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Discovered date | Reporting criterion | Title | Event description | |
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ENS 57033 | 17 March 2024 20:15:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Trip Due to Main Feedwater Pump Trip | The following information was provided by the licensee via phone and email: On March 17, 2024, at 1515 CDT, the Comanche Peak Unit 2 reactor was manually tripped due to an anticipated automatic trip due to lo-lo steam generator (SG) water levels. Prior to the trip, main feedwater pump '2B' tripped and an auto runback to 700 MW (60 percent power) was in progress. Both motor driven auxiliary feedwater pumps and the turbine driven auxiliary feedwater pump started due to lo-lo level in all SGs. Unit 2 is being maintained in hot standby (Mode 3) in accordance with integrated plant operating procedures IPO-007B. The emergency response guideline network has been exited. Decay heat is being rejected to the main condenser via the steam dump valves. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the '2B' main feed pump trip was due to loss of primary and redundant power to the servo control valve. The loss of power to the servo control valve is under investigation. |
ENS 57024 | 12 March 2024 13:16:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Trip | The following information was provided by the licensee via phone and email: On March 12, 2024, at 0816 CDT, Comanche Peak Unit 2 reactor automatically tripped on lo-lo level in the 2-03 steam generator (SG). Prior to the trip, main feedwater pump (MFP) 2A speed reduced and a manual runback to 700 MW (60 percent) was in progress. Both motor driven auxiliary feedwater pumps and the turbine driven auxiliary feedwater pump started due to lo-lo level in all SGs. Concurrent with the loss of speed on MFP 2A, a servo filter swap was in progress on MFP 2A. Unit 2 is being maintained in hot standby (Mode 3) in accordance with integrated plant operating procedure IPO-007A. The emergency response guideline network has been exited. Decay heat is being rejected to the main condenser via the steam dump valves. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the loss of the MFP is under investigation. Unit 1 was unaffected. |
ENS 57021 | 11 March 2024 17:37:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge | Manual Reactor Trip | The following information was provided by the licensee via phone and email: On March 11, 2024, at 1337 EDT, with Unit 1 in Mode 1 at 35 percent power performing power ascension activities, the reactor was manually tripped due to the 'A' reactor feed pump (RFP) tripping on low suction pressure. Due to the power level at the time, the 'B' RFP had not been placed in service. Closure of containment isolation valves (CIVs) in multiple systems and actuation of high-pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) occurred as a result of reaching the actuation setpoint on reactor water level as designed. The trip was not complex, with all safety systems responding normally post-trip. Operations responded and stabilized the plant. The 'B' RFP was placed in service and is controlling reactor water level. Decay heat is being removed by discharging steam to the main condenser using turbine bypass valves. Unit 2 is not affected. Due to the emergency core cooling system (ECCS) discharging into the reactor, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A). Also, the Reactor Protection System actuation while critical is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, it is reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of CIVs, RCIC and HPCI. There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the 'A' RFP is under investigation. The reactor electric plant remains in a normal lineup with both emergency diesel generators available. There were no temperature or pressure technical specification limits approached. |
ENS 56995 | 28 February 2024 14:39:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Scram | The following information was provided by the licensee via fax and email: At approximately 0839 (CST) with Unit 1 in Mode 1 at 100 percent power, the reactor automatically scrammed due to the depressurization of the SCRAM air header caused by an invalid signal that (occurred) during system testing. The SCRAM was uncomplicated with all systems responding as expected. The cause and details of the event are under investigation. Containment isolation valves actuated and closed on a valid Group 2 signal. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B), and an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for the Group 2 isolation signal. Operations responded using the emergency operating procedure and stabilized the plant in Mode 3. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. State as well as Wright and Sherburne Counties will be notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The Anticipated Transient Without Scram (ATWS) circuit was being tested when an invalid signal was sent to depressurize the SCRAM air header. |
ENS 56991 | 24 February 2024 20:46:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Trip Due to Steam Generator 22 Feed Pump Trip | The following information was provided by the licensee via email: At 1546 EST, with unit 2 at 100 percent power, the reactor was manually tripped due to the '22' steam generator feed pump tripping. The trip was uncomplicated with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Operations responded using emergency operation procedure EOP-0, Post Trip Immediate Actions and EOP-1, Uncomplicated Reactor Trip and stabilized the plant in mode 3. Decay heat is removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 is not affected. ESFAS (engineered safety features actuation systems) actuation (auxiliary feedwater manual actuation) is reportable under 10 CFR 50.72(b)(3)(iv)(A) 8-hour report. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56936 | 29 January 2024 17:02:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Scram | The following information was provided by the licensee via email: At approximately 1202 EST on 01/29/24, unit 2 experienced a reactor scram caused by a main turbine trip. Investigation is still ongoing. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All control rods were fully inserted. The licensee indicated that the turbine trip may have been caused by a power load imbalance, however the cause of the incident is under investigation. The scram was not complex. Decay heat is currently being removed thru bypass valves dumping to the main condenser. Initially unit 2 lost the use of the bypass valves due to lack of condenser vacuum. Unit 2 used the high pressure coolant injection (HPCI) system in the condenser storage tank (CST) to CST mode to remove decay heat. Residual heat removal was used to keep the torus cool. Condenser vacuum was regained and unit 2 is back to removing decay heat with the turbine bypass valves. There was no impact to unit 3. The licensee confirmed there was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
