LER-1979-013, /03L-1:on 790530,reactor Core Isolation Cooling Sys Tripped on Overspeed During Flow Test.Caused by Improper Assembly Which Allowed Turbine Wheel Nut to Loosen,Causing Axial Loading of Bearings |
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| 2601979013R03 - NRC Website |
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( With reactor at rated temperature and pressure,.the RCIC tripped on overspeed during ~
~oz I flow 7:est.
> Coring tha investigation, there was a loss of sPeed signal in the control ezc~
the public.
Previous occurrences
BFRO 50-296/7832, BFRO 50-259/7615
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Technical i Specification 3.5.F was involved.
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CODE TYPE NQ.
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~1 2'I 22 23 24 20 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUT DO)VN ATTACHh'IFtiT NPRDP PRIME CohiP, CQAIPONfjnjl1 TAKEtl ACTIOtt ON PLANT METHOD
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In> ro er initial assenbl allowed tnrbine wheal nut to loosen des~tr JdZE tgjERTs~nd A causin axial loadin of bearin s.
Bearin wear allowed shaft to gt~~p~~p causing speed control malfunction, thus throttle valve remained open.
Wheel nut,bear~
- ings, and actuator replaced.
Woodward Governor, SN 968510.
Terry Turbine, Model A825~0 Type GS-l.
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I'or'm I3F-17 BF I,").2 1/l0/79 LI!R SUPPLEMENTAL INFORMATION BFRO-.'>0-260 /
7913 Technical Specificatior. Involved Reported Under Technical Specification T.
S. 6.7.2.b.2 Date of Occurrence 5/'30/79 Time of Occurrence Unit Ederrrification and E)escr~ition of Ocrurr'ence:
RCIC would trip on overspeed when flow test was attempted.
Speed indicati'on was lost in control room during investigation.
(.rir><lition'rior'o O rcurr i rr< c Unit was at 1% power with rated temperature and pressure after refueling outage.
Action specified in the Technical Specific~sticn Surveillance Requirements met duo t~oino orebie eceu~imonc.
Describe.
HPCI operability SI's run.
~Ay)ar'ent Cause
<if Occurr'ence:
Initial malfunction of EG-R actuator caused throttle valve to remain open when RCIC was run resulting in an overspeed trip. During opera-bility tests 'to return RCIC to service, unusual bearing wear allowed shaft to strike magnetic pick-up and caused loss of speed indication.
Bearing wear may have caused initial malfunction of the EG-R. Cracks in bearings were found during disassembly.
The apparent cause of bearing failure was improper initial assembly allowing a turbine (OVER)
An:i~isis of Occrrrr e>>ce:
There was no damage to plant equipment, no activity released, no personnel exposure or injury, no hazard to health or safety of the public.
Cor r'ective Action:
Actuator and bearings replaced; ball and tappet overspeed trip mechanism was replaced; wheel nut was replaced and staked.
The bearings of other units will be inspected during next refueling outage.
I:ailure Data:
Previous occurrences
BFRO 50-296/7832, BFRO 50-259/7615.
":lletention:
eriod - Lifetune; Responsibility -,Administrative Supervisor
'Se) s t
A arent Cause of Occurrence (Continued) wheel nut to unthread destroying its threads and causing axial loading cracking the bearings.
During bearing replacement, it was discovered that mechanical overspeed trip reset mechanism needed ad)ustment.
The ball and tappet trip mechanism was also inspected and the ball was found binding in its socket.
A arent Cause of Occurrence (Continued) wheel nut to unthread destroying its threads and causing axial loading cracking the bearings.
During bearing replacement, it was discovered that mechanical overspeed trip reset mechanism needed ad)ustment.
The ball and tappet trip mechanism was also inspected and the ball was found binding in its socket.
