05000324/LER-1979-068-03, /03X-1:on 790910,downscale Alarm for Average Power Range Monitor F Actuated at Less than Required Percentage. Caused by Monitor Instrument Drift.Monitor Will Be Replaced

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/03X-1:on 790910,downscale Alarm for Average Power Range Monitor F Actuated at Less than Required Percentage. Caused by Monitor Instrument Drift.Monitor Will Be Replaced
ML19254E850
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 10/30/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19254E847 List:
References
LER-79-068-03X, LER-79-68-3X, NUDOCS 7911020401
Download: ML19254E850 (1)


LER-1979-068, /03X-1:on 790910,downscale Alarm for Average Power Range Monitor F Actuated at Less than Required Percentage. Caused by Monitor Instrument Drift.Monitor Will Be Replaced
Event date:
Report date:
3241979068R03 - NRC Website

text

NRc FORM 366 LA R COMMI I (7 7J)

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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h

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While performing PT 1.2.4. APRM High Fluv and Downsenle Teme. the dnuneenle ntnr, fnr O

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