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S AN ATOG A. PENNSYLV ANI A 19464 (rio 27 iroc axv rooo
- February 7, 19'90 M. J. McCORMIC K J... P e.
Docket No. 50-353
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License No. NPF-85 U.S. Nuclear Regulatory Commission
' Attn:. Document Control Desk v
Washington, DC 20555
SUBJECT:
Licensee Event Report Limerick Generating Station - Unit 2 This LER reports a condition prohibited by Technical-Specifications in that the Reactor Enclosure (RE) low difterential pressure:- low isolation actuation instrumentation.
- - had.been: unavailable to perform its intended safety function for-
' longer than the. Technical Specifications allowed maximum two hour time limit.- In' addition, during restoration of the normal RE ventilation system,1an' isolation of the RE ventilation system, an Engineered Safety-Feature, occurred on low differential pressure.
- - Reference:'
Docket Nos. 50-353' Report Number:
2-90-001 Revision: Number:
00 Event:Date:
January 8, 1990 Report Date:
February
.7, 1990
- Facility:.
Limerick Generating Station
'P.O.
Box A, Sanatoga, PA 19464 This LER is being submitted pursuant to.the' requirements of 10 CFR 50.73(a)(2)(iv) and 50.73(a)(2)(1)(B).
Very truly yo rs, I
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W. T. Russell, Administrator, Region I, USNRC T. J. Kenny, USNRC Senior Resident Inspector, LGS o
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On January 8, 1990, a condition prohibited-by Technical Specifications (TS) was identified in that the outside atmosphere to Reactor Enclosure (RE) differential pressure-low isolation actuation instrumentation had been unavailable to perform its intended safety function and the associated action had not been taken within the required time period.
Following restoration of E
L
.the normal RE ventilation (after completion of scheduled l.
maintenance), an inadvertent isolation of the RE secondary l'
containment and initiation of the Standby Gas Treatment System l
and Reactor Enclosure Recirculation System, both Engiireered Safety Features, occurred due to a low differential pressure isolation logic trip.
The TS violation was caused by a personnel error by Main Control Room Operators when they failed to restore i
l the outside atmosphere to RE differential pressure-low L
instrumentation channels to operable status within the TS required time period.
The isolation of the RE ventilation system was due to the local ' Auto / Test' switches being left in the l
' Test' position rather than the ' Auto' position during RE System l
Shutdown for scheduled maintenance.
The root cause of the 1
l improper local switch position was due to insufficient l-communication between the Chief Operator (CO) and the Shift Supervisor (SSV).
The CO was counseled on the importance of communicating all pertinent information.
In addition, the SSV was counseled on the importance of considering all available information when making decisions.
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Unit' Conditions' Prior to the Event:
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. Operating Condition:
1 (Power Operation)
- Power Level.:
100%
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Description of the Event:
On January 8, 1990, at 1914 hours0.0222 days <br />0.532 hours <br />0.00316 weeks <br />7.28277e-4 months <br />, a condition prohibited'by Technical Specifications (TS) was identified.in that the outside atmosphere to Reactor Enclosure (RE) differential pressure-low isolation actuation instrumentation logic had been bypassed
- without the' associated TS action being performed within.the required time-period.
Upon identifying this condition, the RE isolation logic was immediately restored.
An inadvertent isolation of the:RE secondary containment and initiation of the Standby Gas-Treatment. System (SGTS)(EIIStBH).and Reactor Enclosure Recirculation System (RERS)(EIIS:AD)., both Engineered
. Safety Features (ESFs), occurred due to the actuation of the low j
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differential-pressure isolation looic.
At 1701 hours0.0197 days <br />0.473 hours <br />0.00281 weeks <br />6.472305e-4 months <br /> on January 8, 1990, the normal Unit 2 RE.
ventilation system was being placed in-service and the
'B' train cof SGTS zwao'being removed from operation after the completion of
' scheduled maintenance on 'B' -RE exhaust fan.
At this time, the Unit:2RE low differential pressure isolation switches'were placed-to ' Reset' to bypass the RE ventilation isolation ~ signal-
- - and support restoration of the normal RE-ventilation in accordance with system procedure S76.1.B, "Startup'of Reactor Enclosure HVAC."
With the. switches in ' Reset', bothithe CO and SSV recognized entry into the two hour TS; action statement.
