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 Start dateReporting criterionEvent description
05000341/LER-2017-0053 November 201710 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident

At 1000 EDT on September 9, 2017, the Division 2 Mechanical Draft Cooling Tower (MDCT) fans were declared inoperable due to loss of output from the over speed fan brake inverter. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS) and the Emergency Equipment Cooling Water (EECW) system. The Division 2 EECW system cools the High Pressure Coolant Injection (HPCI) system room cooler. As a result, the non-functionality of the fan brakes lead to an unplanned HPCI inoperability.

Since HPCI is a single train system designed to mitigate the consequences of a loss of coolant accident (LOCA), this event could have prevented the fulfillment of a safety function. The cause of the event was the failure of the Division 2 fan brake inverter.

Corrective Actions were taken to replace the inverter and returning the MDCT fans, the UHS, EECW and HPCI to service on September 9, 2017 at 2351 EDT. A failure modes evaluation was performed by the vendor with no direct cause of the failed output determined. The fan brake system is only required for a design basis tornado and there was no credible tornado threat during this event.

The HPCI system is not required to mitigate a design basis tornado. The safety significance of this event is very low and there were no radiological releases associated with this event.

05000341/LER-2017-00410 August 2017
9 October 2017
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
On August 10, 2017, it was determined that inadequate procedural guidance for determining operability for ventilation support systems was being utilized. The Residual Heat Removal (RHR) switchgear and pump rooms have ventilation systems to maintain operability of the equipment in the rooms. Fermi 2 procedures had directed personnel to declare the supported equipment in the rooms inoperable due to nonfunclionality of the ventilation systems only if the room temperature exceeded the operability limit. Following discovery, a review of the RHR switchgear and pump room ventilation systems for the past three years was performed. The review identified multiple instances where the ventilation systems were nonfunctional and should have resulted in entry into applicable Technical Specifications (TS). Many of these instances resulted in operations or conditions prohibited by TS, since TS Required Actions were not completed within the Completion Times for restoration of affected equipment and plant shutdown. In addition, one instance was identified where the plant configuration was such that it could have prevented the fulfillment of the safety function to remove residual heat following a design basis accident. An engineering evaluation of this specific instance was performed and verified that the plant remained within its analyzed design basis. All other instances maintained one fully operable division of heat removal equipment such that no loss of safety function existed. There were no radiological releases associated with this event. The safety significance was determined to he very low. The cause of the event was inadequate procedural guidance. Immediate actions were taken to provide interim guidance related to the procedure. Corrective actions to revise the affected procedure have been completed.
05000341/LER-2017-00322 May 2017
21 July 2017
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On May 22, 2017 at 05:10 am (EST), while placing Division 2 Residual Heat Removal Service Water (RHRSW) in service for biocide treatment of the Division 2 Residual Heat Removal (RI IR) Reservoir, the Division 2 RI IRSW Flow Control Valve (FCV) (El 1 50F068B) failed to fully open.

Troubleshooting discovered the direct cause was failure of the anti-rotation bushing stem key. The apparent cause was system operating conditions (high vibration) resulting in the failed tack welds. Previous troubleshooting on an indication issue on May 5, 2017 for the RHRSW FCV was inadequate, and did not identify the failure of the anti-rotation key. As a result, the RHRSW FCV was returned to service at 2:50 pm on May 7, 2017, and subsequently failed on the next on-demand stroke at 5:10 am on May 22, 2017. Seventeen similar Motor Operated Valves (MOVs) were inspected and no MOVs exhibiting the symptoms observed on the E1150F068B prior to the failure of the anti-rotation key were found, and all anti-rotation devices were found to be intact. The Past Operability determination for 131150E068B found that the MOV was unable to perform its design basis functions from May 3. 2017 at 5:48 am, when the RI IRSW FCV was last successfully stroked under dynamic conditions, through May 24. 2017 at 4:04 pun, when the RI IRSW FCV was returned to service. The Division I RI-IRSW was available throughout the event except on two occasions. Division 1 of RHRSW was declared inoperable for Mechanical Draft Cooling Tower (MDCT) Nozzle Cleaning activities on May 9, 2017 from 8:41 am to May 9, 2017 at I I :18 pm. Division I of RI IRSW was again declared inoperable for IVIDCT Nozzle Cleaning activities on May 11, 2017 at 8:35 am through May 11, 2017 at 10:01 pm. The as found condition of the Division 2 RHRSW FCV is a condition prohibited by Technical Specification 3.7.1 and reportable under 10 CFR 50.73 (a)(2)(i)(13) "Operation or Condition Prohibited by Technical Specifications," and 10 CFR 50.73(a)(2)(v)(13) "Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: Remove Residual Heat.

