05000327/FIN-2009005-02
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Finding | |
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Title | Reactor Trip due to Inadequate Transformer Bus Duct Maintenance Procedure |
Description | A self-revealing finding was identified for an inadequate maintenance procedure which was used to perform a periodic maintenance activity to clean and inspect the bus duct associated with the D common station service transformer (CSST). This resulted in the bus duct being left in a condition that allowed for water intrusion to occur, which led to a fault that caused a loss of one offsite power supply and an automatic reactor trip of both units with main feedwater unavailability. The licensee entered this issue into the corrective action program (CAP) as PER 166884. The finding was determined to be greater than minor because it was associated with the procedure quality attribute of the initiating events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions. Specifically, the use of an inadequate procedure directly contributed to the loss of one offsite power supply and an automatic reactor trip of both units with main feedwater unavailability. Using Inspection IMC 0609, Significance Determination Process, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, the finding was determined to be applicable to a Phase 2 analysis since the finding contributed to both the likelihood of a reactor trip and the likelihood that mitigating systems will not be available. Using IMC 0609 Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations, a Phase 2 analysis was performed using the site specific risk-informed inspection notebook. The finding was assumed to affect the initiating event likelihood (IEL) of a Transient With Loss of Power Conversion System (TPCS), since power availability to the unit boards affects reactor coolant pump function as well as main condenser availability. A regional Senior Reactor Analyst performed a Phase 3 Significance Determination Process evaluation. The evaluation concluded the finding was of very low safety significance (Green) based on an assumed unavailability of the CSST B fast transfer function of 0.11/yr. No cross-cutting aspect was identified since the issue was not reflective of current licensee performance, in that the inadequate maintenance procedure was implemented in December 2006 |
Site: | Sequoyah ![]() |
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Report | IR 05000327/2009005 Section 4OA3 |
Date counted | Dec 31, 2009 (2009Q4) |
Type: | Finding: Green |
cornerstone | Initiating Events |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | E Michel H Gepford E Guthrie L Miller D Simpkins C Young M Speck B Collins W Deschaine |
INPO aspect | |
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Finding - Sequoyah - IR 05000327/2009005 | |||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Sequoyah) @ 2009Q4
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