The
'2A' and '2C'JRE ventilation Supply and' Exhaust fans were placed into operation.
These fans were having difficulty maintaining
~-
adequate RE differential pressure due to known. equipment. problems and therefore the SSV' delayed restoring the ' Reset' switches to prevent inadvertent isolation of RE until the problem of differential pressure oscillations could be evaluated.
The
_ System Engineer for this system adjusted the RE fans such that the differential pressure was stabilized at the negative 0.25 inch waterzgauge by approximately 1845 hours0.0214 days <br />0.513 hours <br />0.00305 weeks <br />7.020225e-4 months <br />.
At 1914 hours0.0222 days <br />0.532 hours <br />0.00316 weeks <br />7.28277e-4 months <br />, the Main Control Room (MCR) SSV realized that the ' Reset' switches had not been returned to the ' Auto' position within the two hour time limit required by TS and immediately directed that the switches be placed to ' Auto' at 1915 hours0.0222 days <br />0.532 hours <br />0.00317 weeks <br />7.286575e-4 months <br />.
Thus, the RE low differential pressure isolation capability was bypassed for y,7a.v.
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Limerick Generating Station, Unit 2 015 l0 l0 lu l3 l 5l 3 9l0 0 l0 l1 O jo 0 13 0F 0l6 reara -.= ::.... : =c,
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approximately 14 minutes in excess of the TS action time limit without completing the action (i.e. SGTS in operation), thereby vio.lating TS LCO 3.3.2.
At 1915 hours0.0222 days <br />0.532 hours <br />0.00317 weeks <br />7.286575e-4 months <br />, when the RE isolation reset switches (HS-76-279A and HS-76-279B) were returned to ' Auto', a RE isolation occurred
- - due-to a RE low differential pressure isolation logic trip.
Subsequent investigation into the cause of the isolation revealed that the local ' Auto / Test' switches (HS-76-298A-5 and HS-76-298B-
- 5) were left in the ' Test' position rather than the ' Auto' o
l position during shutdown of the normal RE ventilation on a previous shift.
The combination of the MCR switches placed in
' Auto' and the local switches in the ' Test' position generated an isolation signal, causing the RE isolation.
Both the
'A' and
'B' trains of SGTS and the A' train of RERS started and operated as designed.
The isolation was reset and normal ventilation was l
restored at 0130 hours0.0015 days <br />0.0361 hours <br />2.149471e-4 weeks <br />4.9465e-5 months <br /> on January 9, 1990.
The RE Secondary L
Containment remained isolated with the SGTS in operation for 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and 15 minutes.
A'four hour notification to the NRC was made on January 8, 1990 l
in accordance with the requirements of 10 CFR 50.72(b)(2)(ii)
[
since this event resulted in the automatic actuation of an ESP.
f Accordingly, this report is being submitted in accordance with the requirements of 10 CFR 50.73(a)(2)(iv).
In addition, this report is being submitted in accordance with the. requirements of 10 CFR 50.73 (a)(2)(1)(B) since the action statement'for TS section 3.3.2 had not been met within the required time period.
1 Consequences of the Event:
The consequences of the RE isolation event were minimal in that, l
both the
'A' and
'B' trains of SGTS and the
'A' train of RERS l
initiated as designed to maintain the RE secondary containment
. differential pressure while the normal RE ventilation system had been isolated.
The redundant
'B' train of RERS was available for operation had the
'A' train failed to properly function.
All-systems responded as designed.
There was no release of radioactive material to the environment as a result of this event.
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During the 14 minutes that the TS action was exceeded, a RE low differential pressure condition did not exist.
Had an accident condition occurred, operators would have been alerted via annu'nciation in the MCR and would have responded accordingly.
Had an accident condition occurred, which' generated a RE
~-
isolation signal other than low differential pressure, SGTS and RERS would have initiated to perform their intended safety function.
Cause of the Event
+
The violation of TS Section 3.3.2 resulted from a personnel error by a licensed MCR operator.
Due to the distractions caused by the' differential pressure oscillations in the RE ventilation system, the MCR.SSV failed to adequately track and direct the return of the switches from ' Reset' to ' Auto' within the two hour TS required time period.