05000341/LER-2017-00219 January 2017
16 March 2017
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)
On January 19, 2017, a condition was identified that impacted the operability of certain functions associated with the High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) systems under low reactor pressure conditions. HPCI and RCIC both have automatic and manual actuation functions to inject water into the reactor vessel. HPCI and RCIC also both have an automatic function (i.e. Level 8 trip signal) to prevent injection to the reactor vessel so that water does not reach the steam lines. This Level 8 trip signal comes from instrumentation that is calibrated to be most accurate at normal operating conditions. Under low reactor pressure conditions (i.e. below 600 psig), the high drywell pressure automatic actuation of HPCI and the manual initiation of both HPCI and RCIC are prevented by a Level 8 trip signal such that the affected HPCI and RCIC functions should be considered inoperable per Technical Specifications (TS). This can cause HPCI to also be considered inoperable, which could prevent the fulfillment of a safety function since HPCI is a single train system. Fermi 2 was at a pressure above 600 psig at the time of discovery and, therefore, the condition did not exist. However, a review of past operating conditions identified twelve instances in the past three years where the condition did exist. Based on an engineering analysis, the affected HPCI and RCIC functions are not required to perform a safety function at low reactor pressures; therefore, there was no adverse impact to public health and safety or to plant employees. There were no radiological releases. The cause of the event was an inconsistency between the Fermi 2 TS and the original design and licensing basis of the HPCI and RCIC systems. For corrective actions, Fermi 2 has submitted a license amendment request to clarify the TS.
05000341/LER-2017-0016 January 2017
6 March 2017
10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident

On January 6, 2017 an Operations Shift Engineer determined that use of the Reactor Protection System (RPS) test box described in station procedures would result in the loss of two RPS reactor scram functions. Technical Specification (TS) 3.3.1.1 requires that RPS instrumentation for Table 3.3.1.1-1 Function 5 for Main Steam Isolation Valves (MSIVs) and Table 3.3.1.1-1 Function 9 for Turbine Stop Valves (TSV) remain OPERABLE. Operations procedures were revised to incorporate the use of the test box in August of 2016.

Between September 22 and 23, 2016 the MSIV and TSV procedures were each performed one time using the test box. The failure to recognize the impact of the procedure revisions is considered a human performance error by engineering and operations personnel.

The procedures were corrected in January 2017 to remove the use of the RPS test box. Subsequently, on January 7 and 9, 2017, respectively, the procedures for the TSVs and the MSIVs were performed successfully.

05000341/LER-2016-00222 March 201610 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

On January 22, 2016, at 1923 EST, both divisions of the Residual Heat Removal (RHR) system were declared inoperable for the Low Pressure Coolant Injection (LPCI) mode of operation due to a failure of the division 1 LPCI outboard injection motor operated valve (MOV), El 1 50F017A. While performing the division 1 RHR pump and valve operability surveillance test, E1150F017A closed properly but failed to open during its required stroke time test. With this valve closed and unable to automatically open, LPCI injection into the Reactor Pressure Vessel (RPV) from both divisions of RHR would be prevented if the LPCI loop select logic selected the division 1 recirculation loop for injection; therefore, this failure rendered both divisions of RHR inoperable for the LPCI function.