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| 05000296/LER-1979-001-03, /03L-0 on 790111:switch on LIS-3-56B Failed to Trip Reactor Recirculation Pump Motor Generator.Caused by Misadjusted Switch on Yarway Model 4418CE.Switch Recalibr & Tested Satisfactorily | /03L-0 on 790111:switch on LIS-3-56B Failed to Trip Reactor Recirculation Pump Motor Generator.Caused by Misadjusted Switch on Yarway Model 4418CE.Switch Recalibr & Tested Satisfactorily | | | 05000296/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000259/LER-1979-001, Forwards LER 79-001/01T-0 | Forwards LER 79-001/01T-0 | | | 05000259/LER-1979-001-01, /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod | /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod | | | 05000260/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000260/LER-1979-001-03, /03L-0 on 790113:during Test of high-pressure Injection Coolant Sys,Steam Supply Valve FCV-73-16 Failed to Open,Rendering Sys Inoperative.Caused by Failure of Limitorque Valve Operator Limit Switch | /03L-0 on 790113:during Test of high-pressure Injection Coolant Sys,Steam Supply Valve FCV-73-16 Failed to Open,Rendering Sys Inoperative.Caused by Failure of Limitorque Valve Operator Limit Switch | | | 05000296/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000259/LER-1979-002-03, /03L-0 on 790129:during Normal Operation While Performing Surveillance Test,Standby Liquid Control Pump 1B Relief Valve Opened Below Tech Spec Min.Caused by Valve Seat Surface Deterioration | /03L-0 on 790129:during Normal Operation While Performing Surveillance Test,Standby Liquid Control Pump 1B Relief Valve Opened Below Tech Spec Min.Caused by Valve Seat Surface Deterioration | | | 05000259/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000260/LER-1979-002-03, /03L-0 on 790203:alarm for Fire Protection Panel 25-236 Annunciated in Control Room.Panel Was Not Alarmed Condition.Caused by Normal End of Life Electrical Failure of Annunciator Point Card.Card Replaced & Sys Normalized | /03L-0 on 790203:alarm for Fire Protection Panel 25-236 Annunciated in Control Room.Panel Was Not Alarmed Condition.Caused by Normal End of Life Electrical Failure of Annunciator Point Card.Card Replaced & Sys Normalized | | | 05000260/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000296/LER-1979-002-03, /03L-0 on 790117:during Maintenance of Reset Switch,Short Circuit Damaged Power Supply & Sensor Circuit Board,Rendering Fixed Spray Automatic Initiation Circuit for Fire Protection Inoperable | /03L-0 on 790117:during Maintenance of Reset Switch,Short Circuit Damaged Power Supply & Sensor Circuit Board,Rendering Fixed Spray Automatic Initiation Circuit for Fire Protection Inoperable | | | 05000296/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000259/LER-1979-003-01, /01T-1 on 790120:during Cold Shutdown,Local Leak Rate Test Indicated Excessive Total Leakage.Caused by Leaking Valve Seating Surface in Eight Valves.Valves Repaired & Retested | /01T-1 on 790120:during Cold Shutdown,Local Leak Rate Test Indicated Excessive Total Leakage.Caused by Leaking Valve Seating Surface in Eight Valves.Valves Repaired & Retested | | | 05000259/LER-1979-003, Forwards LER 79-003/01T-1 | Forwards LER 79-003/01T-1 | | | 05000260/LER-1979-003-01, /01T-0 on 790214:rod Position Info Sys Power Supply Ps X-5 Failed,Causing Loss of Rod Position Indication in Bottom Half of Vertical Core Display.Caused by Failure of Cooling Fan in Trygon Model L5B6-70-OVS4989 | /01T-0 on 790214:rod Position Info Sys Power Supply Ps X-5 Failed,Causing Loss of Rod Position Indication in Bottom Half of Vertical Core Display.Caused by Failure of Cooling Fan in Trygon Model L5B6-70-OVS4989 | | | 05000259/LER-1979-003-03, /03L-2 on 790120:during Cold Shutdown,Local Leak Rate Test Revealed Total Leakage Exceeded Allowable 60% La Per 24-h.Caused by Excessive Leakage of Valve Seating Surface.Eight Leaking Valves Were Repaired & Retested | /03L-2 on 790120:during Cold Shutdown,Local Leak Rate Test Revealed Total Leakage Exceeded Allowable 60% La Per 24-h.Caused by Excessive Leakage of Valve Seating Surface.Eight Leaking Valves