The cause of the second event (unexpected isolation of the. Unit 2 g
RE ventilation system when the RE Isolation ' Reset' switches were returned to ' Auto') was due to insufficient communication between the Chief Operator (CO)-and SSV.
The CO failed to provide all pertinent information to the SSV when gaining clarification on which position to leave the local Test. switches following the shutdown of RE ventilation for maintenance.
The switches were originally placed in the ' Test' position during the removal of L
the Unit 2 RE ventilation system from service to support l
maintenance activities at 0443 hours0.00513 days <br />0.123 hours <br />7.324735e-4 weeks <br />1.685615e-4 months <br /> on January 8, 1990.
The RE l
ventilation was isolated in accordance with procedure S76.8.B, i
" Manual' Initiation of Reactor Enclosure or Refueling Floor Secondary Containment Isolation" which stated to " Momentarily place switches to test".
The plant operator who was. performing this function requested clarification from the CO on the meaning of this statement.
The CO asked the SSV about the position of the switches without conveying all pertinent information.
The SSV, utilizing his system knowledge, determined that the switches should be left in the test position.
He failed to review the guidance available in procedure S76.8.B.
Had he reviewed the procedural guidance available, his attention would have been directed towards the word " momentarily".
He may have then questioned how long " momentarily" was, but he would have realized that the switches were not to remain in the ' Test' position for the entire duration of the isolation.
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- - cause to this event can be attributed to the use of non-standard terminology in procedure S76.8.B.
The word " momentarily" in,
" momentarily placing switches to Test", does not provide explicit direction to the plant operator performing the actions of the procedure.
l
Corrective Actions
L p
Proper isolation of the RE ventilation system and proper initiation of SGTS and RERS were-verified.
The RE remained isolated until 0130 hours0.0015 days <br />0.0361 hours <br />2.149471e-4 weeks <br />4.9465e-5 months <br /> on January 9, 1990, at which time the remainder of the RE ventilation system maintenance had-been completed and normal ventilation was restored.
i
~ Actions Taken to Prevent Recurrence:
i t.
The SSV, who directed restoration of the ' Reset' switches, was counseled on the importance of properly prioritizing and i
addressing all concerns (i.e. TS time limitations).
In addition, I.
the CO was counseled on the importance of proper communication and the need for transferring accurate and complete information when requesting guidance from the SSV.
The SSV (involved in
- - positioning the local ' Test' switches) was counseled on the importance of considering all factors and the available resources i'
when making his decisions.
A shift training bulletin will be issued to all-MCR operators to describe the details'of this event and to emphasize importance of properly tracking TS prescribed time limits for inoperability. --This event 'will be further addressed in an upcoming Licensed Operator Requalification training.
Furthermore, procedure S76.8.B has been revised to include an additional step to direct the restoration of the switches from
. the ' Test' position to their original position after a specified time period (i.e. following the SGTS fan start).
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- - Limerick Generating Station, Unit 2 0 l5 lo lo lo l3l 5l 3 9l0 0l0l1 0 l0 0 16 0F Ol6 itxt,,
- - aw,- aur,,nn Previous Similar Occurrences:
Other RE Secondary Containment isolation events have been reported; however, only ond event was due to a similar cause.
~
Limerick LER l-86-002, reported RE secondary containment isolation due to a handswitch left in the ' Auto' position.
Because the switches in LER l-86-002 were located in the MCR and the switches in this LER are local switches and are operated by different people, the actions to prevent recurrence in LER l 002 would not have been expected to prevent this event.
Tracking Codes:
A07 Failure to properly communicate.
A08 Failure to properly observe changing cond.
A02 Failure to follow implementing procedures.