Technical Specification limiting condition for operation (LCO) 3.5.1, Condition K, was entered, which requires immediate entry into LCO 3.0.3. The cause of the failure was subsequently identified as a foreign material (screw) that affected the function of the MOV contactor. The root cause was determined to be less than adequate inspection procedures and susceptibility of the contactor to foreign material. Inspection of all other susceptible equipment is ongoing to tighten loose screws and a modification is planned to install Foreign Material Exclusion (FME) barriers.

05000341/LER-2016-0016 January 2016
23 January 2017
10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

At 1514 EST on January 6, 2016, while operating at 100 percent Reactor Thermal Power (RTP), the East and West Turbine Bypass Valves (TBV) automatically opened as expected for 3 minutes and 32 seconds in response to the number one High Pressure Turbine Stop Valve (TSV) drifting from full open to 25 percent open due to an actuator malfunction.

Per Technical Specification (TS) Bases 3.3.1.1, TBVs must remain shut while RTP is at or above 29.5 percent to consider all channels of the TSV closure and Turbine Control Valve (TCV) fast closure Reactor Protection System (RPS) functions operable.

Reactor Operators lowered RTP to 91.0 percent and at 1518 EST the TBV automatically closed and the TSV closure and TCV fast closure RPS functions were no longer considered inoperable. TS 3.3.1.1 requires that the TSV closure and TCV fast closure RPS functions be operable at or above 29.5 percent RTP. In this event, during the period of time while TBVs were open, reactor power was maintained above 91 percent and the RPS functions were confirmed to be enabled.

The actuator malfunction was caused by faulty connectors within the actuator. The faulty connectors were replaced.

05000341/LER-2015-00319 March 201510 CFR 50.73(a)(2)(iv)(A), System Actuation

On March 19, 2015 at 0702 EST the reactor protection system at Fermi 2 initiated an automatic reactor scram on Oscil ation Power Range Monitor (OPRM) Upscale following the manual trip of the north reactor recirculation pump due to a cooling water leak. The reactor protection system performed as expected and all control rods were fully inserted into the core. Reactor water level reached a low of approximately 126 inches above top of active fuel and was restored and maintained in the normal operating band by the feedwater and control rod drive systems. No safety relief valves actuated and reactor pressure was controlled by the main turbine bypass valves. Plant systems responded to the scram as designed and all reactor parameters were maintained within design limits following the event.

The cause of the automatic reactor protection system scram on OPRM Upscale was the neutron flux oscillations following the large core flow reduction and lowering feedwater temperature after the trip of a reactor recirculation pump. This event was documented and evaluated in the Fermi 2 Corrective Action Program. The associated root cause evaluation is in progress and may identify additional corrective actions which will be tracked and implemented by the corrective action program.

This event is reportable in accordance with 10 CFR.50.73(a)(2)(iv)(A) as a critical reactor scram.

05000341/LER-2013-00324 November 201310 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material

On November 24, 2013, at approximately 00:01 hours EST, during normal plant operations, the non-safety related Reactor Building Heating Ventilation and Air Conditioning (RBHVAC) system tripped on low steam coil heater temperature. Secondary Containment differential pressure exceeded the Technical Specification (TS) Surveillance Requirement limit of -0.125 inches water column (WC), reaching a maximum of +0.08 inches WC. At 00:04 hours EST, the Standby Gas Treatment System (SGTS) was started and Secondary Containment differential pressure decreased to less than -0.125 inches WC. The RBHVAC system tripped due to lack of steam flow through a heating coil caused by inadequate draining of the downstream steam trap. Investigation revealed the presence of some corrosion and a cracked drain seat in the associated steam drain. The degraded steam drain was then replaced and tested. RBHVAC was returned to normal operation and SGTS was shutdown and returned to standby at 23:46 hours EST on November 24, 2013. Preventive maintenance is being scheduled to inspect, and clean or replace the RBHVAC steam traps and strainers.