Were Repaired & Retested | | | 05000296/LER-1979-003-03, /03L-0 on 790202:linear Heat Generation Rate Out of Tech Spec Limits.Caused by Operation Close to Limiting Values & Increase in Reactivity Due to Gadolina Burnup. Greater Margin to Limiting Value Will Be Maintained | /03L-0 on 790202:linear Heat Generation Rate Out of Tech Spec Limits.Caused by Operation Close to Limiting Values & Increase in Reactivity Due to Gadolina Burnup. Greater Margin to Limiting Value Will Be Maintained | | | 05000260/LER-1979-003, Forwards LER 79-003/01T-0 | Forwards LER 79-003/01T-0 | | | 05000260/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000259/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000259/LER-1979-004-03, /03L-0 on 790227:during Normal Operation,Review of Surveillance Test Data Indicated Monthly Samples of Diesel Fuel Taken in Dec 1978 Have Not Been Analyzed.Caused by Loss of Samples in Transit.Will Try to Measure Samples on | /03L-0 on 790227:during Normal Operation,Review of Surveillance Test Data Indicated Monthly Samples of Diesel Fuel Taken in Dec 1978 Have Not Been Analyzed.Caused by Loss of Samples in Transit.Will Try to Measure Samples on Site | | | 05000296/LER-1979-004-03, /03L-0 on 790411:during Normal Operation,Heat Detector Alarmed & Would Not Clear.Alarm Would Have Masked Signals from Other Detector,Required to Be Operational.Caused by Personnel Damaging Detector | /03L-0 on 790411:during Normal Operation,Heat Detector Alarmed & Would Not Clear.Alarm Would Have Masked Signals from Other Detector,Required to Be Operational.Caused by Personnel Damaging Detector | | | 05000260/LER-1979-004-03, /03L-0 on 790414:reactor Bldg,Turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Failed Surveillance Test SI 4.8.B-4.3,Section 4e.Caused by Failure of Input Card for Radiation Monitor | /03L-0 on 790414:reactor Bldg,Turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Failed Surveillance Test SI 4.8.B-4.3,Section 4e.Caused by Failure of Input Card for Radiation Monitor | | | 05000296/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000296/LER-1979-005, Updated LER 79-005/01T-2:on 790506,RHR Svc Water Supply to RHR HX 2B Isolated Standby Coolant Supply.Caused by Lack of Administrative Control Over Sys Cross Connect Valves. Controls Improved | Updated LER 79-005/01T-2:on 790506,RHR Svc Water Supply to RHR HX 2B Isolated Standby Coolant Supply.Caused by Lack of Administrative Control Over Sys Cross Connect Valves. Controls Improved | | | 05000296/LER-1979-005-01, /01T-1:on 790506,BHR Water Supply Isolation to 2B RHR Heat Exchanger Isolated Standby Coolant Supply to Unit 3.Caused by Lack of Administrative Control Over Sys Cross Connect Valves.Administrative Controls Have Been Improved | /01T-1:on 790506,BHR Water Supply Isolation to 2B RHR Heat Exchanger Isolated Standby Coolant Supply to Unit 3.Caused by Lack of Administrative Control Over Sys Cross Connect Valves.Administrative Controls Have Been Improved | | | 05000259/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000259/LER-1979-005-03, /03L-0 on 790225:reactor,turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Became Inoperable.Caused by Moisture Collection in Detector SC-2.-1.S.Detector Replaced & Moisture Removed | /03L-0 on 790225:reactor,turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Became Inoperable.Caused by Moisture Collection in Detector SC-2.-1.S.Detector Replaced & Moisture Removed | | | 05000260/LER-1979-005-03, /03L-0 on 790419:broken Terminal Discovered on Shutdown Board D Battery.Cause Unknown.Affected Cells Replaced & Personnel Instructed in Proper Tightening Methods | /03L-0 on 790419:broken Terminal Discovered on Shutdown Board D Battery.Cause Unknown.Affected Cells Replaced & Personnel Instructed in Proper Tightening Methods | | | 05000260/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000296/LER-1979-006-03, During Normal Operation, Erratic Indication of Torus Hydrogen Sensor Observed. Hydrogen Sensor Replaced & Tested Satisfactory.Design Change Request Initiated | During Normal Operation, Erratic Indication of Torus Hydrogen Sensor Observed. Hydrogen Sensor