The following information was provided by the licensee via email: Licensee adds 8-hour non-emergency 10 CFR 50.72(b)(3)(iv)(A) specified system actuation report to original 4-hour non-emergency 10 CFR 50.72(b)(2)(iv)(B) RPS Actuation report. At approximately 1202 EST on 01/29/24, unit 2 experienced a reactor scram by a main turbine trip. All control rods inserted. Reactor core isolation cooling system (RCIC) was manually initiated for level control. HPCI was manually initiated for pressure control. Primary containment isolation system (PCIS) Group II and III isolations occurred (specified system actuation). Investigation is ongoing. The NRC Resident Inspector has been notified. |
ENS 56889 | 15 December 2023 00:39:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Automatic Reactor Scram | The following information was provided by the licensee via phone call and email: On December 14, 2023, at 1939 EST, Hope Creek reactor scrammed following closure of turbine control valve number 4. All control rods fully inserted into the core. All safety systems responded as designed and expected. There was no radiological release. The unit is stable in mode 3 with decay heat being removed via the turbine bypass valves rejecting steam to the main condenser. Normal feedwater level control is providing makeup to the reactor vessel. No personnel injuries resulted from the event. The outage control center has been staffed to determine the cause of the reactor scram. The Hope Creek NRC Resident Inspector has been notified. |
ENS 56856 | 16 November 2023 07:27:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Trip | The following information was provided by the licensee via email: At 0227 EST on 11/16/23, Calvert Cliffs Unit 2 experienced an automatic trip from the reactor protection system (RPS) based on reactor trip bus undervoltage (UV). At that time, a loss of U-4000-22 (13 kV to 4 kV transformer) caused a loss of 22, 23, and 24 4 kV busses. This resulted in a loss of both motor generator (MG) sets causing the reactor trip bus UV. The loss of 22 and 23 4 kV non-safety related busses resulted in a loss of main feedwater. Auxiliary feedwater (AFW) was manually initiated and is feeding both steam generators. The 2B diesel generator (DG) started and restored the 24 4 kV safety related bus. Heat removal is via the normal turbine bypass valves to the main condenser. RPS actuation is reportable under 10 CFR 50.72(b)(2)(iv)(B) - 4 hour report ESFAS (engineering safety features actuation system) actuation (2B DG start on UV) is reportable under 10 CFR 50.72(b)(3)(iv)(A) - 8 hour report AFW operation is reportable under 10 CFR 50.73(a)(2)(iv)(A) - 60 day report The NRC Senior Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All rods fully inserted. There was no impact on Unit 1 operations. Unit 2 is stable in mode 3.
ESFAS actuation (AFW manual initiation) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8 hour report Notified R1DO (Defrancisco). |
ENS 56846 | 10 November 2023 08:14:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Scram | The following information was provided by the licensee via email: At 0118 EST, with Unit 1 in Mode 1 at 100 percent power, the reactor was manually scrammed due to degrading main condenser vacuum. The scram was not complex, with all systems responding normally post-scram. The main turbine bypass valves opened automatically to maintain reactor pressure. Operations responded and stabilized the plant. Reactor water level is being maintained via feedwater pumps. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 2 is not impacted. Due to Reactor Protection System actuation while critical, this event is being reported as a four-hour and eight-hour non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). Unit 1 reactor is currently stable in mode 3. An investigation is in progress into the cause of the degrading condenser vacuum. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56839 | 7 November 2023 21:17:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Reactor Trip Due to NON-SAFETY Related Bus Under Voltage | The following information was provided by the licensee via email: At 1617 on 11/7/2023, Calvert Cliffs Unit 2 experienced an automatic trip from a Reactor Protection System (RPS) based on reactor trip bus under voltage (UV). At that time a loss of U-4000-22 caused a loss of 22, 23, and 24 4kV busses. This resulted in a loss of both motor generator (MG) sets causing the reactor trip bus UV condition. The loss of 22 and 23 4kV non-safety related busses resulted in a loss of main feedwater. Auxiliary feedwater (AFW) was manually initiated and is feeding both steam generators. The 2B diesel generator (DG) started and restored the 24 4kV safety related bus. Heat removal is via the normal turbine bypass valves to the main condenser. RPS actuation is reportable under 10 CFR 50.72(b)(2)(iv)(B) - 4-hour report. ESFAS actuation (2B DG start on UV) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8-hour report. ESFAS actuation (AFW manual initiation) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8-hour report. Site Senior NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 1 was unaffected. Estimation of duration of shutdown is 24 hours. |
ENS 56826 | 1 November 2023 10:48:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge | Manual Reactor Trip Due to Trip of Reactor Feed Pump | The following information was provided by the licensee via email: At 0648 EDT on 11/1/23, with Unit 2 in MODE 1 at 56 percent power, the reactor was manually tripped due to a trip of the 'B' reactor feed pump (RFP). The 'A' RFP had been previously isolated due to a leak. Closure of containment isolation valves (CIVs) in multiple systems and the actuation of high pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) occurred as a result of reaching the actuation setpoint on reactor water level as designed. The trip was not complex, with all safety systems responding normally post-trip. Operations responded and stabilized the plant. Reactor water level is being maintained with RCIC. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 was not affected. Due to the emergency core cooling system (ECCS) discharging into the reactor this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A). Also, the reactor protection system actuation while critical is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, it is reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of CIVs, RCIC and HPCI. There was no impact on the health and safety of the public or plant personnel. The Resident Inspector was notified. |