With Secondary Containment differential pressure exceeding -0.125 inches WC, TS Surveillance Requirement 3.6.4.1.1 was not met and Secondary Containment was declared inoperable. No other degradation of Secondary Containment existed at the time of the event. This event was reported per the guidance of NUREG-1022, Rev. 3, section 3.2.7, as a loss of Safety Function. There were no radiological releases associated with this event.

05000341/LER-2013-00230 August 201310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On August 30, 2013 at approximately 0017 hours, while performing a routine surveillance procedure, Instrumentation and Control (I&C) technicians discovered that a thermocouple was improperly wired which resulted in an inoperable Division I Reactor Core Isolation Cooling (RCIC) area room temperature input to the associated steam line isolation logic. The improper wiring was determined to be in place for approximately 14 days without isolation of the RCIC steam line which is greater than allowed by Technical Specification 3.3.6.1.

The event was caused by technicians incorrectly replacing terminal block knife switches on August 16, 2013.

Insufficient rigor and was applied by the technicians during concurrent verification activities for interim alterations of the associated isolation circuitry. The thermocouple wiring was promptly corrected, the associated Channel Functional Test was satisfactorily completed at 0145 hours on August 30, 2013, and the equipment was returned to service. The qualifications of the technicians involved were removed until such time as the individuals were re- trained. Re-training on verification practices was conducted with I&C Group personnel.

05000341/LER-2013-00122 January 201310 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material

On January 22, 2013, at approximately 0113 hours EST, during startup of the Reactor Building Heating Ventilation and Air Conditioning (RBHVAC) system, with the Standby Gas Treatment System operating, Secondary Containment pressure went positive for 27 seconds, reaching approximately +0.15 inches of water column (WC).

The RBHVAC Center Exhaust Fan discharge damper appears to have opened after the Supply Fan discharge damper opened contrary to design, causing the Secondary Containment pressure increase. The System was returned to normal with two RBHVAC trains running and Standby Gas Treatment System shutdown and in standby. Reactor building pressure stabilized at less than -0.125 inches WC. The causes of this event appear to be delayed operation of the center RBHVAC exhaust fan discharge damper and relay timing out of tolerance for the RBHVAC Center Supply and Exhaust fan dampers. Work Management procedures are being followed to troubleshoot the actuator for the discharge damper and the supply and exhaust fan relay timing. This event has been entered into the Fermi 2 Corrective Action Program. Investigation continues and could result in additional corrective actions.

05000341/LER-2003-00410 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)

On November 7, 2003, it was determined Emergency Diesel Generator (EDG) 12 had been inoperable for a period which exceeded the limiting applicable Technical Specifications (TS) allowed outage time per TS 3.8.1, "AC Sources - Operating." Specifically, at 0200 hours on June 2, 2003, EDG 12 had been removed from its standby mode for maintenance. EDG 12 was restored to an operable status at 1448 hours on June 6, 2003; however, subsequent evaluation determined that EDG 12 had remained inopefable until 2134 hours on November 8, 2003. No TS Limiting Condition of Operation (LCO) had been invoked in the interim because it was believed that EDG 12 was restored to its standby operation mode at 1448 hours on June 6, 2003. This event is reportable under 10CFR50.73(a)(2)(i)(13) as an operation prohibited by Technical Specifications.

During maintenance activities for EDG 12 conducted on June 2, 2003, a lube oil pressure sensing line fitting was removed, cleaned, and reinstalled to correct an identified lube oil leak. On November 7, 2003, a loose fitting was discovered on the inside of the engine block. It was determined the fitting had been loosened durifig the June 2, 2003, maintenance to correct the oil leak on the outside of the engine block.

This event was determined to be caused by latent organizational weaknesses: omission of information and insufficient work organization and planning. Corrective actions are being taken to reduce the probability of similar events occurring in the future.

NRC FORM 388 (7.2001) ��

05000341/LER-2003-00310 CFR 50.73(a)(2)(i)

General Electric Company submitted a 10 CFR 21 notification identifying that they had determined that the stability Option III period based detection algorithm (PBDA) period confirmation adjustable variables (period tolerance and conditioning filter cutoff frequency) may be non-conservative, and recommended that the Average Power Range Monitoi (APRM) Operating Power Range Monitor - .