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| | | Reporting criterion |
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| 05000353/LER-1990-001, :on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent Info |
- on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent Info
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-001-01, :on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program Revised |
- on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-002-01, :on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures Adequate |
- on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures Adequate
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000353/LER-1990-002, :on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer Restored |
- on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer Restored
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-003, :on 900208,HPCI Sys Inboard Isolation Valve Isolated During Isolation Logic Surveillance Test.Caused by Mfg Error.Program for Replacement/Rework of Trip Units Being Implemented.Estimated Completion Date Dec 1993 |
- on 900208,HPCI Sys Inboard Isolation Valve Isolated During Isolation Logic Surveillance Test.Caused by Mfg Error.Program for Replacement/Rework of Trip Units Being Implemented.Estimated Completion Date Dec 1993
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-003-01, :on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation Reset |
- on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation Reset
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-003, :on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time Reset |
- on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-004, :on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure Revised |
- on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure Revised
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-005, :on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program Improved |
- on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program Improved
| 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-006-01, :on 900312,automatic Actuation of HPCI Sys & Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Spurious Low Reactor Water Level Signal. Event Discussed at I&C Group Meeting |
- on 900312,automatic Actuation of HPCI Sys & Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Spurious Low Reactor Water Level Signal. Event Discussed at I&C Group Meeting
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-006, :on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All Counties |
- on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All Counties
| | | 05000352/LER-1990-007, :on 900222,high Radiation Reactor Protection Sys Actuation & Isolation Setpoints Set Outside Required Limits.Caused by Personnel Error by Nonlicensed Employee. Setpoints Adjusted & Personnel Counseled |
- on 900222,high Radiation Reactor Protection Sys Actuation & Isolation Setpoints Set Outside Required Limits.Caused by Personnel Error by Nonlicensed Employee. Setpoints Adjusted & Personnel Counseled
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-007-01, :on 900330,actuations of Primary Containment & Reactor Vessel Isolation Control Sys ESF Occurred.Caused by Gross Failure of Inverter Inductor.Inverter Bypassed,Shunt Trip Breaker Closed & Isolations Reset |
- on 900330,actuations of Primary Containment & Reactor Vessel Isolation Control Sys ESF Occurred.Caused by Gross Failure of Inverter Inductor.Inverter Bypassed,Shunt Trip Breaker Closed & Isolations Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-008-01, :on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to Mfg |
- on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to Mfg
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-009, :on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector Replaced |
- on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-010, :on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of Cause |
- on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of Cause
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-011, :on 900713,reactor Encl Secondary Containment Isolation or Low Differential Pressure Occurred.Caused by Severed Instrument Air Line.Instrument Air Line Repaired on 900713 |
- on 900713,reactor Encl Secondary Containment Isolation or Low Differential Pressure Occurred.Caused by Severed Instrument Air Line.Instrument Air Line Repaired on 900713
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-011, :on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm Repositioned |
- on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm Repositioned
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-011-02, :on 900713,positive Differential Pressure Condition Between Reactor Encl Secondary Containment & Outside Atmosphere Occurred,Resulting in Blowout Panel Actuation.Caused by Severed Air Supply Line |
- on 900713,positive Differential Pressure Condition Between Reactor Encl Secondary Containment & Outside Atmosphere Occurred,Resulting in Blowout Panel Actuation.Caused by Severed Air Supply Line