ENS 56692 | 22 August 2023 21:24:00 | 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Trip and Automatic Actuation of Auxiliary Feedwater System | The following information was provided by the licensee via email: At 1724 EDT, on August 22, 2023, with Unit 1 in Mode 1 at 100 percent power, the reactor was manually tripped due to a failure of the non-safety heater drain pump 'B' and the failure of the non-safety condensate pump 'A' to automatically or manually start. At 1735 EDT, a fire was identified on heater drain pump 'B' and was extinguished by the onsite fire brigade at 1807 EDT. Operations responded and stabilized the plant. The trip was not complex, with all safety systems responding normally post-trip. Decay heat is being removed by the main steam system to the main condenser using the steam dumps. There was no impact to Units 2, 3, or 4. An automatic actuation of the auxiliary feedwater system (AFW) also occurred, as expected, due to lo-lo steam generator levels resulting from the reactor trip. AFW is currently controlling all steam generator levels at their normal levels. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the notification of another government agency, the Burke County Fire Department, this event is being reported as a four-hour, non-emergency notification under 10 CFR 50.72(b)(2)(xi). The Burke County Fire Department was not needed to extinguish the fire. This event is also being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the auxiliary feedwater system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56676 | 11 August 2023 08:29:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Scram | The following information was provided by the licensee via phone and email: At 0329 (CDT) on August 11, 2023, with Unit 2 in Mode 1 at 90 percent power, the reactor automatically tripped due to a turbine trip. The trip was uncomplicated with all systems responding normally post-trip. The cause and details of the event are under investigation. Containment isolation valves actuated closed in multiple systems on a valid Group II signal. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B), and an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for the Group II isolation. Operations responded using the emergency operating procedure and stabilized the plant in Mode 3. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56645 | 30 July 2023 19:26:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Trip Due to LOW Main Turbine ELECTRO-HYDRAULIC Control (EHC) Oil Level | The following information was provided by the licensee via email: On July 30, 2023 at 1526 EDT, with unit 1 in mode 1 at 100 percent power, the reactor was manually tripped due to low main turbine electro-hydraulic control oil level. The trip was uncomplicated with all systems responding normally post-trip. Operations stabilized the plant in mode 3. Decay heat removal is being accomplished using the steam dumps in steam pressure mode to the main condenser. Emergency Feedwater actuated due to low-low steam generator level as expected. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector has been notified. |
ENS 56585 | 22 June 2023 14:35:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Trip Occured During Protection System Testing | The following information was provided by the licensee via email: At 1035, on June 22, 2023, with Unit 2 in Mode 1 at 100% power, the reactor automatically tripped due to `A' train reactor trip breaker and `B' train reactor trip bypass breaker opening during testing. The trip was not complex, with all systems responding normally post-trip. MST-021 (Reactor Protection Logic Train `B' At Power) testing was in progress at the time of trip. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). As a result of the reactor trip, emergency feedwater actuated; therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56580 | 16 June 2023 23:32:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Trip Due to LO-LO Steam Generator Level | The following information was provided by the licensee via email: (On June 16, 2023,) at 1832 CDT, Unit 1 reactor automatically tripped on lo-lo level in the '1-04' steam generator (SG). Prior to the trip, the 1B (main feedwater pump) (MFP) tripped due to speed oscillations and a runback to 700MW was in progress. Both motor driven auxiliary feedwater pumps started due to the lo-lo level in SG '1-04'. Unit 1 is being maintained in hot standby (Mode 3) in accordance with Integrated Plant Operating Procedure IPO-007A. The Emergency Response Guideline network has been exited. Decay heat is being rejected to the main condenser via the steam dump valves. The licensee notified the NRC Resident Inspector. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 1 is in a normal post-trip electrical line-up. There was no effect on Unit 2 due to the Unit 1 trip. |
ENS 56551 | 2 June 2023 11:05:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Trip | The following information was provided by the licensee via email: The following event description is based on information currently available. If through subsequent reviews of this event additional information is identified that is pertinent to this event or alters the information being provided at this time a follow-up notification will be made via the ENS (Emergency Notification System) or under the reporting requirements of 10 CFR 50.73. At 0405 MDT on June 2, 2023, the Unit 2 reactor automatically tripped on low steam generator water levels due to degraded flow from the A main feedwater pump. Steam generator water levels reached the automatic Auxiliary Feedwater Actuation System (AFAS) setpoint resulting in automatic AFAS-1 and AFAS-2 actuations and subsequent start of both class auxiliary feedwater pumps. Steam Generator water levels are being restored to normal band with the class 1E powered motor driven auxiliary feedwater pump. Following the reactor trip, all control element assemblies inserted fully into the core. No emergency plan classification was required per the Emergency Plan. Safety related buses remained powered from offsite power during the event and the offsite power grid is stable. Both emergency diesel generators automatically started on the AFAS-1 and AFAS-2 actuations as designed and are currently running unloaded. This event is being reported as a reactor protection system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B) and a specified system actuation in accordance with 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident Inspector has been informed. Unit 1 and 3 are in Mode 1 at 100 percent power. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Decay heat is being removed to main condenser via automatic steam bypass and B auxiliary feedwater pump. |
ENS 56497 | 2 May 2023 08:23:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Manual Reactor Trip | The following information was provided by the licensee via email: At 0423 EDT on 05/02/2023, with Unit 3 in Mode 1 at 14 percent power, the reactor was manually tripped due to securing all main feed pumps, due to sudden high differential pressure on their suction strainers. The trip was not complex, with all safety-related systems responding normally post-trip. No equipment was inoperable prior to the event that contributed to the event or adversely impacted plant response to the reactor trip. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser using the steam dumps, and startup feedwater is supplying the steam generators. Units 1, 2, and 4 were not affected. