LVDT). When an imbalance is introduced (i.e., error signal via a demanded speed change) the amplifier responds by increasing the number of firing pulses in the appropriate direction to resolve the error.

Cause of the Event

The cause of the event was a failure of the 2A reactor recirculation pump motor-generator fluid coupler scoop tube positioner speed control amplifier. A PTH connector failed on a printed circuit card that was located in the scoop tube positioner.

Corrective Action Completed The printed circuit card was replaced and the speed control was restored to normal operation.

Corrective Action Planned An evaluation of the vendor refurbishment practices for Bailey servo-amplifier cards will be performed. This action will be complete by September 30, 2005.

Previous Similar Occurrences There were no previous occurrences of a failure of the reactor recirculation pump motor-generator speed control that caused power to exceed the licensed maximum power level.

Component Data Component: XC-M1-2R622A Recirculation Flow Control A Controller

Cause

B (Design, Manufacturing, Construction/Installation)

System:

AD (Reactor Recirculation System)

Component:

SC (Control, Speed)

Manufacturer:

B045 (ABB Automation Inc.)

Model number:

721002AAAA1 Part Number 6619848A1 Serial number:

171869 Stock code number: 115-00478