(OPRM) Upscale trip (Technical Specification Limiting Condition for Operation (LCO) 33.1.1, function 2.0 be considered inoperable for plants with a PBDA period tolerance setpoint less than 100 msec, and with a cutoff frequency of greater than 1.0 Hz. All OPRM channels were declared inoperable (but were maintained in a functional and armed condition) on October 2, 2003, because the Fermi-2 OPRM period tolerance was set at 50 msec, and the conditioning filter cutoff frequency was set at 3.0 Hz. Alternate methods to detect and suppress thermal hydraulic instability oscillations were placed into effect in accordance with Technical Specification LCO 33.1.1, Action J. The apparent deficiency was identified by General Electric (the OPRM and reactor vendor) following a July 24, 2003 instability event at Nine Mile Point-2. The Fermi OPRM settings would have been sufficient to identify a wide range of stability transients. Additionally, the operators have been trained to recognize instabilities and to take appropriate actions should an instability occur. The period tolerance and conditioning filter cutoff frequency setpoints were changed and all OPRM channels were declared operable on November 18, 2003. This event has been documented in the Fermi 2 corrective action program.

NRC FORM 368 (7.2o01)

05000341/LER-2002-00510 CFR 50.73(a)(2)(i)(B), Prohibited by Technical SpecificationsThe General Electric Company submitted a 10 CFR Part 21 notification identifying that they had determined that the stability Option III period based detection algorithm (PBDA) range for minimum period of detection (Tmin) values that they had specified may be non-conservative, and recommended that the Average Power Range Monitor (APRM) Oscillation Power Range Monitor (OPRM) Upscale trip (Technical Specification Limiting Condition for Operation (LCO) 3.3.1.1, function 2.f) be considered inoperable for plants with Tmin set at greater than 1.2 seconds. In response, all OPRM channels were declared inoperable on November 21, 2002 because the Fermi 2 OPRM Tmin value was set at 1.4 seconds. Alternate methods to detect and suppress thermal hydraulic instability oscillations were placed into effect in accordance with Technical Specification 3.3.1.1, Action J. The apparent deficiency identified in the Tmin value was discovered during recent calculations performed by General Electric in support of extended power uprate analyses for other plants. The newly identified shorter period oscillations have decay ratios of less than 0.8; and therefore, are not of concern. Additionally, the operators have been trained to recognize instabilities and to take appropriate actions should an instability occur. Therefore, this event had no safety significance. Tmin was changed to 1.2 seconds, and all OPRM channels were declared operable on December 19, 2002.
05000341/LER-2002-00410 CFR 50.73(a)(2)(iv)(A), System Actuation

On October 2, 2002, at 1453 hours, the reactor scrammed from 100 percent power. Condenser pressure increased when Circulating Water Pump (CWP) 2, one of four running CWPs, failed. Condenser pressure exceeded the main turbine trip setpoint. The main turbine tripped, resulting in a reactor scram.

Prior to the scram at 1452 hours the Circulating Water Header Low Pressure annunciator was received.

The Condenser Pressure High annunciator was received and control room operators (licensed, utility) entered the Abnormal Operating Procedure for Loss of Condenser Vacuum. The main turbine automatically tripped causing a reactor scram on main turbine control valve fast closure. All safety systems responded as expected. All rods fully inserted into the core. Reactor level decreased below Level 3, resulting in expected isolation signals. After the reactor scram, condenser vacuum recovered.

Reactor level was recovered with the Feedwater/Condensate System. No Emergency Core Cooling Systems initiated and no Safety Relief Valves lifted. The cause of the event was a failure of CWP 2.

This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A), as an event that resulted in manual or automatic actuation of any systems listed in paragraph (a)(2)(iv)(B), i.e., actuation of the Reactor Protection System including reactor scram or reactor trip. The cause of the CWP failure was fatigue failure of the diffuser casing to column bolts due to insufficient or loss of pre-load.