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56478 | 20 April 2023 05:48:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Trip Due to a Turbine Trip | The following information was provided by the licensee via phone and email: At 0148 Eastern Daylight Time (EDT) on April 20, 2023, with Unit 1 in Mode 1 at 100% power, the reactor automatically tripped due to a turbine trip. Turbine Bypass valves did not open on the trip due to Turbine Protection system power supply failure; the Safety Relief Valves (SRVs) opened automatically to control reactor pressure. Reactor Pressure reached approximately 1095 psig on the trip; exceeding the 1060 psig RPS trip setpoint. Operations responded and stabilized the plant. Operations was able to transition from SRVs to main steam line drains to the condenser. Reactor water level is being maintained via the Condensate / Feedwater system. Decay heat is being removed by discharging steam to the main condenser using the main steam line drains. Due to the Reactor Protection System (RPS) actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Reactor water level reached low level 1 (LL1) following the reactor trip. The LL1 signal causes Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sampling isolation valves), and Group 8 (i.e., shutdown cooling isolation valves) isolations. The LL1 isolations occurred as designed; the Group 8 valves were closed at the time of the event. Due to the valid Primary Containment Isolation System (PCIS) actuation and RPS actuation from the reactor pressure signal, this event is also being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A). Unit 2 is not affected by this event. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56446 | 31 March 2023 18:32:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Scram and Automatic Actuation of Containment Isolation Valves (Civs) | The following information was provided by the licensee via email: At 1432 EDT on 03/31/23, with Unit 2 in mode 1 at 97 percent power, the reactor was manually tripped due to a loss of both recirculation pumps. The cause of the recirculation pump trips is under investigation. Additionally, closure of CIVs in multiple systems occurred during the trip as a result of reaching the actuation setpoint on reactor water level as designed. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Reactor water level is being maintained via condensate / feedwater. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 is not affected. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). It is also reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of CIVs. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56329 | 1 February 2023 15:56:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Trip Due and Automatic Actuation of Auxiliary Feedwater System | The following information was provided by the licensee via email: At 0956 CST with Unit 1 in Mode 1 at 100 percent power, the reactor automatically tripped due to a turbine trip. The trip was not complex with all safety related systems responding normally post-trip. During the trip, the non safety related '1A' 4160V bus lost power resulting in the loss of one Reactor Coolant Pump (RCP-1A). Operations responded and stabilized the plant. The '1A' 4160V bus was re-energized at 1031 CST. Decay heat is being removed by steam dumps to the main condenser. Farley Unit 2 is not affected. An automatic actuation of (Auxiliary Feedwater) AFW also occurred, which is an expected response from the reactor trip. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour report per 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Auxiliary Feedwater System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56298 | 5 January 2023 17:42:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge | Automatic Reactor Scram | The following information was provided by the licensee via phone and email: At 1242 (EST) on 05 January 2023, with the Unit in Mode 1 at 99 percent power, the reactor automatically tripped on low Reactor Pressure Vessel level while restoring power to Digital Feedwater Control Stations when there was a perturbation to the level controls. The reason for perturbation is unknown at this time. The trip was not complex, with all systems responding normally post trip. Operations responded and stabilized the plant. High pressure core spray was manually initiated in accordance with site procedures. Reactor water level is being maintained via the Feedwater System. Decay heat is being removed by the Main Condenser. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A) and 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56278 | 17 December 2022 05:51:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Scram | The following information was provided by the licensee via email: On December 16, 2022 at 2351 CST, with the Unit in Mode 1 at 13 percent power, a manual scram was inserted due to lowering Reactor Pressure Vessel (RPV) pressure, which occurred following an unexpected opening of Main Turbine Bypass Valve 1. All control rods fully inserted. Following actuation of the manual scram, RPV pressure lowered, resulting in an automatic Primary Containment lsolation (PCIS) Group 1 isolation (expected response). The main steam isolation valves and steam line drain valves all closed. The Group 1 (isolation) has been reset allowing RPV pressure control with steam line drains to the main condenser. All systems responded as designed. The plant is stable in Mode 3. Investigation of the bypass valve opening is ongoing. This event is reportable under 10 CFR 50.72(b)(2)(iv)(B) RPS Actuation and 50.72(b)(3)(iv)(A) Specified System Actuation. There was no impact on health and safety of the public or plant personnel. The NRC Senior Resident Inspector has been notified. |
ENS 56210 | 4 November 2022 19:00:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Manual Scram Due to Rising Water Level | The following information was provided by the licensee via email: On November 4, 2022, at 1400 hours, with Unit 2 (U2) in Mode 1 at 100 percent power, a manual scram was inserted on U2 due to rising reactor water level, which occurred following an unexpected opening of the 2B Feedwater Regulating Valve. Following the reactor scram, reactor water level decreased to approximately 0 inches, which resulted in an automatic Group II and Group III isolation (expected response). Reactor Water Level control has been established in a normal band. The cause and details of the event are under investigation. The Unit 2 scram was not complicated. Operations responded using the Emergency Operating Procedures and stabilized the plant in mode 3. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 was unaffected by the event and remains at 100 percent power. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56120 | 26 September 2022 07:38:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Manual Reactor Trip Due to Reported Fire on Isophase Bus Duct | The following information was provided by the licensee via fax email: At 0238 CDT on 9/26/2022 with Unit 2 in Mode 1 at 100 percent power, the reactor manually tripped due to a reported fire on the isophase bus duct. The trip was uncomplicated with all systems responding normally post-trip with the exception of the 2A reactor protection system power supply, which tripped and power was transferred to the alternate source. The fire was reported extinguished at 0240 CDT on 9/26/2022. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Operations responded using the emergency operating procedure LGA-001 and stabilized the plant in Mode 3. Decay heat is removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56091 | 6 September 2022 04:45:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Trip Due to Turbine Trip | The following information was provided by the licensee via email: At 2345 CDT, Unit 1 Reactor tripped due to a turbine trip. All auxiliary feedwater pumps started due to steam generator Lo Lo levels. Unit 1 is being maintained in Hot Standby (Mode 3) in accordance with Integrated Plant Operating Procedure IPO-007A. The Emergency Response Guideline procedure has been exited. Decay heat is being rejected to the main condenser via steam dump valves. The cause of the Turbine Trip is currently under investigation. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: NRC Resident Inspector has been notified. Unit 2 is unaffected by this event. |