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-012-02, :on 900715,reactor Scram Occurred Due to Main Turbine Trip on Low Main Condenser Vacuum Due to Failed Pipe.Caused by Insufficient Pipe Support Resulting in Vibration Induced Metal Fatigue.Pipe Replaced |
- on 900715,reactor Scram Occurred Due to Main Turbine Trip on Low Main Condenser Vacuum Due to Failed Pipe.Caused by Insufficient Pipe Support Resulting in Vibration Induced Metal Fatigue.Pipe Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-012, :on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable Sleeved |
- on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable Sleeved
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-013-02, :on 900831,RCIC Sys Isolation Occurred.Caused by Personnel Error Resulting in Procedural Noncompliance. Procedural Compliance & Higher Attention to Detail Reinforced to Personnel |
- on 900831,RCIC Sys Isolation Occurred.Caused by Personnel Error Resulting in Procedural Noncompliance. Procedural Compliance & Higher Attention to Detail Reinforced to Personnel
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-013, :on 900611,review of Dc Electrical Distribution Sys Identified That Divs 1 & 2 Had Inadequate Isolation Capability Between Class 1E & non-Class 1E Components & Also Had under-rated Dc Fuses |
- on 900611,review of Dc Electrical Distribution Sys Identified That Divs 1 & 2 Had Inadequate Isolation Capability Between Class 1E & non-Class 1E Components & Also Had under-rated Dc Fuses
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-013-01, :on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626 |
- on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626
| 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-014-02, :on 900906,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Lack of Attention to Detail Resulting in Procedural Noncompliance.Personnel Counseled |
- on 900906,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Lack of Attention to Detail Resulting in Procedural Noncompliance.Personnel Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-014-01, :on 900705,group III Primary Containment & Reactor Vessel Isolation Control Sys Isolation Signal Occurred,Initiating RWCU Sys Isolation.Causes Included High Outside Air Temp.Normal Ventilation Restored |
- on 900705,group III Primary Containment & Reactor Vessel Isolation Control Sys Isolation Signal Occurred,Initiating RWCU Sys Isolation.Causes Included High Outside Air Temp.Normal Ventilation Restored
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-015-01, :on 900813,RWCU Sys Isolation Occurred. Isolation Resulted from High Regenerative HX Room Temp. Caused by Leaking Sys Vent Valves.Leaking Valves Replaced |
- on 900813,RWCU Sys Isolation Occurred. Isolation Resulted from High Regenerative HX Room Temp. Caused by Leaking Sys Vent Valves.Leaking Valves Replaced
| | | 05000353/LER-1990-015-02, :on 900910,reactor Scram Occurred Due to Spurious Trip Signal from Steam Leak Detection Sys Temp Switch.Caused by Equipment Failure.Temp Switch TTS-25-216D Was Replaced |
- on 900910,reactor Scram Occurred Due to Spurious Trip Signal from Steam Leak Detection Sys Temp Switch.Caused by Equipment Failure.Temp Switch TTS-25-216D Was Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-016-01, :on 900811,Tech Spec 3.7.6.4 Not Met Since Halon Sys Inoperable |
- on 900811,Tech Spec 3.7.6.4 Not Met Since Halon Sys Inoperable
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-016-01, :on 900815,Tech Spec Limiting Condition for Operation Action Not Implemented within Required Time Period Due to Firewatch Employee Failure to Perform Surveillance Procedure.Caused by Personnel Falsifying Tests |
- on 900815,Tech Spec Limiting Condition for Operation Action Not Implemented within Required Time Period Due to Firewatch Employee Failure to Perform Surveillance Procedure.Caused by Personnel Falsifying Tests
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000353/LER-1990-016-02, :on 900811,failure to Meet Tech Spec 3.7.6.4 Since Halon Sys Inoperable & Tech Spec Action Not Taken in Appropriate Time Period |
- on 900811,failure to Meet Tech Spec 3.7.6.4 Since Halon Sys Inoperable & Tech Spec Action Not Taken in Appropriate Time Period
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(8) | | 05000353/LER-1990-017-02, :on 900916,inadvertent Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred |
- on 900916,inadvertent Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-017-01, :on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse Replaced |
- on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-018-02, :on 901030,north Stack Wide Range Monitor Exceeded 7-day Limit for Inoperability of Tech Spec 3.3.7.5 |
- on 901030,north Stack Wide Range Monitor Exceeded 7-day Limit for Inoperability of Tech Spec 3.3.7.5
| | | 05000352/LER-1990-018-01, :on 900830,common Plant Water & Steam Barriers in Degraded Condition & Unit Placed in Unanalyzed Condition. Detailed Cause Analysis Will Be Provided.Task Force Established |
- on 900830,common Plant Water & Steam Barriers in Degraded Condition & Unit Placed in Unanalyzed Condition. Detailed Cause Analysis Will Be Provided.Task Force Established