05000341/LER-2002-00310 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentOn June 27, 2002, Division 1 Control Room Emergency Filtration (CREF) system was started to support a Post Maintenance Test. Following the system start, a Nuclear Operator reported unusual noise from the Division 1 Control Center Heating, Ventilation and Air Conditioning (CCHVAC) Return Air Fan. Vibration analysis concluded that the most probable cause was a failing fan outboard bearing. The fan was shutdown and Division 1 CREF system was declared inoperable. A work request was initiated which identified the need to open an access panel in the fan ductwork. The access panel had to be unlocked and opened to allow access to the fan outboard bearing. The work request was reviewed and authorized by Operations. At 2152 hours, control room pressure increased and control room pressure alarms were received. A Nuclear Operator was dispatched to evaluate the Division 1 CREF system maintenance activities and noted that the access panel was open. Evaluation of the pressure response of the Division 2 CREF system identified that opening the access panel on the Division 1 Return Air Fan duct work resulted in unfiltered, bypass leakage into the Division 2 CREF system. Technical Specification 3.0.3 was entered due to both divisions of CREF system being inoperable. Immediate actions were taken to close the access panel and reestablish CREF system ducting integrity. Analysis of the event identified deficient knowledge of CREF system divisional interrelationship and inadequate implementation of the work control process as the causes.
05000341/LER-2002-00219 February 2002

As a result of a fire protection program self assessment, on May 2, 2002, Detroit Edison Company determined that a field modification performed on February 19, 2002 invalidated an inherent assumption in the procedure for controlling the plant from the dedicated shutdown panel. Specifically, the motor operator for motor operated valve (MOV) N2000F636, Condenser Hotwell Emergency Makeup Bypass Valve, was rotated 180 degrees to help alleviate an oil leakage problem. Rotating the MOV relocated the motor operator handwheel away from the first floor of the Turbine Building such that operators could not reasonably close the valve without the use of a ladder. Procedure 20.000.18, "Control of the Plant from the Dedicated Shutdown Panel," directs operators to de-energize and manually close N2000F636 to prevent losing Condensate Storage Tank (CST) water inventory to the Hotwell, in case a hot short caused the valve to open. Losing CST inventory threatens the ability to achieve safe shutdown conditions in the event of a fire. Therefore, this condition is reportable under Section 2.F of the Fermi 2 Operating License as a violation of License Condition 2.C.(9).

Based on the short delay associated with obtaining a ladder and closing the valve, this condition did not result in any adverse effect on the health and safety of the public.

A dedicated ladder has been staged near the valve. Other corrective actions involve the identification of Appendix R components in the plant CECO database, additional training and guidance on dealing with Appendix R components, and periodic verification of the steps in procedure 20.000.18.

05000341/LER-2001-00310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On November 9, 2001, leak testing of Pressure Isolation Valve (PIV) El 1 00F050A, Division 1 Residual Heat Removal (RHR)/Low Pressure Coolant Injection (LPCI) System injection line inboard isolation check valve, was performed in accordance with Technical Specification (TS) Surveillance Requirement SR 3.4.5.1. The resultant leak rate was determined to be in excess of the specified leakage criteria of 10 gpm. The valve and its air-operated test actuator were disassembled and inspected. It was determined that the disk was being prevented from fully closing by the actuator. The cause of the failure of the disk to fully close was determined to be improper reassembly of the actuator during the previous refueling outage because of inadequate craft skills and insufficient craft supervision during this period. The actuator was rebuilt properly, the soft seat was replaced and the valve was successfully leak rate tested. The opposite division counterpart, E1100F050B, successfully passed its as-found leak test this outage; however, it was also disassembled, inspected, and its soft seat replaced.

With both actuators properly assembled, and with new soft seats installed, historical performance indicates that both valves should pass their as-found leak rate tests at the end of the next operating cycle.