ENS 55975 | 4 July 2022 06:04:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Reactor Manual Scram Due to Lowering Reactor Water Level | The following information was received from the licensee via facsimile: On July 4, 2022 at 0104 CDT, with Unit 2 in Mode 1 at 100 percent power, a manual scram was inserted on U2 due to lowering reactor water level, which occurred following an unexpected closure of the 2A Feedwater Regulating Valve. Following the reactor scram, reactor water level decreased to approximately minus 16 inches, which resulted in an automatic Group II and Group III isolation (expected response). Following the scram, reactor water level rose to plus 75 inches resulting in a trip of all three Reactor Feedwater Pumps. At 0114 CDT, Reactor Water Level lowered to less than the Feedwater Pump High Level Trip setpoint and the 2C Reactor Feedwater Pump was restarted. Reactor Water Level control has been established in a normal band. The cause and details of the event are under investigation. The Unit 2 scram was not complicated. Operations responded using the Emergency Operating Procedure and stabilized the plant in mode 3. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 was unaffected by the event and remains at 100 percent power. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The licensee will notify the Illinois Emergency Management Agency. |
ENS 55964 | 25 June 2022 03:38:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Scram Due to Main Turbine Trip | The following information was provided by the licensee via email: At 2338 EDT, on June 24, 2022, with the unit in Mode 1 at 100 percent power, the reactor automatically scrammed due to an RPS actuation following a Main Turbine Trip. The cause of the turbine trip is not known at this time. The scram was not complex, with systems responding normally post-scram. Operations responded and stabilized the plant. Reactor water level has been recovered and maintained at the normal level. Decay Heat is being removed by the Main Steam system to the main condenser using the Turbine Bypass Valves. All Control Rods inserted into the core. The transient occurred with no surveillances or activities in progress. Investigation into the cause of the Turbine Trip is in progress. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The low reactor water level caused an isolation of Primary Containment (Groups 4/13/15) as expected. The Primary Containment Isolation Event is being reported under 10 CFR 50.72(b)(3)(iv)(A). There was no impact to the health and safety of the public or plant personnel. The NRC resident has been notified. |
ENS 55943 | 15 June 2022 11:24:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Trip and Automatic Auxiliary Feedwater Actuation | The following information was provided by the licensee via email: At 0724 EDT on 6/15/2022, with Unit 1 in Mode 1 at 100 percent power, the reactor was manually tripped due to lowering Steam Generator levels due to a secondary plant perturbation in the Heater Drain System. All control rods fully inserted into the core and the Auxiliary Feedwater System automatically started as designed in response to the full power reactor trip. The trip was not complex, with all systems responding normally post-trip. There was no equipment inoperable prior to the event that contributed to the reactor trip or adversely impacted plant response. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser using the condenser steam dump valves. Unit 2 is not affected and remains at 100 percent power and stable. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, this event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Auxiliary Feedwater System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 55910 | 24 May 2022 08:14:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Trip Following Manual Turbine Trip from High Vibrations on Main Turbine | The following information was provided by the licensee via email: On May 24, 2022, at 0414 EDT, while rolling the Unit 1 main turbine during the Unit 1 Cycle 31 refueling outage, the Unit 1 main turbine experienced high vibrations and the main turbine was manually tripped with reactor power at 12 percent. Main turbine vibrations persisted and the reactor was manually tripped, Main Steam Stop Valves were closed, and main condenser vacuum was broken. This notification is being made in accordance with 10 CFR 50.72(b)(2)(iv)(B), Reactor Protection System (RPS) actuation as a four (4) hour report, and under 10 CFR 50.72(b)(3)(iv)(A), specified system actuation of the Auxiliary Feedwater System, as an eight (8) hour report. The DC Cook Resident NRC Inspector has been notified. Unit 1 is being supplied by offsite power. All control rods fully inserted. Both Motor Driven Auxiliary Feedwater Pumps started properly. Decay heat is being removed via Steam Generator Power Operated Relief Valves. Preliminary evaluation indicates all plant systems functioned normally following the Reactor Trip. DC Cook Unit 1 remains stable in Mode 3 while conducting the Post Trip Review. No radioactive release is in progress as a result of this event. |
ENS 55868 | 29 April 2022 08:05:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Trip and Auxiliary Feedwater System Actuation | The following information was provided by the licensee via email: At 0405 Eastern Daylight Time (EDT), with Unit 1 in Mode 1 at 100 percent power, the reactor was manually tripped due to degrading condenser vacuum. The trip was not complex, with all systems responding normally post-trip. The Auxiliary Feedwater System started automatically as expected. Operations responded and stabilized the plant. Decay heat is being removed by the Main Steam System to the main condenser using the turbine bypass valves. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported per 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the Auxiliary Feedwater System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: No Tech Spec limits were exceeded. Offsite power is available. The suspected cause for the loss of condenser vacuum is when performing the scheduled monthly swap of condenser vacuum pumps, a suction valve failed to shut. |
ENS 55750 | 22 February 2022 03:07:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Trip | The following information was provided by the licensee via fax or email: At 2207 (EST) on 2/21/2022 with Unit 2 in Mode 1 at 68 percent power, the reactor was manually tripped due to lowering water level in the 2A Steam Generator. The trip was not complex with all systems responding normally post-trip. Operators responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Units 1 and 3 were not affected. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non- emergency notification per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."