Replaced & Tested Satisfactory.Design Change Request Initiated | | | 05000296/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000260/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000259/LER-1979-006-03, /03L-0 on 790228:reactor,turbine Bldg & Refueling Zone Ventilation Exhaust Monitor RM-90-250 Became Inoperable for 3.5-h.Caused by Moisture in SC-2B Detector & Leaking Flanges.Moisture Removed & Flanges Tightened | /03L-0 on 790228:reactor,turbine Bldg & Refueling Zone Ventilation Exhaust Monitor RM-90-250 Became Inoperable for 3.5-h.Caused by Moisture in SC-2B Detector & Leaking Flanges.Moisture Removed & Flanges Tightened | | | 05000259/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000260/LER-1979-006-03, /03L-0 on 790427:prior to Refueling Shutdown, Drywell Prepurge Tritium Sample Not Taken.Caused by Lack of Understanding Between Operational & Lab Personnel.Operating Instructions Amended to Prevent Recurrence | /03L-0 on 790427:prior to Refueling Shutdown, Drywell Prepurge Tritium Sample Not Taken.Caused by Lack of Understanding Between Operational & Lab Personnel.Operating Instructions Amended to Prevent Recurrence | | | 05000260/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000296/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000296/LER-1979-007-03, /03L-0 on 790612:during Performance of Procedure SI 4.1.A-14,turbine First Stage Permissive Pressure Switches PS-1-81A & B & PS-1-91A & B Setpoints Exceeded Tech Specs. Caused by Setpoint Drift.Switches Recalibr | /03L-0 on 790612:during Performance of Procedure SI 4.1.A-14,turbine First Stage Permissive Pressure Switches PS-1-81A & B & PS-1-91A & B Setpoints Exceeded Tech Specs. Caused by Setpoint Drift.Switches Recalibr | | | 05000260/LER-1979-007-03, /03L-0 on 790503:during Refueling Outage,Five MSIVs Exceeded Leakage Limits.Caused by Irregularities on Valve Seating Surfaces & Entrapment of Debris Under Seating Surfaces.Valves Will Be Repaired & Retested | /03L-0 on 790503:during Refueling Outage,Five MSIVs Exceeded Leakage Limits.Caused by Irregularities on Valve Seating Surfaces & Entrapment of Debris Under Seating Surfaces.Valves Will Be Repaired & Retested | | | 05000260/LER-1979-008-01, /01T-0 on 790504:while Preparing for Refueling Outage,Secondary Containment Integrity Was Not Conclusively Demonstrated Prior to Breaking Primary Containment.Test Improperly Performed Due to Personnel Error | /01T-0 on 790504:while Preparing for Refueling Outage,Secondary Containment Integrity Was Not Conclusively Demonstrated Prior to Breaking Primary Containment.Test Improperly Performed Due to Personnel Error | | | 05000259/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000259/LER-1979-008-03, /03L-0 on 790612:during Normal Operation, Pressure Switches PS-1-81 a & B & PS-1-91 a & B Setpoints Exceeded Tech Specs by 3-15 Psig. Caused by Model B2T-A12SS Switches Drifting | /03L-0 on 790612:during Normal Operation, Pressure Switches PS-1-81 a & B & PS-1-91 a & B Setpoints Exceeded Tech Specs by 3-15 Psig. Caused by Model B2T-A12SS Switches Drifting | | | 05000296/LER-1979-008-03, /03L-0 on 790627:no Speed Indication Noted on Reactor Core Isolation Coolant.Caused by Broken Wires to Magnetic Pickup EG-M Box.Wires Repaired | /03L-0 on 790627:no Speed Indication Noted on Reactor Core Isolation Coolant.Caused by Broken Wires to Magnetic Pickup EG-M Box.Wires Repaired | | | 05000260/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000296/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000296/LER-1979-009-03, /03L-0 on 790717:hydrogen Ignition Damaged HEPA Filters.Caused by Improper Offgas Recombiner Preheater Operation.Sys HEPA Filters & Charcoal Bed Inspected.Three Filters Replaced.Procedures Will Be Revised | /03L-0 on 790717:hydrogen Ignition Damaged HEPA Filters.Caused by Improper Offgas Recombiner Preheater Operation.Sys HEPA Filters & Charcoal Bed Inspected.Three Filters Replaced.Procedures Will Be Revised | | | 05000260/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000296/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | |
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