05000341/LER-2001-002

On September 28, 2001, Detroit Edison determined that a non-conservative bias existed in the reactor heat balance methodology for calculating core thermal power. Specifically, the main steam moisture carryover fraction used in the heat balance calculations was found to overestimate the actual moisture content of the steam. Due to this condition, it is possible that Fermi 2 exceeded its licensed power limits on one or more occasions; however, this bias represents an insignificant portion of the total thermal power (less than 0.1 percent) and is also small compared to the overall precision of the core thermal power evaluation. Exceeding the thermal power limit in Fermi 2 License Section 2.C.(1) is a reportable condition under Section 2.F. of the Fermi 2 Operating License.

Based on the low order of magnitude of the calculation bias and conservatism inherent in the power levels used for safety analyses, this condition did not result in any adverse impact on the health and safety of the public.

The moisture carryover fraction in the heat balance calculations will be revised to reflect the plant test data. As an interim measure, the maximum reactor power level was administratively reduced by three megawatt thermal.

05000341/LER-1998-008, Forwards LER 98-008-01,re Inboard Pressure Isolation Valve Which Did Not Meet Required Leakage Limits.Revised LER Documents One Previous Occasion Where Inboard Pressure Isolation Valve Did Not Meet Required Leakage Limits26 March 1999
05000341/LER-1998-007, Forwards LER 98-007-00,which Documents Inadvertent Deenergization of Safety Buses 65E,72E,13EC & 72EC When EDG 13 Outbreaker Opened During Performance of Surveillance Testing.Resulting in Several ESF Actuations5 October 1998
05000341/LER-1998-006, Forwards LER 98-006-01,providing Cause & Results of Repair or Rework & Testing for MSIVs Which Failed to Meet Specified Leakage Limits of TS 3.6.1.2 During Sixth RO13 November 1998
05000341/LER-1998-005, Forwards LER 98-005-00 Documenting Unplanned Manual Reactor Scram in Response to Reactor Power Fluctuations.Commitment Made by Util,Listed1 October 1998
05000341/LER-1998-004, Forwards LER 98-004-00 Documenting Unplanned Manual Reactor Scram in Response to Reactor Power Fluctuations.Commitment Made by Util,Listed18 August 1998
05000341/LER-1998-003, Forwards LER 98-003-01,which Addresses Issues Identified as Result of Investigation of Fire Induced Spurious Operation of Valves That Could Cause Inadvertent Opening of Drain Path from CST to Hotwell.Commitments Listed31 July 1998
05000341/LER-1998-002, Forwards LER 98-002-00,per 10CFR50.73(a)(2)(iv) & 10CFR50.73(a)(2)(i)(B),which Documents Inadvertent Load Shed of ESF Bus 72E During Performance of Surveillance Testing. Commitments Being Made within Ltr,Listed19 March 1998
05000341/LER-1997-014, Forwards LER 97-014-01 Which Addresses Issues Identified as Result of Investigation of Unsealed Penetrations in Auxiliary Bldg.Commitments Made in LER Listed6 April 1998
05000341/LER-1997-012, Forwards LER 97-012-00,documenting Issues Identified in Performance of Surveillance Testing for Reactor Recirculation Sys Motor Generator Set Mechanical & Electrical Stops.Testing Considered Adequate3 July 1997
05000341/LER-1997-011, Forwards LER 97-011,documenting Late Performance of Turbine Stop Valve Closure & Turbine Control Fast Closure Channel Functional Tests.Commitments Made Listed6 June 1997
05000341/LER-1997-009, Forwards LER 97-009-00 Re Failure to Inspect Control Rod Drive Housing Support Structure Following Maint in Housing Support Area,Per 10CFR50.73.Commitments Made within Ltr, Listed19 May 1997