The following information was provided by the licensee via phone and email: On 2/21/2022, Unit 2 was in Mode 1 increasing reactor power following startup from a forced outage. At 2205 (EST) with Unit 2 at 68 percent power, a feedwater control valve failed to properly control feedwater flow to the 2A Steam Generator and the Integrated Control System initiated an automatic runback. At 2207 (EST), the reactor was manually tripped from 39 percent power due to lowering water level in the 2A Steam Generator. Immediately following the manual reactor trip, an actuation of the Emergency Feedwater System (EFW) occurred. The 2A and 2B Motor Driven Emergency Feedwater (MDEFW) pumps automatically started as designed when the 'low steam generator level' signal was received for the 2A Steam Generator. The trip was not complex with all systems responding normally post-trip. Operators responded and stabilized the plant. Decay heat was removed by discharging steam to the main condenser using the turbine bypass valves. Units 1 and 3 were not affected. Unit 2 was restarted on 2/27/2022 following repairs. Due to the Reactor Protection System actuation while critical, this event was reported on 2/22/2022 as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Following further evaluation, it was determined that a valid EFW actuation occurred, therefore this event is now also being reported as a late 8-hour non-emergency notification of a valid actuation of the EFW system in accordance with 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. Notified the R2DO (Miller). |
ENS 55732 | 4 February 2022 22:00:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Scram | The following information was provided by the licensee via email: At 1700 EST, on February 4, 2022 with the unit in Mode 1 at 58 percent power, the reactor automatically scrammed due to low Reactor water level due to a transient on the Feedwater System while preparing to shutdown for a refueling outage. The scram was not complex, with systems responding normally post-scram. Operations responded and stabilized the plant. Reactor water level has been recovered and maintained at normal level. Decay Heat is being removed by the Main Steam system to the main condenser using the Turbine Bypass Valves. All Control Rods inserted into the core. The transient occurred while in the process of removing the South Reactor Feed Pump from service. While reducing speed on the South, the North Reactor Feed Pump increased in speed and tripped on low suction. The plant was preparing to shut down for a refueling outage when the trip occurred. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, in preparation of plant shutdown, Primary Containment De-Inerting was in progress. The low Reactor water level caused an isolation of Primary Containment (Groups 4/13/15). The Primary Containment Isolation Event is being reported under 10 CFR 50.72(b)(3)(iv)(A). There was no impact to the health and safety of the public or plant personnel. The NRC resident has been notified. |
ENS 55679 | 29 December 2021 20:52:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Trip and Automatic Actuation of Containment Isolation Valves | This following information was conveyed by the licensee via phone and email: At 1552 EST on 12/29/21, with Unit 1 in Mode 1 at 90 percent power, the reactor was manually tripped due to reactor pressure perturbations. The cause of the reactor pressure perturbations is under investigation. Additionally, closure of (containment isolation valves) CIVs in multiple systems occurred during the trip as a result of reaching the actuation setpoint on reactor water level. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Reactor water level is being maintained via condensate / feedwater. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 2 is not affected. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). It is also reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of CIVs. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 55641 | 10 December 2021 15:24:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Manual Reactor Trip | On 12/10/2021, at 1024 EST, with Unit 1 at 100 percent power, the reactor was manually tripped due to lowering level in the steam generators. All systems responded as expected following the trip. The reactor is currently stable in Mode 3 and operators restored steam generator level utilizing main feedwater. The cause of the reduction in feedwater flow is under investigation. St. Lucie Unit 2 was not affected and remains at 100 percent power. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) for the reactor trip. The NRC Resident Inspector has been notified. All rods inserted into the core during the trip. The plant is in its normal shutdown electrical lineup. Decay heat is being maintained by steam discharge to the main condenser using the turbine bypass valves. |
ENS 55638 | 10 December 2021 05:49:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Automatic Reactor Trip | At 0049 EST, on December 10, 2021, with Unit 2 in Mode 1 at 73 percent power, the reactor automatically tripped due to an unknown condition. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being maintained by discharge steam to the main condenser using the turbine bypass valves. Units 1 and 3 are not affected. The cause of the trip is under investigation. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)iv)(B). There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. All rods inserted into the core during the trip. The plant is in its normal shutdown electrical lineup maintaining normal operating pressure and temperature. |
ENS 55580 | 15 November 2021 22:28:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Manual Reactor Trip Due to Main Transformer Fault | At 1728 EST on 11/15/2021, with Unit 1 in Mode 1 at 47 percent power, the reactor was manually tripped due to a main transformer fault. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed by the emergency feedwater system through the main condenser. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, due to the valid actuation of the emergency feedwater system, this event is being reported as a non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Senior Resident Inspector has been notified."
At approximately 0900 (EST) on 11/16/2021, it was identified that mineral oil from the faulted main transformer had surpassed the capability of the oil containment system and discharged into Lake Monticello. It is estimated that less than 50 gallons of mineral oil entered the Lake. The oil is contained with booms and cleanup is ongoing. The EPA National Response Center and the South Carolina Department of Health and Environmental Control have been notified. This is considered a news release or notification to other government agencies; therefore, this event is reportable under 10 CFR 50.72(b)(2)(xi). The NRC Senior Resident Inspector has been notified. Notified R2DO (Miller). |
ENS 55575 | 14 November 2021 10:25:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Manual Trip Due to Lowering Main Condenser Vacuum | At 0525 EST, November 14, 2021, "Unit 2 was manually scammed by operations due to lowering main condenser vacuum. This resulted in PCIS (primary containment Isolation system) Group II/III isolation signals. All control rods inserted, and all systems operated as designed. Unit 3 is unaffected and remains at 100 percent power in Mode 1. The Resident Inspector was notified. |