| 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000353/LER-1990-019-02, :on 901101,half-scram & Isolations Resulted from Loss of Power to Rps/Uninterruptible Supply Panel Due to Inverter Damage |
- on 901101,half-scram & Isolations Resulted from Loss of Power to Rps/Uninterruptible Supply Panel Due to Inverter Damage
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-019-01, :on 901101,various Actuations of Primary Containment & Reactor Vessel Isolation Control Sys,Esf & Channel B RPS half-scram Occurred.Caused by Damaged Connector in Inverter Circuitry |
- on 901101,various Actuations of Primary Containment & Reactor Vessel Isolation Control Sys,Esf & Channel B RPS half-scram Occurred.Caused by Damaged Connector in Inverter Circuitry
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-019-01, :on 900915,special Rept for Diesel Generator Surviellance Test Failure |
- on 900915,special Rept for Diesel Generator Surviellance Test Failure
| | | 05000352/LER-1990-019-02, :on 900915,diesel Generator Surveillance Test Failure Reported.Diagnostic Testing Inconclusive on Cause & No Subsequent Failure Noted.No Addl Corrective Actions Planned |
- on 900915,diesel Generator Surveillance Test Failure Reported.Diagnostic Testing Inconclusive on Cause & No Subsequent Failure Noted.No Addl Corrective Actions Planned
| | | 05000352/LER-1990-020-01, :on 900918,personnel Manually Initiated Main Control Room Ventilation Sys Chlorine Isolation Due to High Toxic Chemical Concentration Signal |
- on 900918,personnel Manually Initiated Main Control Room Ventilation Sys Chlorine Isolation Due to High Toxic Chemical Concentration Signal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000353/LER-1990-020-02, :on 901119,primary Containment post-LOCA Radiation Monitoring Sys Declared Inoperable Due to Deficient Circuit Board in Three of Four Channels.Caused by Inadequate Design Review.Replacement Installed |
- on 901119,primary Containment post-LOCA Radiation Monitoring Sys Declared Inoperable Due to Deficient Circuit Board in Three of Four Channels.Caused by Inadequate Design Review.Replacement Installed
| 10 CFR 50.73(a)(2)(1) | | 05000353/LER-1990-021-02, :on 901206,emergency Diesel Generator D21 Output Breaker Tripped on Reverse Power & Declared Inoperable.Caused by Closure of Cross Current Control Relay Contacts.Relay Replaced |
- on 901206,emergency Diesel Generator D21 Output Breaker Tripped on Reverse Power & Declared Inoperable.Caused by Closure of Cross Current Control Relay Contacts.Relay Replaced
| | | 05000352/LER-1990-021-01, :on 900911,seismic Monitoring Sys Declared Inoperable in Preparation for Performance of Surveillance Test Procedure |
- on 900911,seismic Monitoring Sys Declared Inoperable in Preparation for Performance of Surveillance Test Procedure
| | | 05000352/LER-1990-022-01, :on 901003,emergency Diesel Generator Sys Start Failed |
- on 901003,emergency Diesel Generator Sys Start Failed
| | | 05000352/LER-1990-023-01, :on 901015,emergency DGs Discovered to Be Inoperable on Various Occasions,Resulting in Condition Prohibited by Tss.Caused by Inadequate Testing of Redundant Rectifier Banks for Emergency DGs |
- on 901015,emergency DGs Discovered to Be Inoperable on Various Occasions,Resulting in Condition Prohibited by Tss.Caused by Inadequate Testing of Redundant Rectifier Banks for Emergency DGs
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-024-01, :on 901025,RCIC Sys Inoperable Due to Physical Separation Deficiency Between Class 1E & Non-Class 1E Cables Due to Personnel Error |
- on 901025,RCIC Sys Inoperable Due to Physical Separation Deficiency Between Class 1E & Non-Class 1E Cables Due to Personnel Error
| 10 CFR 50.73(a)(2)(1) | | 05000352/LER-1990-025-01, :on 901110,spurious LOCA Signal Resulted in ESF Actuations |
- on 901110,spurious LOCA Signal Resulted in ESF Actuations
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-026-01, :on 901118,full Reactor Scram Signal Generated on High Reactor Pressure Vessel Pressure of 1,033 Psig. Caused by Personnel Error.Operator Counseled & Event Will Be Included in Operator Training |
- on 901118,full Reactor Scram Signal Generated on High Reactor Pressure Vessel Pressure of 1,033 Psig. Caused by Personnel Error.Operator Counseled & Event Will Be Included in Operator Training
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-027-01, :on 901120,reactor Scram Signal Occurred When Intermediate Range Monitor F Spiked Upscale Causing RPS Channel B Half Scram.Caused by Equipment Problem Coincident W/Performance of RPS Surveillance Procedure |
- on 901120,reactor Scram Signal Occurred When Intermediate Range Monitor F Spiked Upscale Causing RPS Channel B Half Scram.Caused by Equipment Problem Coincident W/Performance of RPS Surveillance Procedure
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000352/LER-1990-028-01, :on 901126,instrumentation & Controls Personnel Discovered That Facility Tech Specs Required Surveillance Requirements Not Met for Two Intermediate Range Monitors.W/ |
- on 901126,instrumentation & Controls Personnel Discovered That Facility Tech Specs Required Surveillance Requirements Not Met for Two Intermediate Range Monitors.W/
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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