05000341/LER-1997-008, Forwards LER 97-008-00 Re Potential Common Mode Failure Mechanism That Existed w/480 Volt MCC Fused Disconnect Switches12 May 1997
05000341/LER-1997-007, Forwards LER 97-007-00,re Failure of Reactor Building Ventilation Sys Resulting in Loss of Secondary Containment Integrity During Shutdown Conditions.W/Listed Commitments24 April 1997
05000341/LER-1997-006, Forwards LER 97-006-01,re Response Time Testing Not Being Conducted IAW Ts.Rev Provides Revised Dates of non- Compliance Found During Review Being Conducted for Extension of Surveillance Intervals for Current Cycle 627 July 1998
05000341/LER-1997-005, Forwards Rev 1 to LER 97-005 Re Inadequate Design or Consideration of Circuits Involved in Achieving Dedicated Shutdown12 May 1997
05000341/LER-1997-004, Forwards LER 97-004-01 Re Calibration of Primary Containment Oxygen Monitor in de-inerted Environment Challenging Operability of Monitor in Inerted Environment1 August 1997
05000341/LER-1997-003, Forwards LER 97-003-01,which Documents Condition Outside Design Basis Related to EECW Sys Containment Isolation Function.Diverse Power Mod of Eecs Sys Primary Containment Penetrations Have Been Completed8 May 1997
05000341/LER-1997-002, Forwards LER 97-002 Documenting Failure of HPCI Pump Discharge Valve to Open Upon Manual Demand Signal,During SD Conditions.Util Commitment Is to Evaluate SR & Balance of Plant Valves from Overall Plant Risk Perspective18 March 1997
05000341/LER-1997-001, Forwards LER 97-001-00 Re an Error in Mass Flow Conversion Algorithm in Heat Balance Methodology for Calculating Core Thermal Power.Util Commitments Made within Ltr10 March 1997
05000341/LER-1996-023, Forwards LER 96-023-00 Documenting Event That Occurred at Fermi 2 on 961224.Commitments Made within Ltr,Listed23 January 1997
05000341/LER-1996-022, Submits LER 96-022 Re Loss of Positive Position Indication in CR for One Main Steam Line SRV6 January 1997
05000341/LER-1996-018, Forwards LER 96-018-00.Commitments Listed Including Rev to Reactor Head Detensioning & Tensioning Procedure5 December 1996
05000341/LER-1996-017, Forwards LER 96-017-03 Re Failure of SRVs to Open within Specified TS Required Tolerance.Revised Commitments Made by Util,Listed10 November 1997
05000341/LER-1996-016, Forwards LER 96-016-01 Which Deals W/Esf Actuation29 April 1997
05000341/LER-1996-015, Forwards LER 96-015 That Documents ESF Actuation of Division 2 Emergency Equipment Cooling Water Sys Which Occurred During Fill & Vent Evolution of Portion of Sys Located in Drywell.Commitments Made within Ler,Listed14 November 1996
05000341/LER-1996-013, Forwards LER 96-013-00.Reactor Recirculation Pump Motor Power Instrument Loop Will Be Added to Configuration Mgt Sys & Associated Calibr Instruction Will Be Revised4 November 1996
05000341/LER-1996-010, Forward LER 96-010-00 Which Documents ESF Actuation Involving Transfer Af HPCI Suction Flow Path from CST to Suppression Pool.Caused by Radio Frequency Interference Driving Output of CST Level19 August 1996
05000341/LER-1996-005, Forwards LER 96-005-01 Re EECW Being in Unanalyzed Condition & Subsequent TS Required Shutdown.Commitments Made by Util, Listed20 August 1998
05000341/LER-1996-003, Forwards LER 96-003-00 Re ECCS Being Outside Design Basis of Plant During Safeguards Bus 64C Undervoltage Protection Scheme Functional Testing18 March 1996
05000341/LER-1996-001, Forwards LER 96-001-00 Re Identification of Potential for Common Cause Failure of Diesel Generator Cooling Water Function Due to Ice Formation in Pump Column6 March 1996
05000341/LER-1995-008, Provides Commitment Made Re Suppl to LER 95-008 Concerning Nonconservative Bias in Heat Balance Methodology for Calculating Core Thermal Power15 November 1996