ENS 55507 | 5 October 2021 10:32:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Trip and Auxiliary Feedwater Actuation | At 0632 EDT on October 5, 2021, with Unit 2 in Mode 1 at approximately 90 percent power for an end of cycle coastdown, the reactor automatically tripped due to an unexpected unblocking of the low power trip logic. The trip was not complex, with all systems responding normally post-trip. There was no equipment inoperable prior to the event that contributed to the reactor trip or adversely impacted plant response. The Auxiliary Feedwater System automatically started as designed in response to the reactor trip. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser using the condenser steam dump valves. Beaver Valley Power Station Unit 1 is unaffected and remains at 100 percent power in Mode 1. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, the automatic actuation of the Auxiliary Feedwater System is being reported as an eight hour, non-emergency Specific System Actuation per 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 55394 | 3 August 2021 14:26:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Trip | At 1026 EDT on 8/3/21, with Unit 1 in MODE 1 at 100 percent power, the reactor automatically tripped due to low reactor water level. The low reactor water level condition was due to a loss of both reactor feed pumps. The cause of the loss of feed pumps is under investigation. Additionally, the low reactor water level resulted in the automatic actuation of High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) systems, and Containment Isolation Valves (CIVs) in multiple systems. All safety systems responded normally. Operations responded and stabilized the plant. Reactor water level is being maintained via RCIC system. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 2 is not affected. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). It is also reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the HPCI and RCIC systems and CIVs. There was no impact on the health and safety of the public or plant. The Licensee notified the NRC Resident Inspector. The Unit will proceed to Mode 4 while the cause of the loss of feed pumps is under investigation. |
ENS 55370 | 21 July 2021 22:26:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Automatic Reactor SCRAM | At 1826 EDT on July 21, 2021, Susquehanna Steam Electric Station Unit 1 reactor automatically scrammed due to a trip of the Main Turbine. Unit 1 reactor was operating at 100 percent reactor power with no evolutions in progress. The Control Room received indication of a Main Turbine trip with both divisions of RPS (Reactor Protection System) actuated and all control rods inserted. The Reactor Recirculation Pumps tripped on EOC-RPT (end of cycle recirculation pump trip). Reactor water level lowered to +8 inches causing Level 3 (+13 inches) isolations. No ECCS (Emergency Core Cooling Systems) or RCIC (Reactor Core Isolation Cooling system) actuations occurred. The Operations crew subsequently maintained reactor water level at the normal operating band using Reactor Feed Water. The reactor is currently stable in Mode 3 with main condenser available. Investigation into the trip of the Main Turbine is in progress. The NRC Resident Inspector was notified. A voluntary notification to PEMA will be made. This event requires a 4 hour ENS notification in accordance with 10CFR50.72(b)(2)(iv)(B) and an 8 hour ENS notification in accordance with 10CFR50.72(b)(3)(iv)(A) and 10CFR50.72(b)(3)(iv)(B). |
ENS 55346 | 9 July 2021 01:54:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Automatic Reactor Trip Due to Main Turbine Trip | At 2154 EDT on 7/8/2021, with the Unit in Mode 1 at 100% power, the reactor automatically tripped due to trip of the main turbine, caused by failure of a non-safety related breaker during functional testing. Following the reactor trip the Steam Feed Rupture Control System automatically initiated on low Steam Generator 1 level, actuating both turbine-driven Auxiliary Feedwater Pumps. The operators subsequently started the high pressure injection pumps manually per procedure in response to overcooling indications. Operations responded and stabilized the plant. Decay heat was initially being removed via the Main Condenser. During post-trip response actions, while attempting to shut down the Auxiliary Feedwater Pumps, a low pressure condition was experienced in Steam Generator 2, resulting in isolation of the Main Condenser and steam being discharged through the Atmospheric Vent Valves for decay heat removal. There is no known primary to secondary leakage. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported in accordance with 10 CFR 50.72(b)(2)(iv)(A) as a four-hour, non-emergency notification of emergency core cooling system (ECCS) discharge into the reactor coolant system, and in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an eight-hour, non-emergency notification of an event that results in a valid actuation of the Auxiliary Feedwater System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 55320 | 21 June 2021 05:51:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Reactor Trip on Generator Lockout Relay Trip | At 0051 CDT Braidwood Unit 1 experienced an automatic reactor trip due to a generator lockout relay trip and subsequent turbine trip and reactor trip. The cause of the generator lockout relay trip is unknown at this time and is under investigation. Numerous lightning strikes were present in the area during the time of the generator lockout relay trip. Both trains of auxiliary feedwater started automatically following the reactor trip to maintain steam generator water levels. All systems responded as expected with the exception of failure of source range nuclear instruments to automatically re-energize following the reactor trip. Both source range nuclear instruments were manually energized in accordance with station procedures. The main steam dump valves are in service to the main condenser to provide heat sink cooling. The plant is being maintained at normal operating pressure and temperature. AC power is being provided by Offsite Power with the 1B Diesel Generator in standby. 1A Diesel Generator is out of service for planned maintenance. All other safety systems are available. There is no impact to Unit 2. This report is being made per 10 CFR 50.72(b)(2)(iv)(B) for a RPS actuation, 4 hr. notification, and per 10 CFR 50.72(b)(3)(iv)(A) for an automatic actuation of the Auxiliary Feedwater system, 8 hr. notification. The NRC Resident Inspector and Illinois Emergency Management Agency have been informed. |
ENS 55295 | 7 June 2021 20:27:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Automatic Reactor Trip on Turbine Trip Due to Fault and Fire in the Main Transformer | At 1527 (Central Standard Time) Unit 2 Reactor tripped caused by a turbine trip due to a fault and fire on Unit 2 Main Transformer #1. All Aux Feedwater Pumps started due to steam generator Lo-Lo levels. Unit 2 is being maintained in Hot Standby (Mode 3) in accordance with Integrated Plant Operating Procedure IPO-007B. The Emergency Response Guideline Network has been exited. Decay heat is being rejected to the Main Condenser via the steam dump valves. Fire was extinguished at 1546 without offsite assistance. No major injuries reported and no personnel transported offsite for medical attention. Cause of the fault and fire are under investigation. NRC Resident Inspector has been notified. All rods inserted into the core during the trip. There were no relief valves or safety valves lifted during the transient. The plant is stable in its normal shutdown electrical lineup via the auxiliary transformer with all safety equipment available. Unit 1 was not affected by the transient. |
