05000306/LER-1917-001, Regarding 23 Containment Fan Coil Unit Operability

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Regarding 23 Containment Fan Coil Unit Operability
ML17334A040
Person / Time
Site: Prairie Island Xcel Energy icon.png
Issue date: 11/29/2017
From: Northard S
Northern States Power Company, Minnesota, Xcel Energy
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
L-PI-17-048 LER 17-001-00
Download: ML17334A040 (5)


LER-1917-001, Regarding 23 Containment Fan Coil Unit Operability
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(i)
3061917001R00 - NRC Website

text

1717 Wakonade Drive Welch, MN 55089 800.895.4999 xcelenergy.com NOV 2 9 2017 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-001 Prairie Island Nuclear Generating Plant Unit 2 Docket 50-306 Renewed License No. DPR-60 Xcel Energy RESPONSIBLE BY NATUR L-PI-17-048 10 CFR 50.73 Licensee Event Report 50-306/2017-001-00, 23 Containment Fan Coil Unit Operability Northern States Power Company, a Minnesota corporation, doing business as Xcel Energy (hereafter "NSPM"), encloses Licensee Event Report (LER) 50-306/2017-001-00, 23 Containment Fan Coil Unit Operability.

Summary of Commitments This letter contains no new commitments and no revisions to existing commitments.

L!i ~D

~Oll!(vif'llc\\_

Scott Northard Site Vice President, Prairie Island Nuclear Generating Plant Northern States Power Company-Minnesota

Enclosure:

cc:

Regional Administrator, Region Ill, USNRC Project Manager, Prairie Island Nuclear Generating Plant, USNRC Resident Inspector, Prairie Island Nuclear Generating Plant, USNRC State of Minnesota

Document Control Desk Page 2 ENCLOSURE 1 Licensee Event Report 50-306/2017-001-00 3 Pages Follow

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 03/31/2020 (04-2017) ht!Q :1/wwvv. nrc.g ov/reading-rm/doc-collections/nuregs/staff/sr1 022/r3[J the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

13. PAGE Prairie Island Nuclear Generating Plant Unit 2 05000 306 1 OF3
4. TITLE 23 Containment Fan Coil Unit Operability
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED SEQUENTIAL FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR REV MONTH DAY YEAR NUMBER NO.

05000 5

2 2016 2017

- 001
- 00 11 29 2017 FACILITY NAME DOCKET NUMBER 05000
9. OPERAllNG MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §:(Check all that apply)

Unit 1 Mode 1 D 20.2201(b)

D 20.2203(a)(3)(i) 0 50.73(a)(2)(ii)(A)

D 50.73(a)(2)(viii)(A)

Unit 2 Mode 1 D 20.2201(d)

D 20.2203(a)(3)(ii)

D 50.73(a)(2)(ii)(B)

D 50.73(a)(2)(viii)(B)

D 20.2203(a)(1)

D 20.2203(a)(4)

D 50. 73(a)(2)(iii)

D 50.73(a)(2)(ix)(A)

D 20.2203(a)(2)(i)

D 50.36(c)(1)(i)(A)

D 50.73(a)(2)(iv)(A)

D 50.73(a)(2)(x)

10. POWER l,.EVEL D 20.2203(a)(2)(ii) 0 50.36(c)(1 )(ii)(A)

D 50.73(a)(2)(v)(A)

D 73.71(a)(4)

D 20.2203(a)(2)(iii)

D 50.36(c)(2)

D 50.73(a)(2)(v)(B)

D 73.71 (a)(5)

Unit 1 100%

D 20.2203(a)(2)(iv)

D 50.46(a)(3)(ii)

D 50.73(a)(2)(v)(C)

D 73.77(a)(1)

Unit2 100%

D 20.2203(a)(2)(v) 0 50.73(a)(2)(i)(A)

D 50.73(a)(2)(v)(D)

D 73.77(a)(2)(i)

D 20.2203(a)(2)(vi)

['8] 50.73(a)(2)(i)(B)

D 50.73(a)(2)(vii)

D 73.77(a)(2)(ii) 0 50.73(a)(2)(i)(C) 00THER Specify in Abstract below or in Logs using the Open Item option.

This action is complete

4. Revise site work instruction 5AWI 3.15.8, SAFETY FUNCTION DETERMINATION PROGRAM to be more user friendly.

Including graphical explanations. This action is expected to be completed by the end of the year.

PREVIOUS SIMILAR EVENTS

A review of the Corrective Action Program (CAP) and Licensee Event Reports (LERs) for PINGP revealed one similar event over the last three years.

LER 50-282/2015-005-01, Condition Prohibited by Technical Specification (ADAMS Accession Number ML16285A387).

On September 11, 2015, it was identified that 122 Control Room Chiller was removed from service and control valve CV-31837 (121/122 Control Room Chiller Outlet) and CV-31838 (121/122 Control Room Chiller Inlet) were closed. This isolated Train B Safeguards Chilled Water and rendered Bus 16 Unit Cooler non-functional, which will result in unacceptable temperatures in the associated bus room during a postulated High Energy Line Break (HELB). Bus 16 would not have performed its safety function and was inoperable for greater than the time allowed by Tech Specs. Tech Specs 3.8.9 for Distribution Systems-Operating was not entered and the required actions were not taken to restore to an operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or to enter MODE 3 in 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and MODE 5 in 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. This is a reportable event under 10 CFR 50.73(a)(2)(i)(b), Operation or Condition Prohibited by Tech Specs. Page 3 of 3