ENS 55239 | 6 May 2021 16:23:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Manual Reactor Trip | On May 6, 2021 at 1223 (EDT), Unit 1 was manually tripped from 60 percent power due to degrading main condenser vacuum. Unit 1 was in the process of decreasing power due to increased secondary sodium levels identified earlier in the day. The Operations crew entered the reactor trip procedure and stabilized Unit 1 in Mode 3 at normal operating temperature and pressure. All control rods fully inserted into the core following the reactor trip. This reactor protection actuation is reportable per 10 CFR 50.72(b)(2)(iv)(B). Auxiliary Feedwater pumps actuated as designed as a result of the reactor trip and provided makeup flow to the steam generators. The automatic start of the Auxiliary Feedwater pumps is reportable per 10 CFR 50,72(b)(3)(iv)(A) for a valid actuation of an ESF (Engineered Safeguards Features) system. Decay heat is being removed by the condenser steam dump system. The electrical system is in normal lineup for shutdown conditions. There was no effect on Unit 2 operation. The NRC resident inspector has been notified. |
ENS 55078 | 20 January 2021 23:22:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | Automatic Reactor Trip Due to Trip of Motor Control Center | On 1/20/2021 at 1822 EST, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to a loss of Motor Control Center 2B2. The trip was uncomplicated with all systems responding normally post trip. Operations stabilized the plant in Mode 3. Auxiliary feed-water automatically actuated on the 2A Steam Generator post trip. Current decay heat removal is the 2B main feedwater pump to both steam generators and the Steam Bypass Control System to the main condenser. Unit 1 is not affected. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B). The NRC Resident Inspector has been notified. |
ENS 54996 | 13 November 2020 07:45:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Automatic Reactor Scram Due to High Reactor Pressure Signal | At 0245 EST on November 13, 2020, the Limerick Unit 1 reactor automatically scrammed on a valid Reactor High Pressure signal (1096psig). The Reactor High Pressure signal was caused by the closure of the 1B Inboard Main Steam Isolation Valve (MSIV), causing reactor pressure to rise, exceeding the Reactor Protection System (RPS) setpoint of 1096psig. The shutdown was normal and the plant is stable in Hot Shutdown with normal pressure control via the Main Steam Bypass Valves to the Main Condenser and normal level control using the Feedwater System. The closure of the 1B Inboard MSIV appears to have been caused by a loss of Primary Containment Instrument Gas (PCIG) pneumatic supply to the valve. The licensee notified the NRC Resident Inspector, and will be notifying Berks, Chester, and Montgomery Counties, as well as the Pennsylvania Emergency Management Agency. |
ENS 54976 | 1 November 2020 10:34:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Manual Reactor Trip Due to an Un-Isolable Leak on the Turbine High Pressure Fluid System | On November 1, 2020, at 0534 CST the reactor was manually scrammed due to an un-isolable leak on the Turbine High Pressure Fluid System. Initial power level when the leak was identified was 100 percent. Power was lowered commencing at 0525 in accordance with shutdown procedures. The Reactor Operator scrammed the reactor at 0534 from approximately 75 percent power. Following the scram, Reactor vessel water level lowered to approximately -20 inches on the Wide Range Instruments, and was subsequently recovered to normal post scram range (approximately 36 inches) using the Reactor Feedwater system. Group 2 Isolation occurred due to Reactor vessel level reaching the isolation setpoint (3 inches). The plant is stable in MODE 3 and proceeding to cold shutdown. The Main Condenser remained available throughout the evolution and condenser vacuum is currently being maintained by the Mechanical Vacuum Pumps. Pressure is being controlled using the steam line drains to the main condenser. All control rods fully inserted and there were no complications. All systems responded as designed. The Turbine High Pressure Fluid System has been secured. This event is reportable under 10 CFR 50.72(b)(2)(iv)(B) due to RPS Actuation-Critical and 50.72(b)(3)(iv)(A) Valid Specified System Actuation. The licensee has notified the NRC Resident Inspector. |
ENS 54944 | 12 October 2020 04:26:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Automatic Reactor Trip | At 0026 (EDT) on October 12, 2020, D.C. Cook Unit 2 tripped automatically on low-low level of #24 steam generator which occurred after a lowering of main condenser vacuum. The reason for the lowering main condenser vacuum and the reason for the low steam generator #24 level is under investigation. This notification is being made in accordance with 10 CFR 50.72(b)(2)(iv)(B), Reactor Protection System (RPS) actuation as a four (4) hour report. Notification is also being made as an eight (8) hour report under 10 CFR 50.72(b)(3)(iv)(A) due to actuation of the Auxiliary Feedwater System (AFW). The D.C. Cook Resident NRC Inspector has been notified. Unit 2 is being supplied by offsite power. All control rods fully inserted. Auxiliary Feedwater Pumps started as required and are operating properly. Decay heat is being removed via steam generator power operated relief valves (PORVs) due to condenser steam dump unavailability from low main condenser vacuum. All four Reactor Coolant Pumps remain running. Preliminary evaluation indicates all plant systems functioned normally following the reactor trip. D.C. Cook Unit 2 remains stable in Mode 3. No radioactive release is in progress as a result of this event. |
ENS 54888 | 8 September 2020 13:25:00 | 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation | Automatic Reactor Trip on Over Power Delta Temperature | At 0925 EDT, on September 8, 2020, with Unit 1 in Mode 1 at 100 percent power, the reactor automatically tripped on Overpower Delta Temperature. Unit 1 Channel 1 Overpower Delta Temperature was tripped as a planned evolution when an inadvertent Unit 1 Channel 2 Overpower Delta Temperature signal was received. This resulted in an automatic reactor trip. The trip was not complex, with all systems responding normally. Because of the reactor trip, the Auxiliary Feedwater (AFW) System actuated as expected due to on ATWS Mitigation System Actuation Circuitry (AMSAC) signal. Unit 2 is not affected. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser using the condenser steam dump valves. Due to the Reactor Protection System (RPS) actuation while critical, this event is being reported as a 4-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported as an 8-hour non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the AFW system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |